ML20084S564

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Supplemental RO 50-254/76-25:electrical Nitrogen Vaporizers Installed on Nitrogen Makeup Sys.Installation Should Prevent Future Recurrences
ML20084S564
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 10/04/1976
From: Gerner L, Kalivianakis N
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
NJK-76-368, RO-50-254-76-25, NUDOCS 8306170112
Download: ML20084S564 (2)


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s aN J. Keppler, Regional Director s

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Region ill U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 References 1) quad-Cities Nuclear Power Station Docket No. 50-254, DPR-29, Unit 1 Appendix A, Sections 3.7.A.2 and 6.6.B.I.c

2) Reportable Occurrence Report RO 50-254/76-25 Enclosed please find a Supplernental Report for RO 50-254/76-25 for quad-Cities Nuclear Power Station. This occurrence was previously reported by our letter NJK-76-300 dated August 12, 1976.

Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION

' W N. J. Kalivianakis Station Superintendent l

NJK/LFG/1k bei cc:

G.A. Abre11 Ohh54 OCT 18 1976 O

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DOCKET NUMBER FVENT DATE REPORT DATE O 1 CON'T l l

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[T_l y l015 l o l-l 012 l 5l 41 l017121917161 l1 lo lo 14 17 16l 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION gg l Electrical nitrogen vaporizers have been installed on the Nitrogen Make-up system, l

7 89 80 35 l and are currently in operation. This should prevent. future recurrences of this type. l 7 89 Bn EE l These units have " cold" valves downstream of the vaoorizers. which are desianed to l

7 89 80 DE l Isolate on a given low temperature, thereby preventing non-vaporized nitrogen from l

7 89 80 DG l entering the nitrogen makeup system. A modification has been initiated to install l

7 89 80 pnug DE CODE COMPONENT CODE SUPPUER M

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10 12 13 44 45 48 80 ACTMTV COATENT RELEASED OF RELEASE l AMOUNT OF ACTMTY LOCATON OF RELEASE Q

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7 89 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTON 3[ l lN l Al l

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7 89 11 12 80 OFFSITE CONSEGUENCES X

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7 89 80 LOSS OR OAMAGE TO FA;ruTY TYPE DESCRIPTON D2 [_Z_j l

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7 89 80 AOOITIONAL FACTORS D@ l (EVENT DESCRIPTION CONT) this same type of valve downstream of the steam vaporizer to l 7 89 80 DE l the nitrogen purge system.

(R0 50-254/76-25) l 7 89 80 NAME:

Lawrence F. Gerner 309-654-2241 ext. 157 PHONE:

sPo ees.eer