ML20087D299
| ML20087D299 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 02/29/1984 |
| From: | Jackie Cook, Corbin McNeil POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| JAFP-0272, JAFP-272, NUDOCS 8403130350 | |
| Download: ML20087D299 (11) | |
Text
.
j OPERATING DATA REPORT f
50-333 DOCKET NO.
DATE MARCH 1984 COMPLETED BY
_J. COOK TELEPHONE (313)34z-3840 OPERATING STATUS FITZPATRICK Notes
- 1. Unit Name:
840?01-840229
- 2. Reporting Period:
2436
- 3. Licensed Thermal Power (MWt):
- 4. Nameplate Rating (Gross MWe):
883
- 5. Design Electrical Rating (Net MWe):821 0
- 6. Maximum Dependable Capacity (Gross MWe):
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
NONE
- 9. Power Level To Which Restricted,If Any (Net MWe):
NONE
- 10. Reasons For Restrictions,if Any; This Month Yr to-Date Cumulative
- 11. Hours In Reporting Period 696 1440 75337
- 12. Number Of Hours Reactor Was Critical 696 1440 53968.8
- 13. Reactor Reserve Shutdown Hours 0
0 0
- 14. Hours Generator On-Line 696 1440 52639.6
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1627008 3434472 111171058
- 17. Gross Electrical Energy Generated (MWH) 546230 1155820 38375010
- 18. Net Electrical Energy Generated (MWH) 528615 1 118290 36616930
- 19. Unit Service Factor 100%
100%
69.9%
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- 20. Unit Availability Factor 100%
100%
69.9%
93.8%
95.9%
63.6%
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- 21. Unit Capacity Factor (Using MDC Net)
- 22. Unit Capacity Factor (Using DER Net) -
92.5%
94.6%
59.2%
- 23. Unit Forced Outage Rate 0%
0%
14.2%
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each):
MAINTENANCE OUTAGE COMMENCING MARCH 3,1984 LASTING APPROXIMATELY 10 DAYS
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast A' hieved -
c INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8403130350 840229 t
'e ^
PDR ADOCK 05000333 R
PDR.
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AVERAGE DAll.Y UNIT POWER LEVEL 50-333 DOCKET NO.
FITZPATRICK
!! ARCH 1984 DATE J. COOK COMPLETED,8Y (315)342-3840 TELEPHONE FEBRUARY 1984 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWeNet)
IMWe-Net) 794 776 2
7%
763 3
785 502 3
9 20 538 792 5
M2 6
789 789 22 790 789 7
23 8
795 24 791 792 794 9
25 793 793 10 26 11 606 27 792 708 792 4
12 28 13 783 794 29
~
14 787
~~~
30 789 15 31 790 16 SUMARY:
The Fitzpatrick plant operated at Near Full Thermal power for this reporting period with one power reduction for control rod sequence exchange and one for rod pattern adjustment.
O
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50-333
.UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
UNIT NAME _ FIT 7 PATRi ck' DATE MARCH 1984 REPORT MONT11_ FEBRUARY COMPLETED BY
_J. COOK TELEPIIONE _(315)342-3840 5
E u
,$?
"s jY3 Licensee Eg
%'8 Cause & Currective No.
Daic g
ig i
2s5 Event p
gO Attion to s
i-yE
.32 g =g Reportar mO Prevent Recurrence o
u O
1 840210 S
0 4
N/A N/A N/A
.N/A Reduced power for tod sequence Exchange 2
840218 S
0 4
N/A N/A N/A N/A Reduce power for control rod pattern adjustment.
- l 2
3 4
F: Fueced Reason:
Method:
Enhibli G Insin.cilons 5: Scheduled A Equipment Failure (Emplain) 1 Manual foi Piepaiathm of I)ata fl. Maintenance of Test 2 Manual Scram.
Entry Shecis for 1.icensee C. Refueling 3 Automatic Scram.
Event Reping (LElt) l'ile INtil(EG-D Regulatory Resitiction 4-Other (Explaies) 0161i E Operatur Tealning& License Examinailun F Administrative 5
G Operational Ensur (Explain)
Exhibii I. Saine Source ll Other (Explain) m
NEW YORK POWER AUTHORITY JAMES A. FITZPATRICK NUCLEAR POWER PLANT NARRITIVE
SUMMARY
OF OPERATING EXPERIENCE FEBRUARY, 1984 The unit operated at near full thermal power for this reporting period.
On 840210 power was reduced for rod sequence exchange and en 840217 power was reduced for rod pattern adjustment.
At the end of the reporting period the Fitzpatrick plant is operating at approximately 794 MWe.
r
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL a MECHANICAL MAINTENANCE
SUMMARY
ST#
DATE SYSTEM HOW DETECTED CAUSE OF MALFUNCTION ACTIOli TAKEN TO PRECLUDE RECURRENCE T ME HOURS
/3 46 32363 S.T.
Breaker overcurrent Reset trips in spare breaker 50 1/2 P-28 trips outiof calib.
Installed spare 2/4 10 32362 ISI Improper impeller Disassembled, inspeEted, 92 P-1C collet i n~s t a 11a t io n.
reassembled.
2/3 14 31184 ISI Loose mounting bo lt s Re-torqued 1
P-1A 2/8 23 24428 OPS Worn and eroded Hebuilt trip 10 T-3 parts 2/7 23 19465 Visual Improperly supported Installed support 4
SOV-40 cable
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL a MECHANICAL MAINTENANCE
SUMMARY
DATE SYSTEM "
HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE T
2/9 23 11158 N/A N/A Investigated motor winding 24 MOV-60 connections 2/7 23 14354 OPS Improperly adjusted Adjusted limit switches 15 MOV-57 &
limit sw i-t ch e s HOV-58 2/10 23 20596 N/A Modi f ic a t. ion Replaced overspeed trip 188 TU-2 mechanism 2/3 27 32268 OPS Cracked diaphragm Replaced diaphragm & O rings 14 P-118 2/15 27 31066 OPS Broken heat trace Replaced heat trace 11 Drywell Atmosph Monitor 2/11 03 32395 OPS Leaking 111 Valve Replaced valve 4
HCU 18-l 47 1
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRidK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL a MECHANICAL MAINTENANCE
SUMMARY
DATE SYSTEM "
HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 2/11 03 32311 OPS Leaking 111 Valve Replaced valve 4
HCU 30-11 1/31 10 11159 M00.
Improper. valve Replaced operator 130 HOV-39B M1-84-01 ope rator -
2/9 23 321331 OPS Worn packing Re-oacked 50 MOV-14 2/20 14 228141 OPS Charging motor drive Readjusted pawl 6
P-1A pawl out of adjust.
Breaker 2/20 14 31184 P&V ISI Suspected pump pro-Disassembled, inspected, 411 P-1A blem due to ISI vi-replaced rotating components bration readings of pump 2/8 23 29282 Visual Worn packing Re-packed 10 HPI-28C 2/22 27 24538 OPS Misadjusted limit Readjusted limit switches 26 S0V122F1 switches S0V122F2 2/21 27 24572 OPS Burned out coil Replaced coil 8
S0V-12SB 8
POWER AUTHORITY OF THE STATE OF NEW YORK JA'
- S A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL a MECHANICAL MAINTENANCE
SUMMARY
DATE SYSTEM HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 2/23 27 32284 OPS Leaking 0 Rings Replaced 0 Rings 36 P-118 2/24 71 32298 OPS Bad solder joint Re-soldered 6
A Batt.
~
tect r 2/24 23 32394 Visual Seal Tite-pulled out Reconnected 3
A0V-39 of junction box 2/25 27 24633 OPS Overfilled with oil Replaced on relief valve &
12 P-11B check valve - cleaned oil filter 2/27 76 22769 QA Review Valve installed in Reoriented valve 10 FPS-44 wrong orientation 2/28 76 22764 QA Review Valve installed in wrong Reoriented valve 10 FPS-53 orientation
NEWYORK POWER AUTHORITY-JAMES A.FITZPATRICK NUCLEAR POWER PLANT t
MAINTENANCE
SUMMARY
- FEBRUARY, I&C WORK REQUEST NO.
HOW CAUSE OF RESULTS OF ACTION TAKEN REPAIR i
DATE SYSTEM COMPONENT NO.
DETECTED MALFUNCTION MALFUNCTION TO PRECLUDE TIME i
RECURRENCE HOURS l-1/25/84 02 032098 OPS Needed Calibration
%D/P's 10% Diff.
Calibrated and 20 DPI-78G,R from average Adjusted 2/16/84 02-3 024391 JIC Spare Unit Needed Calibration Replaced CR4,R54; 40 GE/MAC SQX Troubleshot Calib.
1/31/34 02-3 032199 JIC Age-Use Right Hand Test Rpled Test Valve, 0.5 i
LIS-72 Valve Stripped Perf. ISP-3.2 1/31/84 06 031126 JIC Wear, Age, Out of Level Indicator is Rpled 6-LI-94, 10 i
LI-94A Proc. Tolerance Faulty Perf. ISP 3-4
(
2/27/84 07 024502 OPS Faulty Amp Card LPRM was drifting Rplce LPRM Amp 4
LPRM-44,45 Card with new i
2/27/84 07 029046 JIC Age Broken Light Removed and rpled 0.5 RBM-A light bulb 1/23/84 07 032244 OPS Wear, age of the Burned out indicator Checked and rpled 20 TIP A,B,CD bulbs bulbs bad bulbs 2/27/84 10 024515 OPS Wear, Faulty Constant alarm when Rpled Control Board 12 f
LS-105B Components full water Per. G30 2/24/84 16 014574 OPS Leaks to Press readings Record, recharge, 8
ELEC. PEN on guages snoop, record 1/30/84 17 031102 JIC Failed 3600 cpm test Test Circuit Adjusted, calib 10 RIS-432B eircuit reading high Perf. IS?-25 t
4 2/7/84 17 032281 OPS Teeded Calib, Wear Found out of Cal, Clean, Adj 5
RR-433 tolerance TAW TMP-6-14 2/7/84 20 032252 OPS ige & wear of timer Timer does not turn Found Pitted Contax s
I SMP Timer ontacts on Replaced SW 16
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NEWYORK POWER AUTiiORITY-JAMES A.FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
FEBRUARY, 1984 I&C l
WORK REQUEST NO.
HOW CAUSE OF RESULTS OF ACTION TAKEN REPAIR DATE SYSTEM yCUR PE E
COMPONENT NO.
DETECTED MALFUNCTION MALFUNCTION g
2/24/84 27 026494 JIC Wear, Faulty Magntic Can't adjust span Install new Mag 20 l
(
02AZ 101B Unit analyzer Unit, Calibrate 2/25/84 27 031133 JIC Instrument Drift Zero would not Calib. and adjstd 12 HAZ -101A adjust Perf ISP-30 2/23/84 66 029365 OPS Requested Calib.
Zero and Span off Labeled Instr.
13 l
DPIS 100 and Labeling Needed Label Reset Zero, Span l
2/17/84 76 024506 OPS Faulty Timer N HPCI Did not Actuate Adjusted Relay 8
l l
TH-149, in Spec l
2/22/84 76 024579 OPS Drift PS Does not Start Changed SW set pt 17 L
PS&PI-102 Pump Cal. Guage 2/8/84 76 032358 OPS Faulty Relays Improper Heat Det.
Rpled RA & RB Rlys 16 FPP Zone 2S Lite Operat.
for A1138 2/2/84 93 032361 OPS Meter Worn from Ammeter Reads Replaced Meter 8
AM-11B Age Upscale 200 AMPS I
i
James A. Fit:P trick Nuclear Pow:r PI:nt PO. Box 41 Lycoming NewYork 13093 315 342.3840
- > NewYorkPower 4v Authority March 8, 1984 JAFP-0272 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washinghton, D.C. 20555 Attention:
Document Control Desk
Reference:
Docket No. 50-333
Dear Sir:
The Operating Status Report for the Month of February, 1984 is enclosed.
The refueling information remains the same as previously submitted.
If there are any questions concerning this report contact John Cook at (315) 342-3840, Ext. 439.
Very truly yours, A
(,N Corbin A. McNeill, Jr.
CAM:JPC:jls Enclosures CC:
Internal Distribution-4+
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