ML20085E485
| ML20085E485 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 09/09/1976 |
| From: | Bixel D CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| References | |
| LER-ER-76-025, LER-ER-76-25, NUDOCS 8308120254 | |
| Download: ML20085E485 (2) | |
Text
_ __
Q Q
~.-
UCENSEE EVENT REPORT CONTROL BLOCK:{l l l l l
l
[M. EASE PRINT ALL RSdBUutED W8PORGAATION)
)
x 1
8 J
1%"
'7v'"'
T"."E tcENu Nu 9Ea lMl Tl Pl A lLl1l l 0l 0l-l 0l 0l 0l 0l 0 l-l 0l 0l l h l 1 l1l 1l 1l l0l3l O
7 89 14 15 25 28 30 31 32 UA1C 00Cx(T NU 9ER EVENT CATE REPORT DATE TYPE O CONT l l l
[LJ l,JJ l0 l 5 l 01-10 l215 l51 lo 18 l1 l 317 l 6l lo 19 l0l 9l 71 61 7 8 57 58 59 80 8*
88 89 74 75 80 EVENT DESCRIPTION gg l While verforming the semiannual operational check of the two hydrogen recombiners, l 7 89 80
@ l Unit "69B could only be loaded to h3 kW and the resulting heater temperature was l
80 7 a9
$ l 170 F below the tennerature reouired by Technical Snecification h.2.2.12.b.h l
7 d9 80 SE l (1200 F).
The heater met the requirements of the six month test but vould not meet l 7 89 go BE I the recuirements of the 18-month test. The unit is considered inoperable. (ER-76-29) 80 7 89 C
DE COMPONENT CODE P!
W1ATON ME l Sl El ]
lR lEl Cl 0] MlBl lW l1 l 2 l 0l
{
7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION DE l '"he ureliminary inspection indicates that one phase of the heater is grounded. A l
7 89 80
@ l detailed investication vill be made at the next plant cold shutdown. In addition l
7 89 80 3 l tc the 1005 redundant recombiner unit the containment purge system is (see Line 18) l 7 89 S
% POWER OTHER STATUS OE OSCOVERY DESCAPTON
[Ej l0l 9l 9l l NA l
[b_]
l NA l
1 7 8 9
10 12 13 44 45 46 80 Es $UISE l l
l NA l
aYtE54 [o AuouNT os ACTmTv LoCAfos os nELEASE l,,ZJ NA E0 W
7 8 9
10 11 44 45 80 IEASONNEL EXPOSURES NUMBE A TYPE DESCApicN
]E l Cl 0 l 0 l Wl NA l'
7 89 11 12 13 80 PERSONNEL INJURIES NUMBER DESCASTON 3E I ol O l 01 1
NA l
7 89 11 12 80 PROBABLE CONSEQUENCES gg l None - Redundant systems are available.
l 7 89 80 LOSS OR DAMAGE TO FACIUTY TYPE DESCAFTON g] ] l NA l
7 89 10 80 PUBLOTY gg l None l
7 89 80 ADDITIONAL FACTORS g l (Contd From Line 10) available. Either system is capable of maintaining H,3 belov l 7 89 80 gg l the combustible limit during post LOCA conditions.
l 7 89 8308120254 760909 PDR ADOCK 05000255 S
r.
^
n Y-(J'
~
e 4
i Consumers f
5 Power f Company General Offices: 212 West Michigan Avenue. Jackson, Michigan 49201. Area Code 517788-0560 September 10, 1976 s
K 9: p,,
i O'?
C[g. $g *Q]V,
gl t 3' Mr James G. Keppler
- w # f s,ac.
Office of Inspection & Enforcement N
4k(,h N#
Region III US Nuclear Regulatory Ccemission 799 Roosevelt Road N /p';':7' '(3 Glen Ellyn, IL 60137 DOCKET 50-255, LICENSE DPR-20 PALISADES PLANT, ER-76-25 HYDROGEN RECOMBINER Attached is a reportable event related to the Palisades Plant. This event has been classified as a condition leading to operation in a degraded mode.
David A. Bixel (Signed)
David A. Bixel Assistant Nuclear Licensing Administrator 9419 copy SENT REGIOR
.