ML20086J455

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Telecopy AO 74-8:on 740918,hydraulic Snubber Found Inoperable.Caused by Locknut Not Tightened Properly.Snubber Being Returned to Svc in Proper Position W/Locknut Properly Tightened
ML20086J455
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 09/19/1974
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086J448 List:
References
AO-74-8, NUDOCS 8401230697
Download: ML20086J455 (1)


Text

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^Mk ggg Peach Botton Atcnnic Power Station Delta, ?cnnsylvania 17314

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September 19, 1974 Mr. James P. O'Reilly, Direc

'r United States Atomic Energy Coc=ission Directorate of Regulatory Operations

..p-631 Park Avenue 4f; O King of Prussia, Pennsylvania 19406 k,h.[-

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Subject:

Abnormal Occurrence 24-I!our Notification

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.;.p Confirming W. T. Ullrich's phone conversation with Mr. Walt Baunack, A.E.C.

i M;!?l,7 Region 1 Regulatory Operations Office on Septo =ber 19, 1974.

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Reference:

License Number DPR-56 i M e.,.- :

Technical Specification Reference 3.5.A.3 l

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7 Report No.:

50-278-74-8

.;;,y Report Date:

September 19, 1974 J c.5 1 u

Occurrence Data:

Septaber 18, 1974 I GQd

! 9'" [..[y Facility:

Peach Ecttc= Atomic Power Station R.D. 1, Delta, Pennsylvania 17314 U..n.

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3 Identification of Occurrence:

l[P;.y Inoperable hydraulic snubber.

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m.g;.);:p Conditions Prior to Occurrence:

y Hafatenance cutage in progress. Reactor shutdown.

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Description of Occurrence:

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During a routine inspection of the Unit 3 hydraulic snubber during a plant L;l caintenance outage, hydraulic onubber 3-1 0-113-5-7 was observed to have becoce M.Yd -

inverted resulting in the draining of all hydraulic fluid out of the reseWoir vent.

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Designation of Apparent Cause of Occurrence:

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Preliminary investigation indicates that the lock nut which prevents rotation of the anubber cechanima was not tightened properly.

I Analysis of Occurrence:

The defective snubber is installed on the discharge piping of the "B" RHR pump for seismic support only.

It serves no f unction during nortal plant operations.

The g losu of fluid from this snubber has minical safety significance.

Corrective Action:

The anubber is being returned to service in the proper position with the lock nut properly tightened. Additional investigation is in progress.

Failure Data:

Nene.

8401230697 740928 PDR ADOCK 05000278 s

PDR Very truly yours, Q Q,Yi&,/

W. T. Ullrich, Superintendent,.

Pe' ach Botten Aconit-Power Station.

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