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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML17309A6211997-09-29029 September 1997 Part 21 Rept Re Final Disposition of Masterflow 713 & Embeco 636 Grout Nonconformance Reported by Master Builders,Inc. Licensee Continuing to Monitor shelf-life of Masterflow 713 & Embeco 636 Grouts Produced at Rancho Cucamonga ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20127D1491992-09-0404 September 1992 Part 21 Rept Re Defect in Component of DSRV-16-4 Enterprise Standby DG Sys Jacket Water Pump Shaft.Caused by Incorrect Tapers Machined on Shaft Due to Vendor Mismatching.All Affected Shafts Recalled & Quality Insp Plans Changed ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20087D3191992-01-14014 January 1992 Potential Part 21 Rept Re Problems W/Elmwood/Fasco Contactor Carriers Breaking in Contactor Model 30-FO-30. Caused by Distortion/Shrinkage of Molded Phenolic Contactor Carrier.Replacement Contactors Installed ML17223A5941990-03-0909 March 1990 Errata to 900126 Part 21 Rept Re Anchor/Darling Actuators Incorporating Use of Teldyne-Republic four-way Valves.Lists Plants Inadvertently Left Out in Original Rept ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating ML20246K7401989-04-26026 April 1989 Part 21 Rept Re Incorrectly Stamped Name Plates on Certain Asco Nuclear Qualified Valves.Vendor Will Contact Each Affected Facility & Furnish Correctly Stamped Plates & in Near Future Discontinue Sale of Rebuild Kits for Valves ML20247P7991989-04-0404 April 1989 Part 21 Rept Re Atmospheric Dump Valves.Cause of Failure Speculative But Result of Piston Ring That Failed to Seal. Resolution to Problem Requires Increasing Pilot Valve Capacity & Reworking of Plug to Enlarge Pilot Flow Area ML20206M4401988-11-21021 November 1988 Deficiency Rept Re Misapplication of Raychem Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880920.Investigation Is in Process.Final Rept Will Be Submitted by 881222 ML20205C9291988-10-18018 October 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow,Per 10CFR21 & 50.55 Requirements.Item Being Tracked by MTS EAI B-5115 & Scheduled for Completion 881030 ML20205D6651988-10-18018 October 1988 Part 21 & Deficiency Rept Re Penetration Seals Found Not to Be Watertight.Initially Reported on 880609.Water Leakage Tests Performed on Unit Upper Cable Spreading Room Seals. All Floor Penetration Seal Assemblies Repaired ML20207P0451988-10-0505 October 1988 Part 21 Rept 146 Re Defect in Left Intercooler Inlet Adapter on Standby Diesel Engine Generator.Recommends Utils Inspect Left Intake Manifold Drain as Part of Operating Plan.Addl Info Expected by 881015 ML20155D6471988-09-28028 September 1988 Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880629.Final Rept Delayed Until 881020 ML20207J7361988-09-20020 September 1988 Interim Deficiency Rept Re Misapplication of Vendor Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880601.Final Rept Expected Prior to 881123 ML20153E2271988-09-0101 September 1988 Part 21 & Deficiency Rept Re ESF Filtration Unit Bolts. Initially Reported on 880628.Contractor Conducted Training Session for Personnel to Stress Importance of Clarifying Incomplete Drawing Info & Requirements of Bolting Procedure ML20151V1901988-08-16016 August 1988 Deficiency Rept Re non-water Tight Penetration Seals.Test Rig Constructed to Simulate Typical Upper Cable Spreading Room Configuration & Sealants Verified to Provide Waterproof Seal.Next Rept Will Be Submitted by 881020 ML20196L4811988-07-0707 July 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880601.Investigation in Progress to Determine Full Scope of Condition.Final Rept Will Be Submitted by 881001 ML20151A7781988-07-0606 July 1988 Deficiency Rept Re nonwater-tight Penetration Seals. Initially Reported on 880609.Investigation Incomplete.Next Rept Expected by 880818 ML20196C2971988-06-28028 June 1988 Deficiency Rept Re ESF Filtration Bolts.Initially Reported on 880601.Investigation of Root Cause of Condition Ongoing. Final Rept Will Be Submitted by 880901 ML20195D8541988-06-16016 June 1988 Part 21 Rept Re Potentially Reportable Condition Associated W/Dresser Model 7440W Check Valves Supplied W/Flow Direction Arrow Stamped Opposite to Valve Flow.Investigation Being Conducted.Evaluation of Bechtel Western Power Co Ltr Encl ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML20154A6841988-05-10010 May 1988 Deficiency Rept Re Electrical Cable Tray Separation. Initially Reported on 880414.Walkdown of All safety-related Cable Trays Conducted to Ensure Any Unacceptable Separation Distance Identified ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20151K2621988-04-14014 April 1988 Interim Deficiency & Part 21 Rept Re Control Room Essential HVAC Sys.Initially Reported on 870914.Addl Concern Noted Re Incorrect Assumption in Design Calculation.Corrective Action Beyond Calculation Review Involves Logic Mod ML20151K2371988-04-14014 April 1988 Part 21 & Deficiency Rept Re Damage to Emergency Diesel Generator Jacket Water HX During Flushing.Initially Reported on 860917.HX Repaired & Installed in Unit 2.Thermostatic Valves Being Modified ML20148R6441988-01-27027 January 1988 Part 21 & Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies Fabricated by Conax Buffalo Corp.Initially Reported on 871203.LOCA Could Cause One or More of nonsafety-related Circuits to Short Circuit ML20237E9941987-12-22022 December 1987 Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies (Epa).Initially Reported on 871203. Investigations in Progress.Final Rept Will Be Submitted by 880130 ML20236V2981987-11-19019 November 1987 Deficiency Rept Re Electrical Separation Criteria Specified in Const Spec X3AR01.Initially Reported on 870909.Second Test of Electrical Separation Requirements Very Positive. Final Rept Expected to Be Submitted Prior to 880301 ML20236K1431987-11-0202 November 1987 Interim Part 21 & Deficiency Rept Re Inductive Current Interruptive Capacity of Solid State Protection Sys Motor Driven Relay Contacts.Shunt Suppression Device Will Be Added to Solenoid ML20236J5371987-10-29029 October 1987 Part 21 & Deficiency Rept Re Solid State Protection Sys motor-driven Relay Contacts Inductive Current Interruptive Capacity.Initially Reported on 870110.Hardware Mods to Affected Circuits Planned Prior to Fuel Load ML20239A2111987-09-14014 September 1987 Part 21 & Deficiency Rept Re Design of Control Room Essential (CRE) HVAC Sys.Initially Reported on 870713. Backdraft Dampers Added to Unit 1 CRE HVAC Units & Will Be Added to Unit 2 Commensurate W/Const Schedule ML20237H7741987-08-12012 August 1987 Interim Deficiency Rept Re Emergency HVAC Sys in Control Room.Initially Reported on 870713.Engineering Evaluation in Progress to Determine Potential Impacts of Condition on Plant Safety.Final Rept Will Be Submitted by 870915 ML20216E4721987-05-28028 May 1987 Part 21 Rept 140 Re Potential Defect in Air Pressure Regulators Mfg by Bellofram.Dripwell Gasket May Fail Due to Mismachining of Gasket Seating Surface Causing Loss of Control Air & Starting Air Pressure 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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te 2, Waynesboro. Georgia 30830 Telephone 404 554-9961 404 724 8114 N MM 15 A 8 : 38 Vogtle Project March 9,1984 United States Nuclear Regulatory Commission File: X7BG03-M51 Office of Inspection and Enforcement Log: GN-327 Region II-Suite 3100 101 Marietta Street Atlanta, Georgia 30303
Reference:
Vogtle Electric Generating Plant-Units 1 and 2, 50-424, 50-425; Pullmcn Power Products-Fabrication Shop Spool Piece Welds; also GN-286, dated 11/21/83.
Attention: Mr. James P. O'Reilly Centlemen:
In our previous correspondence to the NRC, Georgia Power Company indicated that the NRC would be notified by March 9,1984, of the results of our evaluation of visual defects found in pipe spool welds performed in the Pullman Power Products Fabrication Shop. Georgia Power Company has completed its review and evaluation of this event and has concluded that it is reportable as a significant deficiency and a substantial safety hazard. Based upon NRC guidance in NUREG-0302, Revision 1, Georgia Power Company is reporting this event as a significant deficiency pursuant to the requirements of 10 CFR 50.55(e).
An engineering evaluation was performed for weld defects associated with the specific spool pieces and the analysis indicated that, had these defects gone uncorrected,.the system functional performance and plant safety could have been adversely affected. A copy of the evaluation of this concern is attached for your information.
OFFICIAL COPY l
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i United States Nuclear Regulatory Commission Office of Ir..pection and Enforcement Region II-Suite 3100 i
4 101 Marietta Street Atlanta, Georgia 30303 i Page 2 This response-contains no proprietory informatfor. 7.nd may be placed in the NRC Public Document Room upon receipt.
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, . d D. O. Fos er REF/D0F/sfl xc: U. S. Nuclear Regulatory Commission Document Contri' Desk l Washington, D. C. 20555 4
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- xc: R. J. Kelly J. A. Bailey t
R. E. Conway O. Batum G. F. Head G. Bockhold i C. W. Hayes B. M. Guthrie D. M. MacLemore E. D. Groover 4
D. E. Dutton L. T. Gucwa '
W. F. Sa'nders M. Malcom R. H. Pinson H. H. Gregory, III P. D. Rice J. T. Beckham, Jr.
R..A. Thomas J. L. Vota i
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EVALUATION FOR A SUBSTANTIAL SAFETY HAZARD EVALUATION FOR A SIGNIFICANT DEFICIENCY Pullman Power Products - Fabrication Shop Spool Piece Welds f
Initial Report:
On October 21, 1983, Mr. C. W. Hayes, Georgia Power Company's Quality Assurance Manager for the Vogtle Project, reported a potential deficiency to Mr. John Rogge of the USNRC concerning visual weld discrepancies.
Background Information:
This potential deficiency resulted from an Institute of Nuclear Power Operations (INP0) pipe spool visual reinspection program and was initially reported to the ,
Nuclear Regulatory Commission (NRC) on June 17, 1982, by Georgia Power Company.
In a letter dated November 11, 1982, a report was submitted by Georgia Power Company to the NRC in which it was concluded that the potential defects iden-tified at that cime were not reportable under 10 CFR 50.55(e) or 10 CFR Part 21.
Subsequent to that report, additional weld deficiencies were found. This final report includes an evaluation of those potentially reportable weld deficiencies which were not included in the November 11, 1982, evaluation.
All shop fabricated pipe spools which had been shipped by PPP and received on site as of August 1982 were visually rcinspected at the site. The visual de-ficiencies, as identified .in the nonconformance/ deviation reports, had not been noted not reported duriqg the final visual inspection in the shop prior to acceptance and shipment. Consequently, potentially defective piping spools could have been installed and subsequently impact plant operations. The weld deficiencies were evaluated to determine whether the condition impacted safe operation of the plant, and if the condition was characteristic of a quality program breakdown.
Basic Component Identificatico:
The basic components are the piping spools of several plant systems, including safety-related systems.. The potentially deficient welds in these pipe spools are tabulated below.
VISUAL DEFICIENCIES IN PIPE SPOOL SHOP WELDS NONCONFORMANCE/ WELD DEVIATION REPORT SPOOL NO. I.D. DEFICIENCY DESCRIPTION A. System 1202, Nuclear Service Cooling Water MD-2736 2-1202-003-S-01 A Undercut ,
MD-3548 2-1202-004-S-17 90* ELL Grind mark in base metal !
MD-2800 1-1202-084-S-03 B Excess butt weld offset /
root crack ;
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Pullman Power Products Fabrication Shop Spool Piece Welds I Page Two i NONCONFORMANCE WELD DEVIATION REPORT SPOOL # I.D. DEFICIENCY DESCRIPTION A. System 1202, Nuclear Service Cooling Water (Continued)
MD-3245 2-1202-099-S-01 M Incomplete Penetration MD-2823 1-1202-151-S-10 B Excess weld / linear indication MD-2913 2-1202-151-S-10 D Lack of fusion B. System 1206, Containment Spray MD-2767 2-1206-005-S-14 G Lack of fusion MD-3032 1-1206-007-S-10 A,E Incomplete penetration MD-3034 1-1206-007-S-11 D,J Incomplete penetration
- MD-2402 1-1206-007-S-13 E,G Incomplete penetration MD-3035 1-1206-007-S-13 F Incomplete penetration MD-3036 1-1206-008-S-10 J Incomplete penetration MD-3051 1-1206-008-S-13 C Porosity MD-3076 1-1206-009-S-03 K Incomplete penetration MD-2393 1-1206-009-S-04 B Grind mark MD-3077 1-1206-009-S-04 H Undercut / porosity MD-3081 1-1206-01?-S-01 E.F Incomplete penetration i MD-2401 1-1206-013-S-05 D Crater crack
! MD-3080 1-1206-013-S-05 G Incomplete penetration MD-3709 2-1206-013-S-06 G Incomplete penetration
- MD-3027 1-1206-054-S-01 D Incomplete penetration l MD-3033 1-1206-054-5-02 C,F,H Incomplete penetration MD-4092 2-1206-054-S-05 C Undercut i MD-3804 2-1206-054-S-06 D,F,H Undercut 1-1206-054-5-10 Weld crack MD-2815 E MD-3988 2-1206-054-S-10 G Undercut C. System 1208, Chemical and Volume Control MD-3102 2-1208-003-S-07 B Undercut MD-3104 2-1208-003-S-18 A Undercut MD-2279 1-1208-003-5-20 L Incomplete penetration MD-2768 1-1208-078-S-04 B Crater crack MD-3356 1-1208-085-S-03 F Slag MD-2366 1-1208-090-S-02 r Ir. complete penetration MD-2809 2-1208-123-S-10 C Crack D. System 1210, Boron Recycle MD-2432 A-1210-002-S-03 K Incomplete penetration E. System 1213, Spent Fuel Pool Cooling and Purification MD-2635 1-1213-002-S-03 C Weld underfill
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Pullman Power Products Fabrication Shop Spool Piece Welds Page Three NONCONFORMANCE WELD
_ DEVIATION REPORT SPOOL # I.D. DEFICIENCY DESCRIPTION E. System 1213, Spent Fuel Pool Cooling and Purification (Continued) 4 MD-2862 2-1213-002-S-05 C Incomplete penetration MD-2634 1-1213-003 S-02 G Incomplete penetration MD-2781 2-1213-006-S-09 C Incomplete penetration F. System 1217, Auxiliary Component Cooling Water MD-3395 1-1217-011-S-23 E Porosity G. System 1591, Normal Chilled Water MD-3239 1-1591-083-5-01 0 Incomplete penetration MD-3240 1-1591-084-S-01 D Incomplete penetration j
H. System 1592, Essential Chilled Water MD-3407 1-1592-007-5-09 Incomplete penetration l MD-2706 1-1592-044-S-01 A,o Underfill I. System 1901,-Liquid Waste Processing MD-2278 2-1901-102-S-09 B Slag J. System 2303, Seismic Category 1 Fire Protection Water MD-2813 2-2303-022-S-05 A Hole in wcld surface Engineering Evaluation:
An evaluation of each weld defect was conducted to determine if the defect could
, potentially propagate into a through-wall-crack and/or complete weld failure.
Defects demonstrating a propensity of propagation were analyzed further to determine the impact on plant safety. A summary of this analysis is provided as follows:
A. All of the potentially deficient welds were located in moderate energy systems. Consequently, it was unnecessary to consider the dynamic effects of pipe breaks (pipe whip and jet impingement) at the location of the welds.
Pullman Power Products Fabrication Shop Spool Piece Welds Page Four B. A flooding review was performed to determine whether tne existing plant analysis enveloped the effects of piping spool failure at the location of the potentially deficient welds. In all cases, the existing plant analysis postulated failures in other piping spools resulting in larger flooding flow-rates than those associated with the subject piping spools.
C. A facility response analysis was conducted to determine if weld deficien-cies in systems required to place the plant in a safe shutdown condition or mitigate the consequences of an event could result in unacceptable system functional performance and adversely affect plant safety. The analysis conservatively assumed the preexistence of a weld defect in one train, which renders that train inoperable (due to defect propagation and weld failure), concurrent with the most limiting single active failure following the onset of an event (transient or accident condition) requir-ing a response from that system. The results of the analysis indicated that the following deficiencies, had they gone uncorrected could have unacceptably compromised system functional performance and adversely affected plant safety.
NONCONFORMANCE OR l DEVIATION REPORT N0. SP0OL NO. pEFICIENCYDESCRIPTION MD-2800 1-1202-084-S-03 Excess butt weld offset / root crack MD-3245 2-1202-099-S-01 Incomplete penetration MD-3032 1-1206-007-9-10 Incomplete penetration MD-3034 1-1206-007-S-11 Incomplete penetration MD-2402/3035 1-1206-007-S-13 Incomplete penetration MD-3036 1-1206-008-S-10 Incomplete penetration MD-3076 1-1206-009-S-03 Incomplete penetration i MD-3081 1-1206-013-S-01 Incomplete penetration MD-3709 2-1206-013-S-06 Incomplete penetration MD-3027 1-1206-054-S-01 Incomplete penetration MD-3033 1-1206-054-S-02 Incomplete penetration MD-2815 1-1206-054-S-10 Weld crack MD-2279 1-1208-003-S-20 Incomplete penetration MD-2862 2-1213-002-S-05 Incomplete penetration MD-2634 1-1213-003-S-02 Incomplete penetration MD-2781 2-1213-005-S-09 Incomplete penetration MD-3407 1-1592-007-S-09 Incomplete penetration Analysis of Quality Assurance Program:
It was' determined that there was not a significant breakdown in the quality assurance program at Pullman Power Products. Since the 17 defects identified by Bechtel represent a minute fraction of total welds made by Pullman and in-spected; this indicates occasional incomplete execution of procedures and.not an inadequate system.
Also, a special Quality Assurance audit of Pullman's applicable processes and controls was conducted on June 21-23, 1982, with a follow-up on June 29, 1982.
A full-scope Quality Assurance audit was conducted August 25-27, 1982. These
Pullman Power Products Fabrication Shop Spool Piece Welds Page Five audits were conducted in response to the intitial identification of these problems. Results of these audits did not indicate a significant breakdown in the structure or implementation of the Pullman Quality Assurance program.
Subsequent monitoring of the Pullman shop by an SCS shop surveillance repre-sentative indicates that Pullman is continuing to implement their Quality Assurance program.
Conclusion:
The cugineering evaluation performed for the weld defects associated with the pipe spools listed in the engineering evaluation section has indicated that, had they gone uncorrected, the system functional performance and plant safety could have been adversely affccted.
It has also been determined that a significant breakdown of the quality assurance program at Pullman Power Products did not occur.
It has been concluded that the failure of these pipe spools to meet the visual weld requirements of the specification represents a deviation from performance specifications thatrequires extensive repair to establish the adequacy of the system to meet the criteria and basis as stated in the Safety Analysis Report.
This event is therefore reportable as a significant deficiency and as a sub-stantial safety hazard. Based upon NRC guidance in NUREG-0302, Revision 1, Georgia Power Company is reporting this event as a significant deficiency pursuant to the regt.irements of 10 CFR 50.55(e).
Corrective Action:
The spools containing the reported deficiencies have been reworked or repaired and are presently in an acceptable condition, l
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