ML20085M652

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AO BFAO-7340W:on 731115,during Accelerated Surveillance Testing,Hpci Steamflow Excessive Pressure Switches PdIS-73-1A & 1B Malfunctioned.Caused by Contacts in Improper Setting.New Locking Plate Assemblies Installed
ML20085M652
Person / Time
Site: Browns Ferry 
Issue date: 11/23/1973
From: Eric Thomas
TENNESSEE VALLEY AUTHORITY
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20085M654 List:
References
AO-BFAO-7340W, NUDOCS 8311090147
Download: ML20085M652 (3)


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TENNESSEE VALLEY AUTHOFilTY T-~~3M 77 rT -

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CHATTANOOGA, TENNESSEE ij ' ' / / c. {

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November 23, 1973 j@yfi[6]

OIb{7 Mr. John F. O' Leary, Director V

Directorate of Licensing Office of Regulation U.S. Atcmic Energy Ccmmission Washington, DC 20545

Dear Mr. O' Leary:

TEHITESSEE VALLEY AUTHORITY - BEGMS FERRY IiUCLEAR PIAllT UUlT 1 -

DOCK 3T H0. 50-259 - FACILITY OPERATING LICEUSE DPR ABNORMAL OCCURRENCE REPORT DFAO-734Gi The enclosed report is to provide details concerning HPCI steamflow excessive pressure switches' malfunctions which occurred on Browns Ferry Nuclear Plant unit 1 on Hovember 15, 1973, and is submitted in accordance with Appendix A to Regulatory Guide 1.16, Revision 1, October 1973 Very truly yours,

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ITENUESSEE VALIEY AUTHORITY 0-

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E. F. Thomas I (

Director of Power Production Enclosure CC(Enclosure):

Mr. Norman C. Moseley, Director Region II Regulatory Operations Office, USAEC 230 Peachtree Street, IM.

Atlanta, Georgia 30303

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ABNOR!'AL OCCURRENCE REPORT Report No.--BFAO-73!40W Report Date--November 23, 1973 Occurrence Date--November 15, 1973 Facility--Browns Ferry nuclear Plant unit 1 Identificatien of Occurrence Unit 1 HPCI steamflow excessive pressure switches malfunctioned.

Conditions Prior to Occurrence Reactor'at 25-percent ther=al power during startup testing.

Description of Occurrence During accelerated surveillance testing on November 15, 1973, HPCI steamfica excessive pressure switches PDIS-73-1A and 1B were found to operate outside technical specification setpoint of less than or equal to 90 psid as specified in Table 3.2.B.

The as-found settings were 92 5 and 96.o psid, respectively.

Analysis of Occurrence These switches have two contacts in parallel that form a trip logic in the trip system. The trip logic acts to trip the HPCI turbine and isolate the system upon hiSh steamline flow. Since only one set of contacts -in each switch was found out of technical specification setting and the other two contacts tested satisfactorily, the logic would have performed its intended function if required.

Corrective Action

. Locking plate assemblies have been received and are being installed in all Barton Model 288 switches, and an accelerated testing frequency of once a week has been initiated and will continue 1.ntil three consecutive tests prove satisfactory.

The testing frequency will then continue on a biweekly schedule until three consecutive biweekly tests are satisfactory, whereupon'the original schedule will be resumed.

-Failure Data Barton Model 288

, Serial Nos.: PDIS-73-3A, 288-5843; PDIs-73-1B, 288-5842 0

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FailureData(continued)

Switch Date Failure Corrective Action PDIS-73-1A 9/20/73 Operated outside tech spec limit Reset switch, adjusted for free operaticn PDIS-73-1A 11/15/73 Operated outside tech spec limit Installing new locking plate assembly PDIS-73-1B 11/15/73 Operated outside tech spec limit Installing new locking-plate assembly M

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