ML20085L651

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AO 50-267/75/8:on 750224,diesel Engine B of Standby Generator a Failed to Function Properly During Weekly Test. Caused by Defective Temp Thermocouple.New Thermocouple Installed & Preventive Maint Program Instigated
ML20085L651
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 03/07/1975
From: Brey H
PUBLIC SERVICE CO. OF COLORADO
To: Howard E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
AO-50-267-75-8, NUDOCS 8311020212
Download: ML20085L651 (9)


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pubile service company ore celerade P. O. Box 361, Platteville, Colorado 80651

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E. Morris Howard, Director U. S. Nucicar Regulatory Com:nission

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Office of Inspection & Enforcement Region IV 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012

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On 2/24/75, while running the weekly surveillance tests on the emergency diesel generators, "B" engine of the "A" diesel-generator set failed to operate normally due to.a faulty exhaust temperature thermocouple.

C Frederie. E. Svart.

Supt. Nucicar Production'

- Fort St. Vrain Nuclear' Generating Station j

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I:EPORT DATE:

March 4 1975,_

ABN0!U4AL OCCURRENCP.

u OCCURKENCE DATE: Februa ry 24' 1975 y.

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FORT ST. VRAIN NUCLI%R GENERATING STATION PUBLIC SI:RVICE COMPANY OF COLORADO r

P. O. l'OX 361 d i L.!.'.-

PLATTEVII.LE, COLORADO 80651

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s REPORT No. 50-267/75/8 Final C

l IDENTIFICATION OF OCCURRENCE:

On February 24,1975, "B" diesel engine of "A" standby generator failed to function properly during a veckly surveillance test.

The engine started, ran for approx-imately 20 seconds, then shut down.

This is defined as an Abnormal occurrence as per definition 2.1.f) of the Technical Specifica<_fon.

CONDITIONS PRIOR

, steady State Poewr-

, Routine Shutdown tu uccusau.cr.:

Hot Shutdown Routine Load Change X

Cold Shutdown Other (specify)

Refueling Shutdown Routine Startup-The major plant parameters at the time of.the event were as fo))ows:

Power Rtr.

O MWth Elect.

O MWe Secondary Coolant Pressure 260 psig Temperature 68

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. Flow 18,000 ~

  1. /hr.

Primary Coolant Pressure Atmospheric

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'p d Temperature 100

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I-100

  1. F Outlet

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Flow 0

  1. /hr.

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l DESCRIPTION OF

.O..C_CURR_ ENC E :_ _ _ _

During SI; 5.6.1 a-w, weekly test ing of the it andby d iesel generating units, engine B of A generator, started, ran for approximat ely 20 seconds, then shut down and declutched.

A second, immediate attempt to start the engine was unsuccessful.

Exhaust temperature indication for li engine showed no increase during the 20 second run.

APPARENT CAUSE OF OCCURRENCE:

Design

_ _ Unusual Service Cond.

Including Environ.

_ Manufacture

_X

_ Component Failure

_ Installation /Const.

,,_ _ __ Other (specify)

Operator Procedure The exhaust temperature thermocouple had failed, and therefore showed no tempera ture increase.

The control system saw this as a failure of the engine to start, and therefore, shut the engine down and declutched it, en prouane A -nging re-g-7ggi g 2 : pperedly g2:2 inn,

i ANALYSIS OF

.O._C_.CURRESC E :

At tempting to run S.R. 5.6.1-a-w, "B" engine on the "A" diesel-genera tor unit shut down after 20 seconds.

Electrical inspection revealed that the exhaust temperature thercocouple was defective.

These exhaust temperature

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thereccouples cust show high temperature in the exhaust system for a "Go" in the process of starting the units.

However, the thermocouple was not open but failed to produce the necessary millivolt output to drop out the tcaperature relay, which resulted in a declutch and trip of the "B" engine.

All alarms associated with the trip operated norrdilly.

CORRECTIVE ACTION:

PTR 2-350 issued.

'A new exhaust temperature thermocouple was installed, and a program initiated on the preventive maintenance program to change out all thermocouples on the diesel-generator units on an annual basis.

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Fall.URE DATA /

SIMILIAR REPORTED OCCURI:ENCES:

None.

Other thermocouples have becu changed in the pant, but because of suspected deterioration, not complete failure.

PROGRABIATIC I?1 PACT:

None CODE IMI'ACT:

I None Recommended:

Approved:

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Frank M. 'fathic Frederic E.

Swart Superintendent-Maintenance Superintcudent Nuclear Produetion Fort St. Vrnin Nuclear Public Service Company of Colorado Cencrating Station e

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r A Thoned to 1,ois-Grico, Extension 7750, 2/24/75, at

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E. Morris Howard, Director U. S. Nucicar Regulatory Commission Office of Inspection & Enforecaent

-Region IV 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 On 2/24/75, while running the veckly. surveillance tests on the emergency diesel generators, "B" engine of the "A" diesel-generator set failed to operate normally due to.a faulty exhaust temperature thermocouple.

Frederic E.

Swart Supt. Nucicar Product.icn Fort St. Vrain Nuclear Gc.4 crating Station 3

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