ML20086B123
| ML20086B123 | |
| Person / Time | |
|---|---|
| Site: | Fort Saint Vrain |
| Issue date: | 02/12/1975 |
| From: | Rodgers W, Swart F PUBLIC SERVICE CO. OF COLORADO |
| To: | |
| Shared Package | |
| ML20086B083 | List: |
| References | |
| AO-267-74-21A, NUDOCS 8311170062 | |
| Download: ML20086B123 (3) | |
Text
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Februa 2, 1975 Ct v 10rdtA1. OCCUR.Rff;CE
.. L r,:" guTE: __t1/21/74 O
U FORT ST. V.ut!! ::t:Cf.rAR CC?;E:tATI':G STATIO' PUBLIC SE? NICE Cn"?.t!."i OF C01.0RADO P. O. !!OX 361 PLATTEVILLE, COLORADO A0651 4
REPORT I:0. 50-267/74/21-A Final
ne':TIFICATIO:1 0F
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nn ?:ovenber 21, 1974, high pressure in the gas vaste vacuum tank ruptured ru:iture disc and lif ted a relief valve allowinr. an unauthori=cd release of
.:.r pr. win.itelv 700 SCF of uncontaninated gas to the reactor buildinq ventilation This is identified as an abnornal occurrence per Technical Specifications vs:.n.
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CD:.**)I' !G::S PRIOR
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.y Steady State Power Routine..htde.:n Hot Shutdown Routine Load Changg
'X Cold Shutdown
'~ ' Other (specify)
Refueling Shutdown Routine Startup The najor plant parameters at the time of the event were as follows:
Power
- PTR, U/A MJth
- ELECT, N/A Mfe Secondery. Coolant Pressure n/A psig Temperature n/3
- F Flow N/A
- /hr.
~
Prinary Coolant Pressitre o
psig Tenperature 115
- F Core Inlet 135
- F Core Outlet Flow 0
- /hr.
8311170062 760903 g
PDR ADOCK 05000267 S
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si r
gau_
2
van 2 r- %
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9 r
J f
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wrification rareacr1tien s*.'ste, to the.
- 11.
c,t tn deein tha.hclite:
-'f the re eneration of "A" 109 the concInsion va=;t e rur; c tank was alarned.
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f.t..ein ta: h, at
" A" '.t t the inlet valve
.i'.ur%r, high prassure en
" i" tanh 5ut
- r..i :.'r e :'. rator fr~.2diatcl7 n':h chc.i to th.:
ef f cetively sinittins of f
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t d !-
- o ' n'uit,
f to "li" s trre tanh h.9 heen h:'rflo, path of both nas vante cerprem;
('-l 11:1 Tite remiltin:'. abrupt pressurc
.ti char *e e: f' c dischar',e of the conpressor i.
d snicty valve to bc
- b i ro e in the vaettun tank caused the re ture dine an700 FCF of ras to The
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M. v, r..icaning :
vent !!ation exhaust is nonitored and the e instru-,enSubsequest lab analysin o "A" surne tank contents c$.ut e in count rete.
in the p.as.
contained that no detectabic activity was present APPARr.::T CAUSE OF occlintrt:CE:
Unusual Service Cond.
X
_ Design Including Environ.
Conponent Failurc -
Manufacture
_Other (specify)
Q Installation /Const.
llX-Operator '
Procedure
_-X A':AT.YSIS OF ocrr:n-:cE:
..e tank have Icahed The isolation valves at the inlet to cach'nas vaste surgehandjack on a valve Peninn:
h in the past and a practice has been established to set t ein Icakace and release of unanal
. urine. a relcana fica the tank to preventThe handjack was set but not r 9.a s.
h tor A hold tag should have been placed on the handswitch to alert t e opera 4
0;'erator :
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the handjack on ItV-6336 was set closed.
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that l
does not specifically list a" check of handjack renoval or a.
i Procedure:
1 The valve list test of valve operation.
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o Page 3 CORRECTIVE ACTTON:
Design:A Change Notice (#101) has becu issued to replace the seats in the inlet valves to the gas vante surge tanks with soft reatn. A gooil seat in these valves will uake the une of the handjack unnecessary.
Change Notlec #91 has been issued to change the wiring so etther 11V-6335 or HV-63% will always be open. The change provideo for a switch with a mid-position whern both valves are open.
Operator:
Operators have been issued a mt mo t o place a "H01.D" tag on the tank scicetor switch when a bandjack is set on either valve.
Procedure:
The System Operating Procedure valve list has been modified to call for handjack removal after the discharge is complete and includes a test of valve operation. Thin step will be removed after the soft sent valves at the tank inlet are installed and proven to be Icak free.
FATI.URE DATA /
SIMIIAR REI'ORTED OCCURRENCES:
Nonc PROGRA*fMATIC IMPACT:
None CODE IMPACT:
s None Submitted by:
Approved by:
/>
rederic E. Swart W. Duanc Rodgers Operations Supervisor Superintendent Nucicar Production Fort St. Vraln Nuclear Public Service Company Cencrating Station of Colorado l
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