ML20086G656
| ML20086G656 | |
| Person / Time | |
|---|---|
| Site: | Limerick |
| Issue date: | 06/30/1995 |
| From: | Gallagher M, Henricks D PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9507170038 | |
| Download: ML20086G656 (12) | |
Text
Lim ric's Cener: ting Stattra
= ems.
'=gpr PECO ENERGY
- J;;; """"'
Sanatoga, PA 19464 4920
)
T.S.6.9.1.6 July 13, 1995
)
Docket Nos. 50-352
[
50-353 i
License Nos. NPF-39 l
NPF-85 U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, DC 20555
Subject:
Limerick Generating Station Monthly Operating Report For Units 1 and 2 i
Enclosed are the monthly operating reports for Limerick Units 1 and 2 for the month of June 1995 forwarded 4
pursuant to Technical Specification 6.9.1.6.
very truly yours, Michael P. Gallagher Director - Site Engineering drh Enclosures cc:
T. T. Martin, Administrator, Region I, USNRC N. S. Perry, USNRC Senior Resident Inspector LGS W. G. MacFarland, Vice President, LGS l
9507170038 950630 PDR ADDCK 05000352 1
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Docket No. 50-362 Attachment to Monthly Operating Report for June 1996 f
Limerick Generating Station i
Unit 1 June 1 through June 30,1996 1.
Narrative Summary d Operating Exoeriences Unit 1 began the month d June at a nominal 100% of rated thermal power (RTP).
O'1 June 2,1996, at 1617 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.152685e-4 months <br />, power was reduced to 98% RTP due to high turbine backpressure. Power was restored to 100% RTP at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />.
On June 4,1996, at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, power was reduced to 82% RTP for main turbine valve testing t
and a control rod pattom adjustment. Power was restored to 100% RTP at 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />.
On June 19,1996, at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br />, power was reduced to 98% RTP due to high turbine backpressure. Power was restored to 100% RTP at 2212 hours0.0256 days <br />0.614 hours <br />0.00366 weeks <br />8.41666e-4 months <br /> On June 20,1996, at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, power was reduced due to high turbine backpressure Power was reduced to 94% RTP. Power was restored to 100% RTP on June 21,1996, at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />.
On June 22,1996, at 1543 hours0.0179 days <br />0.429 hours <br />0.00255 weeks <br />5.871115e-4 months <br />, the 1B circulating water pump tripped due to a ground
)
overcurrent. This resulted in a decrease in condenser vacuum. Power was reduced to 96 %
RTP in order to recover condenser vacuum. Power was restorad to 100% RTP on June 23, 1996, at 0000 hourt.
Unit 1 ended this operating period at 100% of RTP.
11.
Challanoes to Main ham Safety Relief Valvas i
There were no challenges to the Main Steam Safety Relief Valves during the month of June.
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OVERAGE DAILY UNIT POWER LEVEL
+
DOCKET NO. 50 - 352 i
UNIT LIMERICK UNIT 1 DATE JULY 13 1995 COMPANY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 MONTH JUNE 1995 DAv AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILv POWER LEVEL (WWE-NET)
(MWE-NET) 1 1049 17 1046 2
1037 18 1045 3
1037 19 1036 4
981 20 1008 5
1051 21 1041 6
1049 22 1037 7
1034 23 1036 8
1037 24 1046 9
1050 25 1040 10 1051 26 1033 11 1041 27 1045 12 1045 28 1049 13 1050 29 1050 14 1050 30 1044 15 1049 16 1045 W
OPERQTING DQTO REPORT t
DOCKET NO. 50 - 352 DATE JULY 13, 1995 COMPLETED BV PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 OPERATING STATUS 1
UNIT NAME: LIMERICK UNIT 1 NOTES: THERE WERE NO LOAD DROPS l
- 2. REPORTING PERIOD:
JUNE. 1995 GREATEP THAN 20% THIS MONTH.
3.
LICENSED THERMAL POWER (MWT):
3293 t
4 NAMEPLATE RATING (GROSS MwE):
1092 l
- 5. DESIGN ELECTRICAL RATING (NET MwE):
1055
- 6. MAXIMUM DEPENDABLE CAPACITY (GROSS MwE): 1092
- 7. MAMIMUM DEPENDABLE CAPACITY (NET MwE):
1055 1
8.
IF CHANGES OCCUR IN CAPACITV RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:
9.
POWER LEVEL TO WHICH RESTRICTED. IF ANY (NET MwE):
- 10. REASONS FOR RESTRICTIONS. IF ANY:
THIS MONTH VR-TO-DATE CUMdLATIvE ti. HOURS IN REPORTING PERIOD 720 4.343 81.4B?
- 12. NUMBER OF HOURS REACTOR WAS CRITICA.
720.0 4.242.3 68.350.6
- 13. REACTOR RESERVE SHUTDCwN HOL'R S 0.0 0.0 0.0 14 HOURS GENERATOR ON-LINE 720.0 4.205.8 67.231.3
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
- 16. GROSS THERMAm ENERGY GENERATED (WWH) 2.360.738 13.760.920 208.077.458 17 GROSS ELECTRICAL ENERGY GENERATED (MWH) 776.400 4.486.300 67.670.580
- 18. NET ELECTRICAL ENERGv GENERATED (WWH) 749.037 4.335.915 64.979.921 PAGE 1 OF 2 w
. l OPERQTING DOTO REPORT (CONTINUED)
DOCCET NO. 50 - 352 DATE JULY 13, 1995 THIS MONTH VR-TO-DATE CUMULATIVE
- 19. UNIT SERVICE FACTOR 100.0 96.8 81.5
- 20. UNIT AVAILABILITY FACTOR 100.0 96.8 81.5
~
21 UNIT CAPACITY FACTOR (USING WDC NET) 98.6 94.6 74.7
- 22. UNIT CAPACITv FACTOR (USING DER NET) 98.6 94.6 74.?
- 23. UNIT FORCED OUTAGE RATE O.0 0.9 4.1 24_
SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):
- 25. IF SHUTDOWN AT END 05 ]fPORT PERIOD. ESTIM4TED DATE OF STARTUP:
- 26. UNIT 5 Ih TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 12/19/84 12/22/84 INITIAL ELECTRICITY MID APRIL B5 4/13/85
___~______
CCMMERCIAL OPERATION 15T OTR 86 2/01/8F PAGE 2 OF 2
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 352 UNIT NAME LIMERICK UNIT 1 DATE JULY 13. 1995 REPORT MONTH JUNE. 1995 COMPLETED BY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER l
SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 i
l I
i l
NETHOD OF l LICENSEE ISv5TEMICOMPONENTI CAUSE AND CORRECTIVE ITVPElDURATION REASONISHUTTING DOwNI EVENT l CODE i CODE l ACTION TO NO.i GA'E i (1)l (HOURS)
(2) l REACTOR (3) !
REPORT a (4) l (51 1 PREVENT RECURRENCE I
I I
I I
I i
66 I 9506C2 l F l 000.0 H
4 I
N/A l
HC l HTEXCH I REACTOR POWER WAS REDUCED TO 90% DUE TO 4
l l
l l
l l HIGH TURBINE BACKPRESSURE CAUSED BV 4
I l
l l
l i
l WEATHER CONDITIONS.
4 l
1 1
I I
i l
i 0?
I 950604 i S l 000.0 B
1 4
l N/A i
HA 1 VALVEx
! REACTOR POWER WAS REDUCED TO B2% FOR 4
L l
l l
l 1
l
$ MAIN TURBINE VALVE TESTING AND CONTROL 4
l l
1 i
l I
i ROD PATTERN A DJ U ST M E NT.
4 l 000.0 l
l 1
I i
68 l 950619 F
i H
4 l
N/A I
HC l HTEMCH l REACTOR POWER WAS REDUCED TO 98% DUE TO 4
i i
l l
l l
1 l
l HIGH TURBINE BACKPRESSURE CAUSED BV 4
l l
l l
l l
l WEATHER CONDITIONS.
4 I
I l
l l
1 69 ! 950620 l F
000.0 H
l 4
l N/a l
HC HTEXCH l REACTOR POWER WAS REDUCED TO 94% DUE TO 4
i l
i HIGH TURBINE BACKPRESSURE CAUSEO BV 4
l l
l l WEATHER CONDITIONS.
4 I
i i
i I
70 ' 950622 F
l 000.0 l
A 4
N/A l
HF PUMPMM l REACTOR POWER WAS REDUCED TO 96% DUE TO 4
l t
i i
1 CIRCULATING WATER PUMP TRIP CAUSED BV 4
l l GROUND OVERCURRENT.
4 1
1 4
1 I
l i
i 1
1 1
I I
l (1)
(2)
(3)
(4)
- - FORCED REASON METHOD EXHIBIT G-INSTRUCTIONS S - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE C-REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D - REGULATORv RESTRICTION 4 - OTHER (EXPLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMINATION F _ ADMINISTRATIVE (5)
G - OPERATIONAL ERROR (EMPLAIN)
H - OTHER(EXPLAIN)
ExMIBIT I - SAME SOURCE i
1 Dockd N2. 50-353 Attachment to Monthly Operating Report for June 1995 Umerick Generating Station Unit 2 June 1 through June 30,1996 1.
Narrative Summary of Operating Experiences Unit 2 began the month of June at a nominal 100% of rated thermal power (RTP).
On June 3,1995, at 0003 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, a planned power reduction commenced in order to remove the main turbine from service to repair an EHC leak at the number 4 combined intermediate valve.
Power was reduced to 25 % RTP by 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br />. The main turbine was removed from service at 0518 hours0.006 days <br />0.144 hours <br />8.564815e-4 weeks <br />1.97099e-4 months <br /> and retumed to service at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />. Power ascension began at 1232 hours0.0143 days <br />0.342 hours <br />0.00204 weeks <br />4.68776e-4 months <br /> and power was restored to 100% RTP on June 4,1996, at 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br />.
On June 5,1996, at 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br />, power was reduced to 90% RTP for a control rod pettom adjustment. Power was restored to 100% fiTP on June 6,1995, at 0214 hours0.00248 days <br />0.0594 hours <br />3.53836e-4 weeks <br />8.1427e-5 months <br /> On June 17,1996, at 0500, a planned power reduction commenced to repair the 48 and 58 feedwater heater dump valves. Power was reduced to 60% RTP by 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />. Power ascension began at 1329 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.056845e-4 months <br /> and power was restored to 100% RTP at 1641 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.244005e-4 months <br />.
On June 18,1996, at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, power was reduced to 90 % RTP for a control rod pattom adjustment. Power was restored to 100% RTP at 1749 hours0.0202 days <br />0.486 hours <br />0.00289 weeks <br />6.654945e-4 months <br />.
On June 20,1995, at 1508 hours0.0175 days <br />0.419 hours <br />0.00249 weeks <br />5.73794e-4 months <br />, power was reduced to 97 % RTP due to high turbine backpressure. Power was restored to 100% RTP at 2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br />.
On June 25,1995, at 0134 hours0.00155 days <br />0.0372 hours <br />2.215608e-4 weeks <br />5.0987e-5 months <br />, power was reduced to 90% RTP for control rod scram time testing and a control rod pattom adjustment. Power was restored to 100% RTP at 0741 hours0.00858 days <br />0.206 hours <br />0.00123 weeks <br />2.819505e-4 months <br /> On June 26,1996, at 1624 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.17932e-4 months <br />, the 2B reactor recirculation pump / motor generator set trloped Power was reduced to less than 33% RTP per procedure. Power was stabilized at 31.7% RTP.
The cause for the trip is unknown; system monitoring is in progress. Power ascension comrnonced at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> The 2B reactor recirculation pump was started at 0520 hours0.00602 days <br />0.144 hours <br />8.597884e-4 weeks <br />1.9786e-4 months <br /> and power was restored to 100% RTP on June 27,1996, at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />.
On June 28,1996, at 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br />, power was reduced to 90% RTP for a control rod pettom edjustment. Power was restored to 100% RTP at 1441 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.483005e-4 months <br />.
On June 28,1995, at 1703 hours0.0197 days <br />0.473 hours <br />0.00282 weeks <br />6.479915e-4 months <br />, the 2B reactor recirculation pump ran back to minimum speed when power was lost to the 2B feedwater/ reactor recirculation pump uninterruptable power supply. The 2B reactor foodpump locked up due to the signal failure. Reactor power was stablized at 40% RTP with the A and C reactor feedwater pumps in automatic and the 2B reactor feedpump in standby. Power ascension commenced at 2242 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.53081e-4 months <br /> and power was restored to 100% RTP on June 29,1996, at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br />.
On June 30,1995, at 0310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br />, power was reduced to 90% RTP for a control rod pattom adjustment. Power was restored to 100% RTP at 0542 hours0.00627 days <br />0.151 hours <br />8.96164e-4 weeks <br />2.06231e-4 months <br />.
Unit 2 ended this operating period at 100% of RTP.
ll.
CM':.aes to Main Swm Safety Relief Valves There were no challenges to the Main Steam Safety Relief Valves during the month of June.
)
AVERAGE DAILY UNIT POTER LEVEL 4
DOCKET NO. 50 - 353 UNIT LIMERICK UNIT 2 DATE JULY 13. 1995 1
COMPANY PECO ENERGV COMPANY DAVID R.
HENRICMS REPORTS ENGIt:EER SITE ENGINEERING 4
LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 l
MONTH JUNE 1995 DAV AVERAGE DAILY POWER LEVEL DAV AVERAGE DAILY POWER LEVEL (MWE-NET)
(MwE-NET) 1 1118 17 912 2
1110 18 1110 3
473 19
'110 4
1049 20 1097 5
1106 21 1113 6
1117 22 1117 7
1105 23 1117 8
1109 24 1118 i
9 1122 25 1092 e
10 1122 26 861 J
11 1114 27 771 a
i 12 1118 28 914 13 1122 29 1055 14 1118 30 1109 15 1123 4
l 16 1117 I
i
OPERQTING DOTO REPORT DOCKET NO. 50 - 353 DATE JULY 13. 1995 COMPLETED BY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING
~
LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 OPERATING STATUS 1
UNIT NAME: LIMERICA UNIT 2 NOTES: THERE WERE 4 LOAD DROPS
.____.___.._.______~_________.__._
2.
REPORTING PERIOD:
JUNE. 1995 GREATER THAN 20% THIS MONTH
- 3. LICENSED THERMAL POWER (wwT):
3458 DUE TO THE REPAIR OF AN EHC 4
NAMEPLATE RATING (GROSS MwE):
1163 LEAA. REPAIR OF FEEDWATER HEAT-g
- 5. DESIGN ELECTRICAL RATING (NET MwE):
1115
-ER DUMP WALVES.A RECIRC PUMP l
g 1
- 6. MAXIMUM DEPENDASLE CAPACITY (GROSS UwE): 1155 TRIP AND RECIRC PUMP RUN BACK.
- 7. max! MUM DEPENOABLE CAPACITY (NET MwE):
1115 8.
IF CHANGES OCCUR IN CAPACITV RATINGS (ITEM 5 NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:
9.
POWER LEVEL TO wHICH RESTRICTED. IF ANY (NET MWE):
- 10. REASONS FOR RESTRICTIONS. IF ANY:
THIS MONTH VR TO-DATE CUMULATIVE 11 HOURS IN REPORTING PERIOD 720 4.343 47.999
- 12. NUMBER 05 HOURS REACTOR WA5 CRITICAL 720.0 3.823.4 43.186.4
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
_~________._
14 HOURS GENERATOR ON-LINE 714.4 3.710.2 42.315.1
- 15. UNIT RESERVE SHUTDOWN HOUR 5 0.0 0.0 0.0
- 16. GROSS THERMAL ENERGV GENERATED (MwH) 2.366.669 11.440.141 133.669.724
- 17. GROSS ELECTRICAL ENERGv GENERATED (MwH) 785.100 3.801.000 44.184.500
- 18. NET ELECTRICAL ENERGv GENERATED (MwH) 759.339 3.669.356 42.571.556 PAGE 1 OF 2 L
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m n.
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m.
OPEROTING DOTO REPORT (CONTINUED)
DOCQEV NO. 50 - 353 DATE JULY 13. 1995 THIS MONTH YR-TO-DATE CUMULATIVE
- 19. UNIT SERVICE FACTOR 99.2 85.4 88.2
- 20. UNIT AVAILABILITV 8 ACTOR 99.2 85.4 88.2 4
21 UNIT CAPACITY FACTOR (USING MDC NET) 94.6 76.2 83.7 j
- 22. UNIT CAPACITV FACTOR (USING DER NET) 94.6 76.2 83.7
- 23. UNIT FORCED OUTAGE RATE O.0 2.1 3.3 24 SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TVPE. DATE. AND DURATION OF EACH):
- 25. IF 5HUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED 4
INITIAL CRITICALITV 08/12/89 08/12/89 7
INITIAL ELECTRICITY 09/01/89 09/01/89 COMMERCIAL OPERATION 02/01/90 01/08/90
<i s
1 PAGE 2 OF 2 I
j t
i l'
- - ~ - -,
UNIT SHUTDOWNS OND POWER REDUCTIONS DOCCET NO. 50 - 353 UNIT NAME LIMERICK UNIT 2 DATE JULY 13. 1995 REPORT MONTH JUNE. 1995 COMPLETED BV PECO ENERGY COMPANY DAVID R.
HENRICK$
WEPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 l
\\
\\
l METHOD OF l
LICENSEE ISYSTEulCOMPONENTl CAUSE AND CORRECTIVE 1
lTYPElDURATIONl REASON) SHUTTING DOWN!
EVENT l CODE 1 CODE l ACTION TO NO.1 DATE l (1)! (HOURS)l (2) l REACTOR (3) l REPORT a I (4) l (5) l PREVENT RECURRENCE i
l I
i 1
54 1 950603 l 5 005.6 i
A 4
l N/A I
HA VALVEX l REACTOR POWER WAS REDUCED TO 25% TO 4
l l
l l
l l REMOVE THE MAIN TURBINE FROM SERVICE TO 4
l l
l I
A l
f I
I l
i l
l 55 l 950605 1 5 000.0 l
B l
4 i
N/A RB l CONROD i REACTOR POWER WAS REDUCED TO 90% DUE TO 4
l l
l l
l 1 CONTROL ROD PATTERN ADJUSTMENT.
4 i
I i
1 56 l 950617 F h 000.0 A
4 N/A CH VALVEX l REACTOR POWER WAS REDUCED TO 60% TO 4
l l
l l REPAIR THE FEEDWATER HEATER DUMP VALVE.
4 I
l l
I 57 l 9506'8 l 5 000.0 B
4 l
N/A RB CONROD l REACTOR POWER WAS REDUCED TO 90% DUE TO 4
l l
1 l
l CONTROL ROD PATTERN ADJUSTMENT.
4 l
l I
l I
58 l 950620 l F
000.0 H
4 N/A HC l HTEMCH l REACTOR POWER WAS REDUCED TO 97% DUE TO 4
i l
1 l
l HIGH TURBINE BACM PRESSURE CAUSED BV 4
l l
l l
l WEATHER CONDITIONS.
4 I
I I
I I
I i
59 I 950625 i S 000.0 i
B 4
l N/A l
RB l CONROD I REACTOR POWER WAS REDUCED TO 90% DUE TO 4
l l
l l
l l
i CONTROL ROD PATTERN ADJUSTMENT AND 4
l l
1 l
I i
i CONTROL ROD SCRAM TIME TESTING.
4 l
l 1
I i
l 60 1 950626 l F
000.0 i
A 4
i N/A l
CB l PUMPxx REACTOR POWER WAS REDUCED TO 31.7% DUE 4
(1)
(2)
(3)
(4) r - FORCED REASON METHOD EXHIBIT G - INSTRUCTIONS 5-SCHEDULED A - EOUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY 5HEETS 50R LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D - REGULATORY RESTRICTION 4 - OTHER (EMPLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMINATION P - ADMINISTRATIVE (5)
G - OPERATIONAL ERROR (EXPLAIN)
H - OTHER(EXPLAIN)
EXHIBIT I - SAME SOURCE
. ~.. _. _-.-..-
UNIT SHUTDOWNS OND POWER REDUCTIONS DOCGET NO. 30 - 353 j
UNIT NAME LIMERICK UNIT 2 DATE JULY 13. 1995 REPORT MONTH JUNE. 1995 COMPLETED BY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICM GENERATING STATION TELEPHONE (610) 718-3772
~
l l
l METHOD OF l LICENSEE l SYSTEM COMPONENTI CAUSE AND CORRECTIVE lTVPElDURATIONl REASON SHUTTING DOwNI EVENT l CODE CODE 1 ACTION TO NO.
DATE l (1)! (HOUR 5)I (2)
REACTOR (3) l REPORT
- l (4)
(5) l PREVENT RECURRENCE 1
l l
l I TO REACTOR RECIRCULATION PUMP / MOTOR 4
l l
l GENERATOR SET TRIP.
4 I
I I
(1 950628 l 5 000.0 B.
4 l
N/A RB CONROD l REACTOR POWER WAS REDUCED TO 90% DUE TO 4
1
)
l l
l I
i i CONTROL ROD PATTERN ADJUSTMENT.
4 I
i I
I i
I e2 1 950628 i
- 000.0 A
l 4
l N/A l CB l PUMPA7 i REACTOP POWER WAS REDUCED TO 40% DUE TO 4
l l
I l
l POWER LOSS TO FEEDwATER/ REACTOR 4
l l
l RECIRCULATION PUMP.
4 1
i 63 950630 S
000.0 B
4 N/A l
RB CONROD I REACTOR POWER WAS REDUCED TO 90% DUE TO 4
i CONTROL ROD PATTERN ADJUSTMENT.
4 I
4 l
l l
4 l
l 4
l l
1 5.6 l
l 1
1 (1)
(2)
(3)
(4) s. FORCEO REASON METHOD EXHIBIT G - INSTRUCTIONS S-SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA l
B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D-REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMINATION q
F _ ADMINISTRATIVE (5) i G - OPERATIONAL ERROR (EXPLAIN)
H - OTHER(EXPLAIN)
EXHIBIT I - SAME SOURCE 1
4 i
b a
-