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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20086B1731976-11-0909 November 1976 AO 50-267/74-20A:on 741116,during Low Power Physics Testing, Conflict Found Between Tech Specs 4.2.11 & 4.4.1 Re Moisture Limits.Caused by Last Minute Change in Tech Specs 4.2.11. Tech Specs Revised ML20086B1781976-11-0909 November 1976 AO 50-267/74-20A:on 741116,during Low Power Physics Testing, Conflict Found Between Tech Specs 4.2.11 & 4.4.1 Re Moisture Limits.Caused by Last Minute Change to Tech Specs 4.2.11. Tech Specs Revised ML20086B1001976-09-0303 September 1976 AO 50-267/74-21C:on 741121,high Pressure in Gas Waste Vacuum Tank Lifted Relief Valve Allowing Release of 700 Scf Uncontaminated Gas.Caused by Operator Error.Valves Will Be Replaced W/Kerotest Valves & Change Notice 91 Issued ML20086A0441976-05-28028 May 1976 Telecopy AO 76-012:on 760527,helium Circulator 1B Tripped Twice.Caused by Buffer Seal Malfunction.Sys Operating Procedure Will Be Revised ML20086A0691976-05-20020 May 1976 AO 76-011:on 760510,helium Circulator 1C Tripped Due to Negative buffer-midbuffer Differential Pressure.Cause Associated W/Test ML20086A0871976-05-0303 May 1976 Telecopy AO 76-010:on 760429 & 30,circulators 1A & 1B Tripped on Loss of Bearing Water.Caused by Operator Error ML20085M4351976-02-17017 February 1976 Telecopy AO 76/005:on 760227,loss of Essential 480-volt Bus 2 Caused Trip of Three Helium Circulators Due to Circulator Bearing Water Problems.Loss of 480-volt Bus Could Cause Temporary Loss of Forced Circulation ML20085M4731976-02-0606 February 1976 Telecopy AOs 76/03 & 76/04:on 760206,generator Set 1-B Load Breaker Would Not Close & Generator Set 1A Trouble Alarm Received,Indicating Partial Disconnection of Engine 1B from Generator.Causes Not Stated ML20085M5651975-12-22022 December 1975 AO 50-267/74/23A:on 741211,engine a of Standby Diesel Generator 1A Declutched During 2 H Surveillance Run & No Alarm Annunciated.Caused by Dirt Under Seat of Solenoid Valve.Plant Change Notice 12 Initiated ML20085M7181975-12-22022 December 1975 AO 50-267/75/15A:on 750709,during Repair of Minor Oil Leak on Gasoline Engine of Emergency Fire Pump,Inlet Manifold Piping Found Cracked.Caused by Component Failure.Manifold Repaired ML20086B1541975-12-18018 December 1975 AO 50-267/74-7A:on 740424,fuel Handling Machine Failed to Engage & Lift Reflector Element 09-06-R-01.Caused by Mfg Error.Reflectors de-burred & Ga Co Will Supply Two Column 1 Metal Clad Reflector Elements ML20085M5631975-11-18018 November 1975 AO 50-267/75/24:on 751108,static Seal on Helium Circulator B Inadvertently Released.Cause Presently Undetermined. Circulator B Brake & Seal Manually Set ML20085M6211975-10-21021 October 1975 AO 50-267/75/18A:on 750816,during Installation Preparation, Helium Circulation Damaged.Caused by Lack of Adherence to Approved Procedure.Personnel Counseled to Adhere to Approved Procedures & Supervision ML20085M5711975-09-26026 September 1975 AO 50-267/75/23:on 750916,essential Electrical Cable Discovered to Have Failed.Caused by Circumstances Associated W/Work in Progress.Damaged Cable Replaced ML20085M5771975-09-26026 September 1975 AO 50-267/75/22:on 750912,during Gas Waste Routine Release, Trouble W/Gas Vacuum Tank Observed by Reactor Operator.Cause of Malfunction Unknown.Failure Could Not Be Reproduced.No Further Action Planned ML20086B1151975-09-26026 September 1975 AO 50-267/74-21B:on 741121,high Pressure in Gas Waste Vacuum Tank Lifted Relief Valve Allowing Release of 700 Scf Uncontaminated Gas.Caused by Operator Error.Inlet Valve Seats Will Be Replaced W/Soft Seats ML20085M5821975-09-22022 September 1975 AO 50-267/75/21:on 750911,control Rod Drive Inserted Into Pcrv Rotated 180 Degrees from Required Orientation During Control Rod Drive Mod.Caused by Design & Procedure Error. Procedures Modified ML20085M6181975-09-0505 September 1975 AO 50-267/75/19:on 750825,engine a of Standby Generator a Automatically Shut Down & Declutched During Cooldown Portion of Weekly Surveillance Test.Caused by Difference in Fuel Rack Setting.Setting Changed ML20085M6231975-09-0505 September 1975 AO 50-267/75/18:on 750816,during Installation Preparation, Helium Circulator Damaged.Caused by Lack of Adherence to Approved Procedure.Personnel Counseled to Adhere to Approved Procedures & Supervision ML20085M6121975-09-0505 September 1975 AO 50-267/75/20:on 750826,12 Cord Sets Connecting Process Controllers at I-05 & I-06 Control Board to Cable Rack in Auxiliary Electric Equipment Room Switched.Caused by Malicious Mischief ML20085M6781975-08-15015 August 1975 AO 50-267/75/17:on 750808,instrument Air Compressor 1C Observed Running Continuously in Unloaded Condition.Caused by Component Failure.Failed Unloader Actuator Replaced W/New Unloader Actuator & Tested ML20085M7021975-07-21021 July 1975 AO 50-267/75/16:on 750610,when Engine B of Standby Generator a Dissassembled,Broken Rings,Scored Cylinders & Cracked Pistons Found.Caused by Water Engine.Engines Inspected.Pistons,Liners & Rings Replaced ML20085M7251975-07-18018 July 1975 AO 50-267/75/15:on 750709,during Repair of Minor Oil Leak on Gasoline Engine of Emergency Fire Pump Inlet Manifold, Piping Found Cracked.Caused by Component Failure.New Manifold Ordered & Defective Casting Replaced ML20085M7401975-06-11011 June 1975 AO 50-267/75/14:on 750530,engine B of a Diesel Generator Oversped to 1,900 Rpm While Electrical Overspeed Trip Being Set.Caused by Procedure Error.Test Procedure Changed ML20085L6331975-05-27027 May 1975 AO 75-267/75/13:on 750519,I-B Engine of I-A Standby Diesel Generator Failed to Start.Caused by Failure to Transmit Info That Engine Was Out of Svc to Adjust Overspeed Switches ML20085L6481975-05-12012 May 1975 AO 50-267/75/10:on 750501,exam Revealed Pin on Declutching Mechanism of Engine D of Standby Diesel Generator D Sheared Off.Caused by Inadequate Lubrication.Pin Replaced & Lubrication Frequency Increased ML20085L6301975-05-12012 May 1975 AO 50-267/75/9:on 750404,valve HV-2188-8 Did Not Open When Circulator Seal Release Permissive Circuit Directed Valve to Open.Cause Not Stated.Air Solenoids Inspected & Cleaned ML20085L7871975-05-0707 May 1975 AO 50-267/74-25:on 741018,diesel Engine B of Standby Generator a Tripped from High Water Jacket Temp on Routine Test.Caused by Improper Filling of Water Jackets.Personnel Counseled ML20085L6411975-05-0707 May 1975 AO 50-267/75/11:on 750424,preliminary Calculations Indicated That Helium Bottles Supplying Reserve Shutdown Sys Did Not Have Adequate Restraint for Dbe.Cause Not Stated.New Bottle Racks Designed & Installed ML20085L7881975-04-16016 April 1975 AO 50-267/74/24A:on 741222,static Seal on Helium Circulator a Released During Removal of Temporary Jumpers.Caused by Jumper Contact W/Station Ground ML20085L7671975-04-0808 April 1975 AO 50-267/75/3A:on 750123,dew Point Moisture Monitor Failed to Initiate Reactor Scram When Moisture Content Exceeded Trip Setpoint.Caused by Design & Procedure Inadequacies.New Procedure Developed ML20085L6491975-04-0707 April 1975 AO 50-267/75/9:on 750329,leak in Mechanical Seal of Helium Circulator B Discovered.Caused by Foreign Matl on Sealing Surfaces.No Corrective Actions Planned ML20085L6831975-04-0202 April 1975 AO 50-267/75/6A:on 750202,gas Waste Vacuum Tank Rupture Disc Ruptured,Releasing Small Quantity of Gas.Caused by Improper Closure of Air Operated Drain Valve Due to Foreign Matl on Valve Seat.Seat Repaired ML20086E1651975-03-21021 March 1975 AO 50-267/74/6A:on 750202,gas Waste Vacuum Tank Rupture Disc Ruptured,Releasing Small Quantity of Gas.Caused by Failure of Air Operated Drain Valve to Close Properly.Valve Repaired & Reinstalled ML20085L7071975-03-14014 March 1975 AO 50-267/75-4-A:on 750125,tritium Leaked from Secondary Closure of Refueling Region 1.Caused by Normal Presence of Tritium in Pressurizing Gas ML20085L6511975-03-0707 March 1975 AO 50-267/75/8:on 750224,diesel Engine B of Standby Generator a Failed to Function Properly During Weekly Test. Caused by Defective Temp Thermocouple.New Thermocouple Installed & Preventive Maint Program Instigated ML20085L6581975-03-0404 March 1975 AO 50-267/75/7:on 750121-23,reactivity Anamoly Occurred Due to Release of Hopper of Reserve Shutdown Mall Into Core. Cause Not Stated.Valve Seats Modified ML20086B0681975-02-26026 February 1975 AO 50-267/74-22A:on 741129,high Pressure in Gas Waste Vacuum Tank Blew Rupture Disc & Lifted Relief Valve Allowing Release of 750 Scf Uncontaminated Gas.Caused by Design Inadequacy.Pressure Indicator Installed ML20085L6851975-02-18018 February 1975 AO 50-267/75/6:on 750202,gas Waste Vacuum Tank Rupture Disc Ruptured,Releasing Small Quantity of Gas.Caused by Improper Closure of Air Operated Drain Valve.Valve Will Be Disassembled for Insp ML20085L7011975-02-17017 February 1975 AO 50-267/75/5:on 750127,gas Vacuum Tank Rupture Disc Ruptured,Releasing Small Quantity of Gas.Caused by Inadequate Procedures.Procedure Rewritten ML20085L7121975-02-14014 February 1975 AO 50-267/75/4:on 750125,tritium Leaked from Secondary Closure of Refueling Region 1.Cause Will Be Determined When Vessel Pressure Dropped to Atmospheric or Below ML20085L7721975-02-12012 February 1975 AO 50-267/75/3:on 750123,dew Point Moisture Monitors Failed to Initiate Reactor Scram When Moisture Content Exceeded Trip Setpoint.Caused by Failure of Sample of Primary Coolant to Reach Monitor.Tech Specs Revised ML20086B1231975-02-12012 February 1975 AO 50-267/74-21A:on 741121,high Pressure in Gas Waste Vacuum Tank Lifted Relief Valve Allowing Release of 700 Scf Uncontaminated Gas.Caused by Procedural Error.Inlet Valve Seats Will Be Replaced & Interim Procedure Modified ML20085L7401975-02-0707 February 1975 AO 50-267/75/1:on 750118,230-kV Breaker Tripped Due to High Winds,Causing Standby Diesel Generator a to Receive Start Signal.Generator B Did Not Receive Start Signal.Caused by Sensitive Relay Setting.Relay Recalibr ML20085L7271975-01-31031 January 1975 AO 50-267/75/2:on 750113,reactor Bldg Exhaust Charcoal Filters Failed to Meet Tech Spec Leak Rate Requirements. Caused by Use of oil-based Paint & Organic Solvents.Filters Changed Out ML20085L6501975-01-25025 January 1975 AO 50-267/75/24A:on 741222,static Seal on C-2101 (Helium Circulator C) Released During Removal of Temporary Jumpers. Caused by Blown Fuse & Seal Release Valve Leak.All Circulator Brake & Seal Vent Valves Checked ML20085L7341975-01-24024 January 1975 Telecopy Ao:Charcoal in Reactor Bldg Exhaust Filters Failed to Meet Tech Spec Requirements ML20085L7901975-01-14014 January 1975 AO 50-267/74/24:on 741222,static Seal on C-2101 (Helium Circulator C) Released During Removal of Temporary Jumpers.Caused by Jumper Across Logic Circulator a Coming in Contact W/Station Ground ML20086B0501974-12-23023 December 1974 AO 50-267/74-23:on 741211,engine a of Standby Diesel Generator 1-A Declutched & No Alarms Annunciated.Caused by Cylinder Air Pressure Decay Due to Dirt Under Solenoid Valve Seat.Change Notice 11 Re in-line Filters Approved ML20086B0641974-12-19019 December 1974 Telecopy AO 50-267/74-23:on 741211,diesel Engine a of Standby Generator 1-A Declutched 1976-09-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
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' . PUBLIC SERVICE COMPANY OF COLORADO P. O . B O X 040 . DENVER. COLonA00 00201 It. I'. WALM Ult i
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October 22,197V V E.k/,, xa
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M]D' OC/gO Mr. E. Morris Howard, Director Region IV f. ~
Directorate of RegulatoryOperations i / p United States Atomic Energy Connission g <,' ,M N i
10395 West Colfax - Room 200 s?6\ : " ' ,j ^' _'
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Denver, Colorado 80215 \ fx
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Dear Sir:
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Please find attached Abnomal Occurrence Report No. 50-267/74/17A, Final, concerning the helitna circulator Pc1 ton whccls.
c.
- At the appropriate time, we may wish to request Regulatory Opera-tions to certify that the plant is ready to go to Phase 2 of the Startup 4
program as defined by LCO 4.9.1 and to proceed into Startup Tests A-6 and A-8 and then into the first part of SUr B-0 to detomine the reactor core temperature coefficient of reactivity at or about 6000F utilizing the presently installed cast Inconal Pelton whccls. During these tests <
reactor power would be limited Administratively to a maxima of 2':i re-acter rated themal power. This limit would remain in effect until new forged Inconel Pc1 ton wheel assemblies are installed.
Following this series of tests, the reactor would be shut down and the cast Inconel Pelton wheels removed, and new forged Inconel Pelton
- whccls installed on the helium circulators. Following installation, each
- , helium circulator will be functionally tested to 7000 rpra to assure re-
- actor shutdown cooling capability.
j.
j Risc to 100% reactor power would follow as presently planned in the "B" series Startup Tests.
!I j - If you have any questions or comments concerning these plans,
(, please contact me as soon as possibic.
j'
,f ( Very truly yours,
+
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') 8311170168 751215 \L L ' cr '('
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^ PDR ADOCK 05000267
.: d " S PDR R. F. Walker, Vice President i!
Engineerine and Planning .
- Electric Department .
F COPY SWF REGIOlt '
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o o Date: October 21, 1974 ABNORMAL OCCURRENCE
. s FORT ST. VRAIN NUCLEAR CENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P.O. BOX 361 PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/74/17 A 4
Final i -
IDENTIFICATION OF OCCURRENCE:
i Physical examination of "A" helium circulator pelton wheel, Serial No._4, ,
indicates cracking at the roots of the teeth of the curvic coupling and at
~
the root of the splitter on six (6) of the tuenty (20) pelton turbine buckets. This is considered an abnormal occurrence per Item 2.1(f) of the Technical Specifications.
CONDITIONS PRIOR TO OCCURRENCE: Steady State Power Routine Shutdown ,
Hot Shutdown Routine Load Change Cold Shutdown X Other (specify)
Refueling Shutdown Helium circulator had been re-l moved to inspect failed static Routine Startup seal bellows. Examination of '
-pelton wheel _ indicated potential problems. The circulator had been operated at various speeds over_its entire speed range (up to 10,000 rpm) using both the stenn and Pelton water turbines for a total of approximately 450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br />. This total includes operating time at both the Valmont Helium Circulator Test Facility and Fort St. Vrain. No problems were observed during operation. Cracking at the pelton wheel coupling and in the buckets was found following removal of the circulator for other reasons, i
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4 Page 2
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, The major plant parancters at the time of the event were as follows:
, Power RTR, N/A MWth ELECT, N/A IMc Secondary Coolant- Pressure N/A psig Temperature N/A 'F Flow N/A #/hr.
Primary Coolant Pressure N/A psig '
Temperature N/A 'F Core Inlet N/A 'F Core Outlet Flow N/A #/hr.
"A". helium circulator had been removed from its normal position in its PCRV bottom head penetration and had been repinced by the sparc due to probices with the static seal bellows (see Abnormal Occurrence Report #50-267/74/13 dated July 11,1974 and #50-267/74/13A dated October 3,1974). Helium cir-culator components were being examined in manufacturer's shops in San Diego, California.
DESCRIPTION OF
_0CCURRENCE: ,
Removal of "A" helium circulator from the PCRV due to static seal actuating bellows prob 1 cms afforded the opportunity to examine components of the helium circulator in detail. -
-A fluorescent penetrant (Zyglo ZL-22) examination of the " nuclear" pelton whcc1 coupling area indicated uniform cracking at the root of all the coupling teeth and revealed six (6) of twenty (20) pelton turbine buckets with crscks at the root of the splitter. None of these cracks were visible to the naked cyc.
DESCRIPTION OF OCCURRENCE: x Design Unusual Service Cond.
Including Environ.
Manufacture Installation /Const. Component Failure
+
Operator X Other (specify)
Procedure Apparent' incipient failure V
1 l
~
j
Page 3
' ANALYSIS OF OCCURRENCE:
A detailed metallurgical and engineering analysis of pelton whccls Scrial No.
3 and 4 in conjunction with an experimental program has resulted in the following conclusions:
FR0!! METALLURIGICAL EXAMINATIONS (a) Based on the oxidation of the fracture surfaces, it is concluded that the cracking in the curvic coupling area on S~crial No. 3 and 4 wheels was produced during operation at the Valmont Helium Circulator Test Facility.
- (b) Some limited propogation of the Curvic cracking may have occurred during operation of Scrial No. 4 whccl at Fort St. Vrain.
(c) Due to the lack of heavy oxidation of the fracture surfaces and since bucket cracking was confined to Serial No. 4 wheel which had also been operated at Fort St. Vrain, in addition to operation at Valmont, it is assumed the bucket cracking took place at Fort St. Vrain.
(d) All the cracking on both wheels appeared similar in character and was concluded to be due to high cycle fatigue.
(e) The material and physical properties of the pelton whcc1 castings obtained from the heat treatment were considered to be within specifi-cations limits for this particular casting configuration.
- Wheel Serial No. 3 was operated only at the Valmont Helium Circulator Test Facility. Wheci No. 4 was operated at both Valmont and Fort St. Vrain.
i FROM THE PREVIOUS OPERATING HIFTORY AND EXPERIMENTAL STRESS AND ANAD*TICAL ANALYSI3:
- 1. Incipient cracks in the Buckets j
(a) The cause of the cracks is high-speed (> 8000 rpm) water operation.
(b) At 7000 rpm, cracks will not be initiated.
, (c) At 7000 rpm, buckets with incipient cracks have essentially an l infinite life. (no crack propogation)
- 2. Localized cracks in the Curvic Coupling Area (a) The cracks were initiated by a vibratory stress, most probably cmanating from the steam turbine disc.
(b) Steam conditiens at Valmont (pressure, temperature, and flow) required higher than design pressure ratios across the turbine nozzles (choked flow condition) to adequately test the circulator gas side performance. It is thought these conditions were conducive to exciting the turbine disc at the amplitude sufficient to generate the damaging alternating stress component.
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(c) The total stress experience at the Curvic coupling, although sufficient to initiate cracks in the 718 pelton wheel, is within the strength capability of the wrought 422 stainless material of the steam wheel, i (d) The cracks will be confined to the immediate vicinity of the Curvic coupling and will not impair the capability of the unit
- to function satisfactorily.
, SAFETY ASPECTS:
To evaluate safety aspects of the Fort St. Vrain operation with reduced rpm
] (7000 rpm vs 10,500 rpm) of the Pelton whccis, the following approach was adopted:
(1) From a list of events requiring operation of the circulators j
on Pelton wheel drives, the events imposing the most severe requirements were
, selected. (2) These events were re-analyzed assuming restricted operating i
conditions of the Pelton wheel drives. (3) The re-analysis was then evaluated i
with respect to cafety limits and AEC accident-dose guidelines. As the result l of re-analysis of the safety aspects of plant operation, the following was i
concluded: (1) The safe Shutdown Earthquake or Maximum Tornado events are in-consequential, i.e., no release of radioactive material occurs, and no damage which could increase the potcatial for release takes place. (2) The Rapid Depressurization event does not result in component or fuel damage which would increase the release of fission products beyond the icvel already reviewed by the AEC via the original FSAR analysis (10,500 rpm) uith one circulator operat-ion limited to 7000 rpm.
On the basis of the technical investigations, the following conclusions have
- been reached
) (a) No new limitations are required for steam operation of the helium
- circulators.
(b) The forged pelton wheels can be safely operated for postulated j cmcrgency conditions by imposing a lower limit on maximum pelton i whccl speed. (7000 rpm vs 10,500 rpm)
(c) The plant safety is not. compromised at 105% power conditions with an
~
I imposed Pelten wheel speed limit of'7000~ rpm.
I
- These conclusions are based on specific facts and evidence obtained from (1) review of the operating history, -(2) metallurigical investigations and
, analyses, (3) experimental results, (4) fracture mechanics analysis, and (5) plant safety analyces associated with reduced pelton whcci maximum speed. ,
z
- See attached report GA-A13175 for details.
CORRECTIVE y ACTION: '
- i i We are taking the following corrective actions:
4
- 1. Limiting the1 helium circulator speed to 7000' rpm when operating on 4 the pelton turbine..
! /'
l O e 8e s
- 2. Replacing the present cast inconel 718 pelton wheels with forged inconel 718 pelton wheels.
- 3. Including in our Technical Specifications an in-service surveillance program for the helium circulator pelton wheels. This is to be discussed and finalized with AEC-DOL.
Reducing the helium circulator operating speed to 7000 rpm, when driven by.
the Pelton wheel, will assure a reduction of stress Icvels in the buckets that will not produce or propogate cracks. Also, the use of forged inconel will increase the bucket resistance to fatigue cracking.
The use of forged inconel 718 to replace the east inconci 718 material will markedly increase the strength of the pelton whccl assembly. The metalluricical and mechanical properties of the forged inconel 718 are more similar to the forged 422 stainless material of the steam turbine whcci which has to date in-dicated no signs of stress at the curvic coupling.
A review of the postulated accident conditions indicates the most severe condit- j fons requiring helium circulator operation on pelton turbines are associated with the Rapid Depressurization accident. Reanalysis of this accident indicates that although peak temperatures during the transient are higher with the circulator operating at 7000 rpm as compared to those if the circulator is operating at 10,500 rpm, no ccmponent safety limits are exceeded and the risk to the health and safety of the public is not increased. *
- For inore details, see report GA-A13175.
i FAILURE DATA /SIMU.AR REPORTED OCCURRE"CES: I 1 l
- Sec reports
- October, 1973 l To: Dr. Donald Knuth Directorate of Regulatory Operations Deficiency Report, '
Fort St. Vrain Uclium Circulators August, 1972 To: Mr. F.E. Krucsi Directorate of Regulatory Operations j Deficiency Report j Fort St. Vrain Helium Circulators
_PROCRAhMATIC IMPACT: '
10 - 12 week delay.
_ CODE IMP!.CT:
None / ,
f .
s /h _ p ** DW '
rederic E. Svart Superintendent Nuclear Production
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