ML20093A386

From kanterella
Jump to navigation Jump to search
Informs That Addl Testing on Small Leakage Increase in Steam Generator B,Noted During Insp Described in , Completed.Tube 80-45 Plugged & New Plug Added Below Explosively Welded Plug
ML20093A386
Person / Time
Site: Crane Constellation icon.png
Issue date: 07/03/1984
From: Hukill H
GENERAL PUBLIC UTILITIES CORP.
To: Stolz J
Office of Nuclear Reactor Regulation
References
5211-84-2169, NUDOCS 8407100428
Download: ML20093A386 (2)


Text

.

o Nuclear L"e u e m " "

Route 441 South Middletown, Pennsylvania 17057 0191 717 944-7621 TELEX 84 2386 Writer's Direct Dial Number:

5211-84-2169 July 3, 1984 Office of Nuclear Reactor Regulations Attn: John F. Stolz, Chief Operating Reactors Branch No. 4 U. S. Nuclear Regulatory Commission Washington, D.C. 20555

Dear Mr. Stolz:

Three Mile Island Nuclear Station, Unit I (TMI-1)

Operating License No. DPR-50 Docket No. 50-289 TMI-1 Steam Generator Inspection In my letter of June 27, 1984, I described additional testing being conducted to investigate a small leakage increase in the "B" steam generator. This testing is now complete.

As reported previously, bubble testing identified only one tube as bubbling significantly, tube 80-45 in OTSG "B".

A fibrescope was placed in tube 80-45 with the secondary pressurized. Water could be seen coming through a crack at a point above the kinetic expansion joint qualified length, confirming that the leakage path was between the tube and tubesheet. This tube has been plugged.

Drip tests of the "B" steam generator identified nine plugs in the lower tubesheet, and three tubes that were dripping very slightly.

The three tubes (which included 80-45) had all been previously identified by the bubble test.

Eight of the slightly dripping plugs were rolled plugs.

Slight dripping or wetness is acceptable and not unexpected for this type of joint. A third plug was an explosively welded plug, which was repaired by placing a new plug below it.

Eddy current testing using a differential probe has now been conducted for all tubes identified as bubbling, all tubes with less than 40 percent through wall indications left in service in the "B" generator, and approximately seventy other tubes in the "B" generator which are part of the supplemental ECT sample population. No new eddy current indications were found. No kn

..n indications were found to have grown. No tubes that were bubbling have any ECT indications below the kinetic expansion joint, confirming that bubbling is past the joint in all cases. No additional ECT is planned.

0407100428 840703 f)8f PDR ADOCK 05000289 G

PDR GPU Nuclear Corporation is a subsidiary of the General Public Utilities Corporation E

I One very low voltage ECT signal was noted by data analysts in tube 70-8 in the "B" generator, six inches above the lower face of the upper tube sheet.

A review of previous inspections showed a signal of the same shape and voltage at that location for both pre-and post-expansion inspections, indicating that this signal does not represent a new or growing defect.

This size and type of signal, which is very close to the threshold of detectability of the probe in use, cannot reliably be distinguished from background using this probe.

This threshold of detectability has been considered and found acceptable in GPU's evaluation of the steam generators. When such small signals are identified, additional inspections using the more sensitive 8x1 probe are normally conducted to determine whether the anomalous signal represents an ECT indication or simply part of background. The additional time necessary to prepare equipment and to carry out this inspection is not considered warrented for one tube. Rather than leave the steam generators open to oxygen for the additional time period this tube will be plugged as a precautionary measure.

In addition to the two tubes described above, GPU plans to plug one additional tube in the "B" generator, tube 79-41.

This is one of the slightly bubbling tubes identified in my June 27, 1984 letter. Although it bubbled so slightly that the water surface above remained undisturbed, bubble formation at the tube surface appeared somewhat more frequent than for other slight bubblers.

In the interest of maintaining secondary activity levels as low as possible, this tube is being plugged.

GPU's investigations of the small leakage increase are now complete, and

~

plugging is complete. The steam generators will be closed and returned to service this week. All evidence continues to support the conclusions drawn in GPU's submittals on the acceptability of the steam generators for return to service.

Baseline leakage will be re-established, as require after plugging, prior to criticality.

Sincerely, kill Vice President - TMI-1 HDH/MJG/ RAS /mle cc:

R. Conte J. Van Vliet

_ _