ML20087M673
| ML20087M673 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 02/29/1984 |
| From: | Brons J, Kelly L POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| IP-LK-881, NUDOCS 8403300159 | |
| Download: ML20087M673 (7) | |
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OPERATING DATA REPORT DOCKET NO.
50-236 DATE 03 /01/94 COMPLETED BY L-Kellv TELEPHONE (914) 739-8200 OPERATING STATUS
- 1. Unit Name: Indian Point No. 3 Nuclear Power Plant bOI'8
- 2. Reporting Period:
Februarv 1984
- 3. Licensed Thermal Power (MWt):
3025
- 4. Nameplate Ratir;(Gross MWe):
1013
- 5. Design Electrical Rating (Net MWe):
965
- 6. Maximum Dependable Capacity (Gross MWe):
1000
- 7. Maximum Dependable Capacity (Net.MWe):
965
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Remons:
- 9. Power Level To Which Restricted,If Any (Net MWe):
- 10. Reasons For Restrictions.If Any:
This Month Yr.-to-Date Cumulative
- 11. Hours in Reporting r'eriod 696 1440 65,761
- 12. Number Of Hours Reactor Was Critical 691.3 753.1 35,177.6
- 13. Reactor Resene Shutdown Hours 0
0 0
- 14. Hours Generator On.Line 667.6 667.9 33,809.9
- 15. Ur.it Reserve Shutdown Hours 0
0 0
- 10. Gross Thermal Energy Generated (MWH) 1.542.818 1,543,241 87,968,886
- 17. Gross Electiical Energy Generared (MWH) 482.660 482.665 26,849,275
- 18. Net Electrical Energy Generated (MWH1 460,451 460,451 25,704,629
- 19. Unit Service Factor 95.9 46.4 51.4
- 20. Unit Availability Factor 95.9 46.4 51.4
- 21. Unit Capacity Factor (Using MDC Net) 68.6 33.1 40.5
- 22. Unit Capacity Factor (Using DER Net) 68.6 33.1 40.5 1.7 53.1 24.5
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each1:
8403300159 840229 PDR ADOCK 05000286 m9 R
PDR yi l-25 If Shur Down At End Of Report Period. Estimated Date of Startup:
l 26 Units In Test Status iPrior to Commercial Operation):
Forecast Achieved i
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i INITIAL CRITICALITY INITIA L ELECTRICITY COMMERCIAL OPERATION.
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-286 Indian Point UNIT No. 3 DATE 03/01/84 COMPLETED BY L. Kelly TELEPHONE (914) 739-8200 MONTH February 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL t MWe-Net)
Mwe-Net)
I 94 815 37 2
172 gg 816 3
175 g9 818 4
183 20 662 5
409 21 69 6
499 33 782 7
609 812 23 8
581 24 864 9
500 25 928 10 793 26 927 11 816 37 928 12 813 929 7g 13 813 931 29 14 815 30
~
IS 33 16 816 l
INSTRUCTIONS 4
On this format, list the average daily unit power level in MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.
1 (9/77)
50 2Hf>~
DOCKE1?lo.
UNII SilU1 DOWNS /.ND POWER REDUC 1 IONS UNIT NAME N -
DATE COMPLETED llY REPORT MON 111 Fohrunry 1984 fELErilONE 914-739-8200
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j.E 5 1.icensee E,
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Cause & Cosrective No.
Date g
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_g s 5 Event 37 Action -
gV fE y
j;g l' ipos #
cn V Psevent Recurrence H
g d
01 840201 S
6.13 B'
N/A N/A ZZ ZZZZZZ Unit removed from service for Turbine Overspeed Trip Test.
02 840209 F
4.58 A
3 N/A HH INSTRUC Reactor Trip caused by trip of #31 &
- 32 Heater Drain Tank Pumps.
03 840220 F
7i00 A
3 N/A IIH VALVOP P
- 32 Steam Generator Low Level Mis-match caused by a failed Feedwater Regulating Valve Solenoid.
j 04 840221 F
10.65 B
N/A N/A ZZ ZZZZZZ Repairs to drain line on feedwater discharge header.
I i
1 t
l I
2 3
4 F: Forced Reason:
Metimd:
Exinhit F-Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Picparation of Data it Maintenance of Test 2-Manual Scram.
I nisy Sheets for 1.icensee C Refueling
- 3. Automatic Ser.am.
lisen Repois (I I R)I sie (NtlRIL D-Regulatory Restriction 4-Other (lixplain) 0161) li-Operator Training & License lixamination F Administrative 5
G-Operational E:ror (lixplain)
ITinbit H-Same Source (9/77)
Il-Other (lixplain )
MONTHLY MAINTENANCE REPORT February 1984 MONTH WR#
DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION 3743 2/03/84 Service Water Zurn Thermal overloads tripping Replaced fuses and reset Strainers #31,32,35 and thermal overloads 36 3832 2/03/84 Fuel Storage Building Drive motor trips Realigned drive mechanism Sliding Door 4177' 2/03/84 Spent Fuel Pit Cooling Oil leak Tightened loose pipe fitting Pump #32.
4195 2/10/84 Charging Pump #33 Packing leaks Repacked pump 4103 2/11/84 Primary Water Valve 552 Improper position indication Replaced Limit Switch 4204 2/17/84 Charging Pump #32 Recirc-Packing leaks Replaced valve ulation Valve 276 3453 2/22/84 PAB-VC Exhaust Fan #31 Belts broken Replaced belts 4196 2/22/84 Charging Pump #32 Relief Valve leaking Replaced valve Valve 234 4242 2/28/84 Charging Pump #32 Packing leaks Repacked pump
~. _..
MONTHLY I-& C REPORT February 1984 Month
~ W.R. #-
DATE EQUIPMENT.
MALFUNCTION CORRECTIVE ACTION
- IC-1-1759 2-08-84 Reactor. Coolant Pump #33 Improper indication Replaced RTD Seal. Outlet RTD
>IC-1-2408~
' 2-08-84 Steam Generator Blowdown Improper indication Re' paired cracked cable i
~ Radiation Monitor R-19 3
. 2-28-84L
' Instrument Bus #31 Inverter Improper output on Replaced defective normal supply diode and blown fuse h
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SUMMARY
OF OPERATING EXPERIENCE FEBRUARY 1984 Indian Point Unit 3 was synchronized to the bus for a total of 667.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, providing a gross generation of 482,660 Mwe for this reporting period.
On February 1, at 1134 hours0.0131 days <br />0.315 hours <br />0.00187 weeks <br />4.31487e-4 months <br /> the unit was removed from service for a scheduled turbine overspeed trip test.
The test was successful and the unit was returned to service at 1742 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.62831e-4 months <br />.
The unit tripped at 1118 hours0.0129 days <br />0.311 hours <br />0.00185 weeks <br />4.25399e-4 months <br /> on February 9, because condensation accumulated in the instrument air to a level controller which led to a temporary loss of #31 and #32 heater drain pumps. The air regulator was orificed to provide for a constant air blowdown and the unit was returned to service at 1553 hours0.018 days <br />0.431 hours <br />0.00257 weeks <br />5.909165e-4 months <br />. A failed feedwater regulating valve solenoid led to a unit trip at 1945 hours0.0225 days <br />0.54 hours <br />0.00322 weeks <br />7.400725e-4 months <br /> on February 20.
Repairs were completed and the unit was returned to service at 0245 on February 21.
The unit was intentionally removed from service at 0812 hours0.0094 days <br />0.226 hours <br />0.00134 weeks <br />3.08966e-4 months <br /> on February 21 for repairs to a 3/4" drain line on the feedwater discharge header. Repairs were completed and the unit was returned to service at 1851 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.043055e-4 months <br />.
t
I Indian Point 3 Nuclear Power Plant P.O. Box 215 Buchanan, New Wrk 10511 914 739.8200
- > NewYorkPbwer 4# Authority March 15, 1984 IP-LK-881 Docket No. 50-286 License No. DPR-64 Director, Nuclear Reactor Regulation Office of Management Information and Program Control U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Dear Sir:
Enclosed you will find two copies of the monthly operating report relating to Indian Point 3 Nuclear Power Plant for the month of February,1984.
Very truly yours, ohn. Brons Resident Manager LK/bam Enclosure cc: Director, Office of Inspection & Enforcement (40 Copies) c/o Distribution Services Branch, DDC, ADM U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Dr. Thomas E. Murley, Regional Administrator Region 1 U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 i
i IP3 Resident Inspectors' Office
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George Wilverding (SRC), WPO l
J. P. Bayne, WPO S. V. Fuller, NYO g
W. R. Yario, NYO INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta,' Georgia 30339