ML20085E206
| ML20085E206 | |
| Person / Time | |
|---|---|
| Site: | Limerick |
| Issue date: | 05/31/1995 |
| From: | Gallagher M, Hendricks D PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9506160468 | |
| Download: ML20085E206 (11) | |
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PECO ENERGY
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Sanatoga, PA 19464-0920 T.S.6.9.1.6 i
June 12, 1995 Docket Nos. 50-352 l
50-353 e
i License Nos. NPF-39 NPF-85 U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, DC 20555
Subject:
Limerick Generating Station Monthly Operating Report For Units 1 and 2 Enclosed are the monthly operating reports for Limerick Units 1 and 2 for the month of May 1995 forwarded pursuant to Technical Specification 6.9.1.6.
i Very truly yours, Michael P. Gallagher Director - Site Engineering drh Enclosures cc:
T. T. Martin, Administrator, Region I, USNRC N. S. Perry, USNRC Senior Resident Inspector LGS W. G. MacFarland, Vice President, LGS 1
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9506160468 950531 r
PDR ADOCK 05000352
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Attachment to Monthly Operating Report for May 1995 Limerick Generating Station Unit 1 -
l May 1 through May 31,1995 i
f 1.
Narrative Summary d Operating Experiences I
Unit 1 began the month d May at a nominal 100% d rated thermal power (RTP).
On May 7,1995, at 0021 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br />, power was reduced to 90% RTP for main turbine valve testing Following testing, the Unit commenced a shutdown to perform maintenance on the 'C' drain cooler, 'A' recirculation pump seal, and the condenser waterboxes. The reactor was scrammed at 0904 hours0.0105 days <br />0.251 hours <br />0.00149 weeks <br />3.43972e-4 months <br /> on May 7,1995. On May 10,1995, the mode switch was placed in startup and control rod withdrawal commenced shortly thereafter. The unit 1 reactor went critical at 1815 l
hours and on May 11,1995, at 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />, the mode switch was placed in run. The main i
generator was synchronized to the grid at 1227 hours0.0142 days <br />0.341 hours <br />0.00203 weeks <br />4.668735e-4 months <br />. Power was restored to 100% RTP on -
May 15,1995, at 0007 houm.
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Unit 1 ended this operating period at 100% d RTP.
i ll.
Challenges to Main Steam Safety Relief Valves There were no challenges to the Main Steam Safety Relief Valves during the month of May.
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AVERAGE DAILY UNIT POWER LEVEL e
DOCKET NO. 50 - 352 UNIT LIMERICK UNIT 1 DATE JUNE 09 1995 COMPANY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICM GENERATING STATION TELEPHONE (610) 718-3772 t
MONTH MAY 1995 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MwE-NET)
(MwE-NET) 1 1029 17 1051 2
1034 18 1047 3
1025 19 1064 4
1029 20 1050 5
1025 21 1051 6
1029 22 1059 7
190 23 1051 0
0 24 1047 9
0 25 1046 10 0
26 1054 11 91 27 1050 12 722 28 1053 13 924 29 1045 14 898 30 1045 15 1044 31 1054 16 1055
OPERATING DAVQ REPORT
+
DOCKET NO. 50 - 352 DaTE JUNE 09, 1995 COMPLETED BV PECO ENERGV COMPANY DAVID R.
HENRICKS REDORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 OPERATING STATUS 1
UNIT NAME: LIMERICM UNIT 1 NOTES: THERE WAS 1 LOAD DROP 2.
REPORTING PERIOD:
MAV. 1995 GREATER THAN 20% THIS MONTH 3.
LICENSED THERMAL POWER (MWTi:
3293 DUE TO A SHUTDOWN TO PERFORM 4
NAMEPLATE RATING (GROSS MWE):-
1092 MAINTENANCE.
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5.
DESIGN ELECTRICAL RATING (NET MwE):
1055 l
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- 6. MAXIMUM DEPENDABLE CAPACITY (GROSS MwE): 1092 I
7.
MAXIMUM DEPENDABLE CAPACITY (NET MWE):
1055 i
8.
Ir CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:
9.
POWER LEVEL TO WHICH RESTRICTED. IF ANV (NET MWE):
- 10. REASONS FOR RESTRICTIONS. IF ANY:
THIS MONTH VR-TO-DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD 744 3.623 81.767
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 662.8 3.522.3 67.630.6
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 14 HOURS GENERATOR ON-LINE 644.6 3.485.8 66.511.3
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
- 16. GROSS THERMAL ENERGV GENERATED (MWH) 2.094.746 11.400.182 205.716.720
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 667.400 3.709.900 66.894.180
- 18. NET ELECTRICAL ENERGY GENERATED (MWH) 644.273 3.586.878 64.230.884 PAGE 1 05 2
OPERATING DATQ REPORT (CONTINUED)
DOCCIET NO. 90 - 352 DATE JUNE 09. 1995 THIS MONTH VR-TO-DATE CUMULATIVE
- 19. UNIT SERVICE FACTOR 86.6 96.2 81.3 2C. UNIT AVAILABILITY FACTOR 86.6 96.2 81.3
- 21. UNIT CAPACITY FACTOR (U51NG MDC NET) 82.1 93.8 74.5
- 22. UNIT CAPACITY FACTOR (USING DER NET) 82.1 93.8 74.5
- 23. UNIT FORCED OUTAGE RATE O.0 1.1 4.1
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):
- 25. IF 5HUTDOWN AT END OF REPORT DERIOD. ESTIMATED DATE OF STARTU":
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 12/19/84 12/22/84 INITIAL ELECTRICITV MID APRIL 85 4/13/85 COMMERCIAL OPERATION IST QTR 86 2/01/86 PAGE 2 OF 2
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I e-UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 352 UNIT NAME LIMERICK UNIT 1 DATE JUNE 09 1995 REPORT MONTH MAv. 1995 COMPLETED BV PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 l
l UETHOD OF l LICENSEE SYSTEMLCOMPONENTl CAUSE AND CORRECTIVE l
TYPE DURATION REASON 15 HUTTING DOWN!
EVENT CODE CODE I ACTION TO NO.l DATE (1)
(HOURS);
(2) l REACTOR (3) l REPORT a (4)
(5) i PREVENT RECURRENCE I
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64 1 950507 l 5 000.0 B
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N/A HA VALVEX l REACTOR POWER WAS REDUCED TO 90.0% FOR 4
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l MAIN TURBINE VALVE TESTING.
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65 950507 5
099.4
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B 2
N/A HH HTEXCH l REACTOP WAS SHUTDOWN TO PERFORM MAINT.
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ON "C"
DRAIN COOLER.
"A" RECIRCULATION 4
PUMP SEAL. AND THE CONDENSER WATERBOXES.
4 4
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99.4 l
(1)
(2)
(3)
(4)
F - FORCED REASON METHOD EXHIBIT G - INSTRUCTIONS 5 - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMINATION F - ADMINISTRATIVE (5)
G - OPERATIONAL ERROR (EXPLAIN)
H - OTHER(EXPLAIN)
EXHIBIT I - SAME SOURCE l
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Docket No. 50-353 j
Attachment to Monthly Operating Report for -
May 1995 Limerick Generating Station Unit 2 May 1 through May 31,1995 j
l.
Narrative Summary of Operating Exoeriences i
i Unit 2 began the month of May at a nominal 100% of rated thermal power (RTP).
On May 6,1995, at 0020 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />, power was reduced to 90% RTP for a control rod pattom i
adjustment. Power was restored to 100% RTP at 0338 hours0.00391 days <br />0.0939 hours <br />5.588624e-4 weeks <br />1.28609e-4 months <br />.
On May 15,1995, at 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />, power was reduced due to high turbine backpressure Power was reduced to 91.5% RTP. Power was restored to 100% RTP at 1945 hours0.0225 days <br />0.54 hours <br />0.00322 weeks <br />7.400725e-4 months <br />.
On May 16,1995, at 1411 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.368855e-4 months <br />, power was reduced due to high turbine backpressure Power i
was reduced to 96% RTP, Power was restored to 100% RTP at 2025 hours0.0234 days <br />0.563 hours <br />0.00335 weeks <br />7.705125e-4 months <br />.
On May 17,1995, at 1446 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.50203e-4 months <br />, power was reduced due to high turbine backpressure. Power was reduced to 90% RTP. Power was restored to 100% RTP at 2135 hours0.0247 days <br />0.593 hours <br />0.00353 weeks <br />8.123675e-4 months <br />.
t On May 18,1995, at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, power was reduced due to high turbine backpressure. Power was reduced to 96.5% RTP. Power was restored to 100% RTP at 1950 hours0.0226 days <br />0.542 hours <br />0.00322 weeks <br />7.41975e-4 months <br />.
Unit 2 ended this operating period at 100% of R1P.
f II.
Challenges to Main Steam Safety Relief Valves There were no challenges to the Main Steam Safety Relief Valves during the month of May.
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'o QVEROGE DOILY UNIT POWER LEVEL DOCKET NO. 50 - 353 UNIT LIMERICK UNIT 2 DATE JUNE 09. 1995 COMDANY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORT 5 ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772 MONTH MAY 1995 DAY AVERAGE DAILY POWER LEVEL DAV AVERAGE DAILY power LEVEL (WWE-NET)
(MwE-NET) 1 1122 17 1081 2
1125 18 1094 3
1117 19 1122 4
1117 20 1114 5
1118 21 1118 6
1103 22 1127 7
1109 23 1123 8
1119 24 1114 9
1116 25 1119 10 1111 26 1121 11 1107 27 1122 12 1109 28 1127 13 1110 29 1114 14 1117 30 1114 15 1085 31 1125 10 1106
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OPERQTING DaTo REPORT DOCMET NO. 50 - 353 DATE JUNE 09, 1995 COMPLETED BY PECO ENERGY COMPANY DAVID R.
HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 710-3772 OPERATING STATUS 1.
UNIT NAME: LIMERICK UNIT 2 l NOTES: THERE wERE NO LOAD DROPS I
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2.
REPORTING PERIOD:
MAv. 1995 GREATER THAN 201f. THIS MONTH.
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3.
LICENSED THERMAL POWER (wwT):
345B l
4 NAMEPLATE RATING (GROSS MwE):
1163 I
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DE$1GN ELECTRICAL RATING (NET MWE):
1115 l
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MAXINUM DEPENDABLE CAPACITY (GROS 5 MwE): 1155 7.
max!NUM DEPENDABLE CAPACITY (NET MWE):
115 B.
IF CMANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:
9.
POWER LEVEL TO WHICH RESTRICTED. IF ANY (NET MWE):
- 10. REASONS FOR RESTRICTIONS. IF ANY:
THIS MONTH v7-TO-DATE CUMULATIVE 11 HOURS IN REPORTING PERIOD 744 3.623 47.279
- 12. NUMB ER OF HOURS REACTOR WAS CRITICAL 744.0 3.103.4 42.466 4
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 14 HOURS GENERATOR ON-LINE 744.0 2.995.8 41.600.7
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
- 16. GROSS THERMAL ENERGv GENERATED (MwH) 2.564.933 9.073.472 131.303.055 17 GROSS ELECTRICAL ENERGY GENERATED (MwH) 856.000 3.015.900 43.399.480
- 18. NET ELECTRICAL ENERGY GENERATED (MWM) 828.631 2.910.017 41.812.217 PAGE 1 OF 2
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OPERATING DATA REPORT (CONTINUED)
DOCKET NO. 50 - 353 DATE JUNE 09 1995 l
THIS MONTH VP-TO-DATE CUMULATIVE
- 19. UNIT SERVICE FACTOR 100.0 82.7 88.0
- 20. UNIT AVAILABILITY FACTOR 100.0 82.7 88.0 21 UNIT CAPACITV FACTOn (USING WDC NET) 99.9 72.6 83.6
- 22. UNIT CAPACITV FACTOR (USING DER NET) 99.9 72.6 83.6
- 23. UNIT FORCED OUTAGE RATE O.0 2.6 3.4 24 SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):
- 25. IF SHUTDOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
' (
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 08/12/89 08/12/89 INITIAL ELECTRICITY 09/01/89 09/01/89 COMMERCIAL OPERATION 02/01/90
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PAGE 2 OF 2
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UNIT SHUTDOONS QND POWER REDUCTIONS DOCnET NO. 50 - 353 b-UNIT NAME LIMERICM UNIT 2 DATE JUNE 09 1995 REPORT WONTH MAY. 1995 COMPLETED BY PECO ENERGY COMPANY DAVID R. HENRICKS REPORTS ENGINEER SITE ENGINEERING LIMERICK GENERATING STATION TELEPHONE (610) 718-3772
.___.._---__-.________._-. -_-_...__.....__________..._________._-_______.___-~__-___.____..-________..__ __.___......._.._.
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l METHOD OF l LICENSEE ISYSTEMICOMPONENTl CAUSE AND CORRECTIVE l
lTVPElDURATIONlREASONj$ HUTTING DOwn!
EVENT l CODE CODE l ACTION TO NO.l DATE i (1)) (HOURS){
(2) i REACTOR (3) l REPORT
- 1 (4)
(5)
I PREVENT RECURRENCE i
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49 950506 1 5 000.0 i
B 4
i N/A RB CONROD 1 REACTOR POWER WAS REDUCED TO 90% DUE TO 4
1 1
l l CONTROL ROD PATTERN ADJUSTMENT 4
1 1
1 50
- 9505t5 1 5 000.0 i
B.
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N/A HC HTEXCH REACTOR POWER wAS REDUCED TO 92% DUE TO 4
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l H C.H TURBINE BACK PRES 5URE.
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51 1 950516 l 5 000.0 B l 4
l N/A HC l HTEXCH REACTOR POWER WAS REDUCED TO 96% DUE TO 4
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HIGH TURBINE BACk PRESSURE.
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52 950517 i S i 000.0 B l 4
l N/A HC HTEXCH
. REACTCR POWER WAS REDUCED TO 90% DUE TO 4
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l HIGH TURBINE BACk PRESSURE.
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l 53 l 950518 I 5 000.0 B l 4
N/A i
HC HTEXCH I REACTOR POWER WAS REDUCED TO 97% DUE TO 4
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HIGH TURBINE BACK PRESSURE.
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(1)
(2)
(3)
(4)
F - FORCED REASON METHOD EX4IBIT G-INSTRUCTIONS S - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)
FILE (NUREG-0161)
E - OPERATOR TRAINING + LICENSE EXAMINATION F - ADMINISTRATIVE (5)
G - OPERATIONA. ERROR (EXPLAIN)
H - OTHER(EAPLAIN)
EXHIBIT I - SAME SOURCE
.. - -