ML20084U169

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LER BFRO-50-259/7620:on 760923,loop II Core Spray Sparger/ Vessel Dp PdIS-75-56 Found Valved Out.Caused by Personnel Error.Instrument Left Valved Out Following Maint.Section Instruction Ltr to Be Issued
ML20084U169
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 10/22/1976
From: Fox H
TENNESSEE VALLEY AUTHORITY
To: Moseley N
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
LER-BFRO-50-259-762, NUDOCS 8306270084
Download: ML20084U169 (2)


Text

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Q TENNESSEE VALLEY AUTHORITY CHATTANOOGA TENNESSEC 374o1 f

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Q Mr. Norman C. Moseley, Director f

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230 Peachtree Street, NW., 8th Floor Atlanta, Georgia 30303

Dear Mr. Moseley:

TEICIESSEE UTHORITY - BROWHS FERRY UUCLEAR PIANT UNIT 1 -

DOCKET NO.

0-2

- FACILITY OPERATING LICENSE DPR REPORTABLE l

OCCURRENCE (TBFRO-50-259/7620 The enclosed report is to provide details concerning the loop II core spray sparger/ vessel DP (PdIS-75-56) which was found valved out. This report is submitted in accordance with Browns Ferry Technical Specifi-cations Section 6.

This event occurred on Browns Ferry Nuclear Plant unit 1.

Very truly yours, TENNESSEE VALLEY AUTRORITY t

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H. S. Fox i

Director of Power Production Enclosure (3)

CC (Enclosure):

l Director (3) l Office of Management Information and Program Control U.S. Nuclear Regulatory Co=nission 1

Washington, D.C.

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Director (10) 4 I

Office of Inspection and Enforecment U.S. Nuclear Regulatory Commission 4

Washington, D.C.

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