ML20086H807

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Telecopy AO 75-39:on 750518,excessive Leakage Found Through Loop a RHR Inboard & Outboard Torus Cooling Valves MO-2-10-34A & MO-2-10-39A.Cause Under Investigation. Corrective Action to Be Determined
ML20086H807
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 05/19/1975
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086H806 List:
References
AO-75-39, NUDOCS 8401200248
Download: ML20086H807 (1)


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h uj*/dc4'dfg,4 Pili 1ADELPflIA ELEC.TRIC COMPANY Peach Botto:a Atonic Power Station Delta, Pennsylvania 17314 /

Hay 19, 1975 Mr. James P. O'Reilly, Director Office of Inspection and. Enforcement Region 1 "7.)iTWSt5tbrEIcIcar HegTII5toIf tT=iIssroh~ -

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631 Park Avenuo King of Prussia, Pennsylvania. 19406

Subject:

Abnomal Occurrence 24-lbur Notification Confiming J. Franz *f p1mne 'convers:ction..with Mr. Walt Baunack, Region. I., United

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'Referenec:

License 26=ber DPR-44 Technical Specification Referenec:

4.7.A.2.f Report No.:

50-277-75-39 Report Date:

May 19,1975

, Occurrence Date:

13ay 10, 1975 Facility:

Peach Eotton. Atoalc. Power Station R.D. 1, Delta, Pennsylvania 17314 Identification of Occurrencer Excessive leakage thru the "A" loop RICI inboard and outboard torus cooling valves (MO-2-10-34A 6 MO-2-10-39AF.

C:r.d' itic.: "r*:r :: Occurrcr.;c:

Unit 2 shutdown.

- Descriptirn of Occurrence: -

During a routine Iccal Icak test of tho {l11R'"A" Icop torus cooling i

voivas, valver !?O-2-10-34A 0 !:0 2-10-10A ucre four I to Ic;k.. Thc prelininary test pcTfor ed, which identified the Icak, was with waterr later testing with air confimed the leakage rate to be in cr.ccss of 6000 cc/ pin.

Designation of Apparent Cause of Occurrence:

Under investinction-Analysis of Occrrrencc:

Nornal operating pressurceof the PJUt ptemps during the design basis accident is greater.then 49.1 psig thereby prec vding cuticakagerinto-the RIEL r.ystus.

Even if the contninaent nteosphere Icake,i.back thrcugh 4

these valves, the 1er.Lnge t.uuld enter theiPJ'.T systen which is a closed

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systcu nn.1 :2e tested satisfactorily as part of the Type A IIRT..

Safety icplications of this occurrence are therefore niniusl:.

Corrective Action:

To be detemired Fai10ro Data:

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8401200248 750528 PDR ADOCK 05000277 S

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