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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217F8011999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of McGuire Nuclear Station.Areas That Warranted More than Core Insp Program Over Next Five Months,Not Identified.Historical Listing of Plant Issues Encl ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F8231999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of Catawba Nuclear Station.Based on Review,Nrc Did Not Identify Any New Areas That Warranted More than Core Insp Program Over Next Five Months.Historical Listing of Issues,Encl ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20212J7801999-10-0404 October 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for McGuire NPP & 990615.Informs That NRC Reviewed Responses & Concluded That All Requested Info Re Y2K Readiness Provided.Subj GL Considers to Be Closed ML20212J2191999-10-0404 October 1999 Informs That Util 980326 Response to GL 97-06, Degradation of SG Internals Provides Reasonable Assurance That Condition of Steam Generator Internals Are in Compliance with Current Licensing Bases for Facility ML20217C4471999-10-0404 October 1999 Forwards Insp Repts 50-369/99-06 & 50-370/99-06 on 990801- 0911.Determined That One Violation Occurred & Being Treated as Non-Cited Violation ML20212J3011999-10-0101 October 1999 Forwards Exemption from Certain Requirements of 10CFR54.17(c) Re Schedule for Submitting Application for Operating License Renewal.Se Also Encl ML20217K2651999-10-0101 October 1999 Forwards Retake Exams Repts 50-413/99-302 & 50-414/99-302 on 990921-23.Two of Three ROs & One SRO Who Received Administrative Section of Exam Passed Retake Exam, Representing 75 Percent Pass Rate 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments ML20217A7911999-09-24024 September 1999 Forwards Insp Repts 50-413/99-05 & 50-414/99-05 on 990718- 0828 at Catawba Facility.Nine NCVs Identified Involving Inadequate Corrective Actions Associated with Degraded Svc Water Supply Piping to Auxiliary Feedwater Sys ML20212E6471999-09-24024 September 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for Catawba NPP & 990615.Informs That NRC Reviewed Response for Catawba & Concluded That All Requested Info Provided.Considers GL 98-01 to Be Closed for Catawba ML20212M1651999-09-23023 September 1999 Refers to 990917 Meeting at Region II Office Re Licensee Presentation of self-assessment of McGuire Nuclear Station Performance.List of Attendees & Licensee Presentation Handouts,Encl ML20212F0941999-09-21021 September 1999 Discusses Closeout of GL 97-06, Degradation of Steam Generator Internals for Cns,Units 1 & 2 ML20212M2001999-09-20020 September 1999 Confirms 990913 Telcon Between M Purser & R Carroll Re Management Meeting to Be Conducted on 991026 in Atlanta,Ga to Discuss Operator Licensing Issues 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D1671999-09-20020 September 1999 Forwards Exemption & SER from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Re Isolation of Main Steam Branch Lines Penetrating Containment.Exemption Related to Licensee Application ML20212B6491999-09-15015 September 1999 Informs That Encl Announcement Re 990913 Application for Amend to Licenses NPF-9 & NPF-7 Forwarded to C Observer in North Carolina,For Publication ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212M1931999-09-13013 September 1999 Refers to 990909 Meeting Conducted at Region II Office Re Presentation of Licensee self-assessment of Catawba Nuclear Station Performance.List of Attendees & Licensee Presentation Handout Encl ML20212A3751999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementation Code Case for Duration of Insp Interval ML20212A0501999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementing Code Case for Duration of Insp Interval ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211J3671999-08-31031 August 1999 Forwards Public Notice of Application for Amend to License NPF-9 Seeking one-time Extension of Surveillance Frequency for TS SR 3.1.4.2 Beyond 25% Extension Allowed by TS SR 3.0.2 ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211K8831999-08-26026 August 1999 Forwards Insp Repts 50-369/99-05 & 50-370/99-05 on 990620-0731.Two Violations Occurred & Being Treated as NCVs ML20211M8191999-08-25025 August 1999 Confirms 990825 Telcon Between G Gilbert & R Carroll Re Mgt Meeting to Be Held on 990909 in Atlanta,Ga,To Allow Licensee to Present self-assessment of Catawba Nuclear Station Performance 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211G5181999-08-24024 August 1999 Forwards SE Re second-10-yr Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211A9641999-08-20020 August 1999 Forwards SE Authorizing Licensee 990118 Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section XI for Plant,Units 2 ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20196E9541999-06-18018 June 1999 Forwards SG Tube Insp Conducted During Unit 1 End of Cycle 11 Refueling Outage.Attachments 1,2,3 & 4 Identify Tubes with Imperfections in SGs A,B,C & D,Respectively ML20195K4571999-06-14014 June 1999 Forwards MORs for May 1999 & Revised MORs for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195J1691999-06-10010 June 1999 Forwards Written Documentation of Background & Technical Info Supporting Catawba Unit 1,notice of Enforcement Discretion Request Re TS 3.5.2 (ECCS-Operating),TS 3.7.12 (Auxiliary Bldg Filtered Ventilation Exhaust Sys) ML20217G5771999-06-0909 June 1999 Forwards Post Exam Comments & Supporting Reference Matls for Written Exams Administered at Catawba Nuclear Station on 990603 1999-09-09
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- jrnta;] tiil DUKEPOWER February 27,1992 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555
Subject:
McGuire Nuclear Station Unita 1 and 2 Docket Nos. 50-369/370 Catawba Nuclear Station Units 1 and 2 Docket Nos. 50-413/414 Response to Generic Leiter 91-13 Essential Service Water System Failures at Multi-Unit Sites Gentlemen:
On September lit,1991 the NRC issued Generic Letter 91-13 requesting information from .
licensees at affected multi-unit sites regarding the Loss of Essential Service Water System (ESWS) postulated event.
The Generic Letter proposes that the Licensee implement certain administrative improvements such as. Technical Specification amendments and emergency procedure upgrades in order to enhance the availability of the ESWS. While enhancements for both stations have been ' identified, Duke Power has determined that existing Technical ,
Specifications for McGuire and Catawba adequately ensure the availability of their respective Essential Service Water systems.
Accordingly, please find our attached response to the Generic Letter for McGuiie and Catawba Nuclear Stations. If there are questions concerning our response, please contact Allison D. Jones at (704) 373-2026.
I declare under penalty of perjury that these statements are true and correct to the best of
!: mj knowledge, l
p Very truly yours, 1 ,
,a Cf/ /j ~ #
/ -
H. B. Tucker Senior Vice President Nuclear Generation ,
9203020311 920227 hJ l PDR. ADOCK 05000369 l P PDR
U.S,NRC Page 2 February 27,1992 Attachment xc: S. D. Ebneter Regional Administrator, Region II T. A. Reed, ONRR R. E. Martin, ONRR P, K. VanDoorn Senior Resident Inspector.
9 W. T. Orders Senior Resident Inspector
.- = . .- .-~ _ - - - .
4 4
DUKE POWER COMPANY RESPONSES TO GENERIC LETTER 91-13 McGUIRE AND CATAWDA NUCLEAR STATIONS
- 1. INTRODUCTION Generic Issue 130, " Essential Service Water System Failures at Multi-Unit Sites," was initiated to investigate concerns regarding the Essential Service Water (ESW) system at multi-unit reactor sites th :c contained two ESW trains per unit and crosstie capability between units ESW Systems. It was found that this crosstie feature enhanced operational flexibility and would reduce the consequences associated with a loss of ESW crent.
Insights from the evaluation indicated that the core damage.
frequency associated with a loss of ESW event was highiv sensitive to the reliability and availability of this crosstic feature. Based on the results of these evaluations, the NRC staff has. decided that improvements to existing Technical Specifications, testing procedures, and emergency procedures may be warranted for certain plants based on the safety benefit derived and the cost of implementation. Generic Letter 91-13 forwarded the recommended Technical Specification and procedure improvements and requested information regarding the applicability, and implementation of the proposed improvements.
- 2. MCGUIRE RESPONSE 2.1 McGuire Nuclear Service Water (RN) System At McGuire the Essential Service Water System is referred to as the Nuclear Service Water (RN) System. McGuire Units 1 and 2 cach have a two-pump train RN System which provides cooling for many plant loads. The RN System is an open-loop system which normally takes suction from Lake Norman and discharges to the Condenser Circulating Water (RC) System discharge piping which leads back to the lake. The RN Systems are normally isolated between units but do contain cross-connect piping and normally shut manual valves which can be opened to cross-connect RN between units in the case of an emergency. Normal power operations require one pump train to be in operation providing cooling for all normal essential and non-essential loads for that unit. The other RN pump train is normally in standby and would be started autonatically following a blackout, a safety injection (SS) signal, starting of a motor driven Auxiliary Feedwater (CA) pump, I and by procedure following indication of insufficient RN flow.
At McGuire,.the Containment Ventilation Cooling Water (RV) System can deliver adequate backup cooling water in the event of a loss of the normal RN flow. The McGuire Inservice Testing program (IWV) requires those valves necessary for the proper RV to RN alignment to be tested quarterly. McGuire also has an independent
r-GL 91-13 Response Page 2 Standby Shutdown Facility (SSF) which contains a dedicated makeup pump to supply injection flow to the Reactor Coolant (NC) pump seals in the event of a loss of all normal seal cooling.
2.2 Probabilistic Risk Assessment Results Results from the McGuire Probabilistic Risk Assessment (PRA) study (MNS IPE Submittal Report, Nov., 1991) indicate that the core melt frequency resulting from the loss of RN event is approximately 1E-05/yr. Credit is taken in the PRA for recovering from this loss of RN event by either (i) aligning the. containment Ventilation Cooling Water (RV) System to provide cooling water backup through the RN non-essential header, (ii) cross-connecting to the other units RN System to provide cooling water, or (iii) activating the SSF standby makeup pump to provide NC pump seal cooling.
Failure for cross-connecting to the other unit's RN System is d'minated by the human error associated with performing the alignment in a timely manner. Human error also dominates the reliability of the RV backup and SSF alignment.
2.3 Applicability of Recommended Technical Specification and Procedural Changes McGuire currently has Technical Specifications (Tv; covering allowed outage times for RN trains while in Modes 1 through 4 (TS 3/4.7.4). Additionally, Technical Specifications for Residual Heat Removal (RHR) System requirements in Modes 5 and 6 (TS 3/4.1.4 and 3/4.9.8) and Diesel Generator (DG) requirements in
' Modes 5 and 6 (TS 3/4.8.1.2) adequately ensure availability of RN while in these modes since the operability of the required RHR and DG trains depend on the availability of the associated RN train. McGuire has developed an operability Test for the manual RN crossover isolation valves to be performed during Unit i refueling outages. The McGuire Loss of RN procedure already provides guidance (including valve locations) for manipulating the RN crosstic between units during a loss of RN accident.
Generic. Letter 91-13 evaluations assume that the Essential Service Water system crosstle feature is the only means of combating a loss of-service water event. However, McGuire has two other systems which mitigate the consequences of a loss of RN event. The RV System can provide adequate backup cooling to RN System loads. Also, the'SSF standby makeup pump provides an independent means of supplying NC pump seal cooling which will prevent NC pump seal degradation. The current Loss of RN procedure contains guidance for aligning both of these systems.
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t GL.91-13 Response Page 3 As-a result of these design features, McGuire is not solely dependent-on the RN crosstle feature for preventing core melt following a loss of RN ovent.
Thus, imposing the additional specifications does not appear justified _since (i) the current specifications adequately ensure RN availability in all modes, (ii) the reliability of the cross-connect feature is dominated by human-error and not the availability of the other unit's RN System, and (iii) there are two backup-systems (RV and SSF) which can mitigate the consequences of a loss of RN event. Based on these facts, additional RN System Technical Specification requirements would not1 reduce the calculated core melt frequency at McGuire.
2.4 Proposed Actions McGuire has developed an Operability Test for the RN crossover isolation valves (Valve #'s 1RN-33, 34, 36, & 38)
(PT/1/A/4700/64). This test will be performed during each Unit I refueling outage.
McGuire will perform a one time flush of the stagnant RN piping between the crosstic valves to evaluate the existence of sedinentation and loose tubercles. Two wet taps to allow videoscope inspection for this section of piping will be installed. These actions will be completed during the Unit 1 EOC-8 refueling outage.
McGuire has reviewed the adequacy of the Loss of RN procedure (AP/1/A/5600/20) concerning the alignment of the RV System, steps for opening the RN crosstle valves, and SSF activation guidance, and has-concluded that the procedure contains sufficient detail for performing these tasks.
Examination of the existing Technical Specifications indicates that the current Technical Specifications are adequate to provide reasonable assurance that=the other unit's RN System would be available during conditions involving the limited period of Modes 5 and 6 operations. No change to the current Technical Specifications is necessary in response to this Generic Letter.
2.5 Bases for Resolution McGuire has_several design and operational features which reduce the consequences resulting from a loss of RN event. First, the RN System at_McGuire can receive backup cooling flow from the RV System. This system is aligned to the RN non-essential header but can deliver adequate flow to the RN essential loads. The RV System contains three 3200 gpm pumps which will start automatically on low RN System pressure. Second, McGuire has an I
GL 91-13 Responso Page 4 independent backup system, the SSF, which contains a dedicated makeup pump to supply injection' flow to the NC pump-scals. The Loss of RN procedure directs the operators to (1) ensure that the RV System is providing sufficient flow, (ii) align to the other unit's RN System through the system crosstie if insufficient RN flow exists, and (iii) activate the SSF if all seal cooling is lost. As a result of these design features, McGuire is not solely dependent on the RN crosstie feature for preventing core melt following a loss of RN event. Imposing additional Technical Specifications will not result is a decrease in the calculated core melt frequency since credit for this crosstic feature is dominated by human error and not system availability, and credit for the other backup systems (RV and SSF). reduce the consequences of a loss of RN ovent.
The McGuire Selected Licensee Commitments (SLC) Manual provides a single location within the FSAR where certain selected licensee commitments are presented. The content is based on the results of application of a set of criteria to determine the content of technical specifications. Those previous technical specification requirements which did not meet the criteria are located in this manual. The SLC Manual includes requirements for ensuring the SSF is available for each unit in operation. These requirements include quarterly testing of the Standby Makeup pump. McGuire also has Technical Specifications covering allowed outage times for RN-trains while in Modes 1 through 4. Additionally, Technical Specifications for Residual Heat Removal system and emergency DG requirements in Modes 5 and 6 adequctely ensure availability of RN while in these modes.
- 3. CATAWBA RESPONSE 3.1 Catawba Nuclear Service Water (RN) System-At Catawba,'the Essential Service Water System is referred to as the Nuclear Service Water (RN) System. The RN System at Catawba is shared between the two units. The RN System is an open-loop system with 4 pumps which normally take suction from Lake Wylie and discharge to the Conventional Low Pressure Service Water (RL)
System piping which leads back to the lake. Normal power operations typically require 1 RN pump to be in operation providing cooling for all normal essential and non-essential j loads for both units. The-other three RN pumps are normally in standby and will start automatically following a blackout, a-safety injection (SS) signal, low-low RN pump pit level, and by
_ procedure following indication of insufficient RN flow.
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l GL 91-13 Response Page 5 Catawba also has an independent Standby Shutdown Facility (SSF) which contains a dedicated makeup pump to supply injection flow to the Reactor Coolant (NC) pump seals in the event of a loss of all normal seal cooling.
3.2 Applicability of Recommended Technical Specification and Procedural Changes Generic Letter 91-13 evaluations assume that (i) the essential service water system crosstic feature is the only means of combating a loss of service water event, and (ii) the essential service water systems for each unit are independent and normally isolated. The Generic Issue 130 (GI-130) assessment is applicable to multi-unit sites where each unit has an independent service water system. The calculated core melt frequency of these plants was found to be affected by the ability to cross-connect to the other unit in the event of a loss of service water on one unit.
This system arrangement does not apply to Catawba and therefore the evaluation results of GI-130 are not directly applicable. The RN System at Catawba is normally operated in a shared configuration. One RN pump normally supplies adequate cooling to both units RN loads. The isolation valves to unit specific RN headers in use are normally open with power removed. Should a loss of RN event occur, the SSF can be activated to provide NC pump seal cooling and thus prevent a potential seal LOCA. Based on the above discussions, the new additional Technical Specification requirements identified in Generic Letter 91-13 are not applicable to Catawba.
Operability and testing of these unit specific RN isolation valves is currently required. Technical Specifications concerning the system requirements in various operational modes currently exist (TS 3/4.7.4).
The Loss of RN procedure is being updated to include guidance for reopening valves that may have transferred closed (including unit specific RN isolation valves) and activating the SSF following a complete loss of RN in order to prevent an NC pump seal LOCA.
3.3 Proposed Actions Catawba is improving the Loss of RN procedure to include guidance for ensuring unit isolation valves and discharge valves are open, and for activating the SSF in a timely manner. This action will be completed by October 1, 1992.
Examination of the existing Technical Specifications indicates that the current Technical Specifications are adequate for ensuring operability of the crosstie valves and provide assurance that an adequato number of RN pumps would be available during
4 GL 91-13 Response Page-6 conditions involving the limited period of Modes 5 and 6 operations.- No change to the current Technical Specifications is necessary in response to this Generic Letter.
3.4 Bases for Resolution Catawba's RN System is shared between units and normally operates with the unit specific isolation valves open. Thus, any of the 4 RN pumps can provide flow te either units RN loads. During normal power operation, 1 RN pump is sufficient for meeting all RN flow requirements on both units. Catawba has an independent facility, the SSF, which can provide backup cooling to the NC pump seals and prevent a seal LOCA, thereby mitigating the consequences of a loss of RN event. Technical Specifications are in place for ensuring the SSF is available (TS 3/4.7.13), and include quarterly testing requirements for the Standby Makeup pump.
Catawba has Technical Specifications in place that cover the RN System requirements in various operational modes that adequately ensure the availability of RN while in Modes 5 and 6.
Operability and testing of these unit specific RN isolation valves is currently required. The Loss of RN procedure is being updated to include guidance for opening or reopening unit specific isolation valves and activating t!.e SSF in a timely manner.
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