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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20217G7821997-07-22022 July 1997 Special Rept:On 970227,ECCS Sys Was Actuated & Injected Water in Rcs.Declared HPCI Subsystem Operable Following Restoration of Subsystem to Normal Standby Lineup ML20097D4661992-05-27027 May 1992 Special Rept,Reflecting Quad-Cities Nuclear Power Station, Unit 2 Summary Status of Fuel Performance at End of Cycle 11. No Sipping Performed on Reload Fuel Assemblies at End of Cycle 11 ML20066J6331991-01-31031 January 1991 Forwards Summary Status of Fuel Performance for End of Cycle 11 ML20207P1881987-01-0606 January 1987 Special Rept:Summarizes Status of Fuel Performance as of End of Cycle 8.Of 2031 Assemblies used,289 Determined to Have Failed & Discharged as Leaker Assemblies.Aug 1986 Sipping Tests Showed No Indication of Assembly Failure ML20082P6541983-12-0505 December 1983 Telecopy RO 50-83/20-01T:on 831202,review of Ultrasonic Test Data Obtained During Current Refuel Outage Revealed Circumferential Linear Indication in Heat Affected Zone of Weld 02B-S9.Further Info Expected within 14 Days ML20078J8531983-10-12012 October 1983 Telecopy Ro:On 831011,during Performance of Ultrasonic Insp of Cleanup Sys Piping,Crack Indication Discovered in Heat Affected Zone of Weld 12S-S27 of Line 2-1202-6A.Further Info to Be Provided within 14 Days ML20084S1401977-05-13013 May 1977 Ro:On 770512,unit Experienced Sudden Turbine Control Valve Opening Resulting in Feedwater Flow Increase & Reactor Scram from APRM flux.Short-term Reactivity Increase Corresponding to Reactor Period of Less than 5s Experienced ML20084S1531977-05-0909 May 1977 Ro:On 770507,station Experienced Momentary Short Period of Less than 5s During Shutdown Margin Demonstration.Similar Experience Occurred on 770504.Addl Info Will Be Submitted in RO 50-254/77-23 ML20084S1901977-02-17017 February 1977 Telecopy Ro:On 770217,info Received by Station Indicated That MAPLHGR Limit Curves Given by Tech Specs Shall Be Additionally Lowered.Reduction Resulted from Review of ECCS Analysis.Maplhgr Curves Lowered Effective 770217 ML20084S2041977-01-18018 January 1977 Telecopy Ro:On 770118,info Received by Station Indicated That MAPLHGR Limit Curves Shall Be Lowered.Reduction Resulted from Review of ECCS Analysis.Curves Lowered ML20084S3501977-01-0404 January 1977 RO-50-254/76-37:on 761205,limit for Having No More than 2 Ci Activity in Radwaste Tank Farm in 24h Exceeded. Caused by Deterioration of Effectiveness of Radwaste Sys to Perform as Designed.Radwaste Sys Being Updated ML20084S3551976-12-30030 December 1976 RO 50-254/76-36:on 761202,cooling Water Suction Header Common to Both RHR Containment Cooling Loop 1A & Diesel Generator 1 Cooling Water Pump Airlocked.Caused by Procedure Inadequacy.Maint Procedures Will Be Revised ML20084S2861976-12-28028 December 1976 RO 50-254/76-38:on 761215,GE Notified Util That NRC Discovered Errors in Code Inputs to ECCS App K Analysis, Caused by GE Incorrectly Applying Data for ECCS App K Analysis.Maplhgr Curves Reduced by 4% ML20084S3391976-12-16016 December 1976 Ro:On 761215,preliminary Info Received by Station Indicated That MAPLHGR Curves Should Be Lowered by 4%.Change Resulted from Review of ECCS Analysis.Curves Lowered ML20084S3611976-12-16016 December 1976 RO 50-254/76-35:on 761203,discovered Discrepancy Between Tech Spec & Nedo 20360 Rod Worth Minimizer Operable Rated Power.Orders Written in Daily Order Book Requiring Rod Worth Minimizer Operability Below 20% ML20084S3701976-12-0303 December 1976 Ro:On 761203,info Received Indicated That Rod Worth Minimizer (RWM) Operability Requirements Should Be Changed from 10% to Below 20% Rated Power.Caused by Review of Rod Drop Accident Analysis ML20084S3791976-11-22022 November 1976 Updated RO 50-254/76-33:on 761029,repairs to RCIC Pump Consisted of Rebuilding Pump Casing & Installing New Rotary Element.Pump Reassembled & Repairs Completed by 761111.Welds on Piping Acceptable ML20084S3771976-11-12012 November 1976 RO 50-254.76-34-on 761104,electromatic Relief Valves 1-203-3C & 1-203-3E Failed to Open When Actuated from Control Room.Caused by Excessive Steam Leakage Into Area Below Valve Disc.Investigation in Progress W/Manufacturer ML20084S3941976-11-10010 November 1976 RO 50-254/76-33:on 761029,while Performing RCIC Sys Pump Operability Surveillance,Discovered That Pump Could Not Achieve Flow & Pressure Required.Caused by Two of Five Stages Being Severely Damaged.Pump Being Rebuilt ML20084S5421976-10-30030 October 1976 Updated RO 50-254/76-26:on 760803,rod Worth Minimizer Not Operable for Withdrawal of First Twelve Control Rods to Fully Withdrawn Position While in Startup Mode.Caused by Burned Out Wire Runs on Relay Board.Software Modified ML20084S4031976-10-13013 October 1976 RO 50-254/76-32:on 761001,main Chimney Monitoring Sys & Reactor Bldg Vent Sample Sys Not Functioning Properly.On 760919,flexible Sample Hose Wrapped W/Tape to Stop Possible Leak.Caused by Failure of Flexible Suction Hose ML20084S5641976-10-0404 October 1976 Supplemental RO 50-254/76-25:electrical Nitrogen Vaporizers Installed on Nitrogen Makeup Sys.Installation Should Prevent Future Recurrences ML20084S4761976-10-0404 October 1976 RO 50-254/76-31:on 760920,station Informed by GE of Error in Reload 2 Licensing Submittal in Determining Max Change in Critical Power Ratio Due to Abnormal Operating Transient. Caused by Incorrect Analysis in Preparing Submittal ML20084S4831976-09-21021 September 1976 RO Re Notification by GE of Oversight in Reload 2 Licensing Submittal Leading to Possible Nonconservative Operation During Cycle 3.Work Request to Lower Rod Block Monitor Line to 10% at Full Flow Initiated ML20084S5031976-09-0909 September 1976 RO 50-254/76-29:on 760809,surveillance of Primary Containment Oxygen Concentration Revealed Increase in Concentration from 4.2 to 4.8%.Caused by Instrument Drift. Oxygen Analyzer Recalibr ML20084S5151976-09-0707 September 1976 RO 50-254/76-28:on 760809,position Indication Lost on Reactor Water Cleanup Sys Isolation Valve Mo 1-1201-2.Caused by Relay 595-125 Shorting Out & Burning Up Control Transformer.Relay & Transformer Replaced ML20084S5781976-08-26026 August 1976 RO 50-254/76-24:on 760727,reactor Bldg to Suppression Chamber Vacuum Breaker Pressure Switch PS-1-1622B Tripped at 0.536 Psid.Caused by Instrument Setpoint Drift.Switch Recalibr ML20084S5241976-08-19019 August 1976 RO 50-254/76-27:on 760806,ECCS Analysis Performed by GE for BWR-3 Type Plant Resulted in Calculated Peak Clad Temp Greater than 2,200 F for Reduced Core Flows.Caused by Severity of Conservatisms Associated W/Using App K ML20084S5511976-08-16016 August 1976 RO 50-254/76-26:on 760803,rod Worth Minimizer Multiple Output Distributor Error Detected.Caused by Burned Out Wire Runs on Relay Board.Board Repaired & Hardware & Software Mods & Procedural Changes Being Considered ML20084P7411976-06-23023 June 1976 Telecopy Ro:Initial Swipe Survey of Nuclear Fuel Svcs NFS-4 Cask Indicated Three of 38 Tests Exceeded Limits ML20084P7551976-06-17017 June 1976 Telecopy Ro:On 760617,HPCI Sys Motor Speed Changer Failed to Come Off Low Speed Stop During Monthly Surveillance.Caused by Motor Speed Changer Linkage Being Bound.Linkage Freed ML20084S4131976-03-30030 March 1976 Telecopy Ro:On 760330,suppression Chamber Water Level Instrumentation Found Miscalibrated.Suppression Chamber Water Level Immediately Returned to Normal.Addl Info Will Be Submitted in RO 50-265/76-04 within 14 Days ML20084Q1751976-03-26026 March 1976 Telecopy Ro:On 760326,chemical Waste Sample Tank Discharged to River at Rate in Excess of Limits ML20084S4151976-01-0909 January 1976 Telecopy Ro:On 760108,while in Cold Shutdown,Crack Indications Found on a & B Loops in valve-to-pipe Junctions on Sides of Bypass Valve That Cannot Be Isolated & in Heated Zones ML20084S5091976-01-0505 January 1976 RO 50-254/76-1:on 760105,w/unit in Cold Shutdown for Refueling,Pinhole Leak Found in Fillet Weld of 3/4 Inch Drain Line.Caused by Degradation of Reactor Coolant Primary Boundary.Work Request Being Issued ML20084S5311975-12-31031 December 1975 RO 50-265/75-47:on 751231,w/unit Operating at 805 Mwe, Reactor Core Isolation Cooling (RCIC) Trip Throttle Valve Could Not Be Reset Following Successful Monthly Surveillance Functional Testing.Hpci Tested & Found Operable ML20084U2081975-02-25025 February 1975 Ro:On 750212,following Verification of Reactor core,mixed- Oxide Fuel Assembly Identification Number Stamped in Wrong Orientation Discovered.Caused by Mfg Error.Fuel Insp Procedure Changed to Verify Number Orientation as Correct ML20084U2121975-02-20020 February 1975 Ro:On 750212,during Core Spray Operational Hydrostatic Test, Water Observed Overflowing Reactor Bldg Floor Drain Sump 1B.Caused by Premature Actuation of Core Spray Discharge Header Relief Valves.Test Procedure Amended ML20085C9241974-11-15015 November 1974 Ro:On 741011,control Rod Drive N-11 Jammed Fully Inserted Past Position 00 & Would Not Withdraw After Increasing Drive Pressure.Caused by Broken Seals on Stop Piston.Drive N-11 Replaced ML20085C9181974-11-15015 November 1974 Ro:On 741017,during Removal of Faulty Intermediate Range Monitor 18 Detector,Detector Became Stuck in Shuttle Tube. Caused by Coupling Between Shuttle & Drive Tubes Overtightened.New Shuttle Tube Ordered ML20084K5181974-06-26026 June 1974 Telecopy RO Re Setpoint Drift of Standby Liquid Control a Relief Valve.Valve Reset & Tested ML20084K6451974-06-22022 June 1974 AO 50-265/74-12:on 740612,high Differential Pressure Noted Across Combined High Efficiency & Carbon Filters.Caused by Exhausted High Efficiency Prefilter.Original Carbon Filters, New Rough Prefilters & New Efficiency Prefilters Installed ML20084K5461974-06-19019 June 1974 Telecopy Ro:On 740619,water Leak Discovered at Pressure Test Connection & Feedwater Line.Caused by Cracked Weld at Weldolet Line.Repairs in Process ML20084K5541974-06-19019 June 1974 Telecopy Ro:On 740619,water Leak Discovered at Pressure Test Connection & Feedwater Line.Caused by Cracked Weld at Weldolet Line.Repairs in Process ML20084K5891974-06-14014 June 1974 Telecopy Ro:On 740613,level Switch LIS-2-263-72D Failed. Switch Lightly Pressed & Functioned Normally.New Switch Ordered ML20084K5941974-06-14014 June 1974 Telecopy Ro:On 740613,level Switch LIS-2-263-72D Failed. Switch Functioned Normally When Lightly Pressed.New Switch to Be Installed ML20084K6291974-06-13013 June 1974 Telecopy Ro:Level Switch Failed to Actuate Control Room Annunciator.Cause Under Investigation ML20084L0441974-06-10010 June 1974 Telecopy Ro:On 740609,high Water Conductivity Discovered in Reactor.Shutdown & Water Cleanup Initiated ML20084K8401974-06-10010 June 1974 Telecopy Ro:On 740610,feedwater Valve Failed.Caused by Wall Thickness Being Less than Design Min.Cleanup, Decontamination & Water Processing Initiated ML20084K8361974-06-10010 June 1974 Telecopy Ro:On 740610,feedwater Low Flow Valve Failed.Caused by Not Maintaining Min Wall Thickness.Radiation Released Not Above Normal Level.Decontamination,Cleanup & Water Processing Initiated 1997-07-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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- Com lth Edisin 'j Quad-Cities Nue! ear Power Station ~
IE FILE COPY Post Office Box 216 Cordova, Illinois 6* 242 Telephone 309/651-2241 A 5 NJK-76 395 ret $vE0 ev
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October 30, 1976 E illllf%"
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J. Keppler, Regional Director Office of Inspection and Enforcement Region lli U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137
Reference:
Quad-Cities Nuclear Power Station Docket No. 50-254, DPR-29, Unit 1 Appendix A, Sections 3.3.B.3.b and 6.6.B.I.b Enclosed please find an Update Report for Reportable'Occurr,ence Report No.
RO 50-254/76-26 for Quad-Cities N,uclear Power Station. This occurrence was previously reported to Region Ill, Office of Inspection and Enforcement en August 16, 1976.
Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION-
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//f f . A445 N. J. Kalivianakis Station Superintendent NJK/LFG/lk cc: G. A. Abrell
- 15. .!6 J 8306170098 770318 PDR ADOCK 05000254 S PDR NOV 111976
7 -.. ,
frNNuI$$rtM LICENSEE EVENT REN CCNTR LOCK:l l l l l l l (PLEASE PRINT ALL REQUIRED INFORMATION) 1 8 AME LCENSE NUMBER YPE YPE O1 ll lL lQl Al 0l 1l l0 l0 l-l 0 l 0 l 0l 0l 0l-l0 l0 l l 4 l 1 ll l1lll l0 l1 l 7 89 14 15 25 28 30 31 32 CATEGORY T ff OCCKET NUMBER EVENT DATE REPORf OATE D 1 CONT l l l y l0 l5 l0 l-10 l 2 l 5 l 4l l0 l8 l0 l 3 l 7 l 6 l 68 89 74 l1 lo l3 l0 l7 l 6 l 75 80 7 8 57 58 59 80 81 EVENT OESCRIPTION DE lAn Update Report is submitted to document the portion of Reportable Occurrence Report l 7 89 80 BE Ino 50-254/76-26 related to the improper rod sequence loading into tne Rod Worth l 7 89 80
@ l Minimizer. See attached summary. l 7 89 80 El 7 89 80 l
EXE I l 7 89 pas 80
' CEE CODE COMPONENT CODE SUPPUER ACTURER VOLATON M lRIBl W 7 89 10 11 lZl Zl Zl Zl Zl Zl 12 17 W43 44 l Gl 0l 8l 0l 47 U 48 CAUSE DESCRIPTION DE l NA l 7 89 80 BE I I 7 89 80
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's'TiG s power oTsER STATUS "ofSCoTERY oISCovERY oESCni, ton 1 y l0l0l0l l NA l @ l NA l 7 8 9 10 12 13 44 45 48 80 R LEAS 0 0 ASE AMOUNT OF ACTMTV LOCATON OF RELEASE 7 8
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PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTON DE I 010 l o I 7 89 11 l.ZJl 12 13 NA 80 l
PERSONNEL INJUR!ES NUMBER DESCRIPTON gg l 0l 0l 0 l l NA l 7 89 11 12 80 OFFSITE CONSEQUENCES DE l NA l 7 89 80 LOSS OR OAMAGE TO FACILITY TYPE DESCRIPTON g] Ql NA l 7 89 10 80 PUBLICITY DE I NA l 7 89 80 ADDITIONAL FACTORS l gg l NA l 7 89 80 DE I I 7 89 80 m e. Gary spedi pgggg;pW22M en. 242
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. e' REPORT NUMBER: 50-254/76-26 REPORT DATE! August 16, 1976 OCCURRENCE DATE: August 3, 1976 FACILITY: Quad-Cities Nuclear Power Station Cordova, Illinois 61242 IDENTIFICATION OF OCCURRENCE:
The Unit One rod worth minimizer was not operable for the withdrawal of the first twelve control rods to the fully withdrawn position while in the STARTUP mode as required by Technical Specification 3.3.B.3.b.
CONDITIONS PRIOR TO OCCURRENCE:
Urif t One was commencing rod withdrawals in anticipation of starting up following an outage to repair a primary containment purge line.
DESCRIPTION OF OCCURRENCE: On August 3, 1976 at 7:35 P.M., control rod withdrawal commenced in anticipation of starting up Unit One. At 8:38 P.M.
control rod withdrawal was halted after withdrawal of the 50th control rod. The rod worth minimizer was still displaying the 6th control rod to be withdrawn in group one, and was apparently not following the control rod withdrawals. At this point the control rod pattern was verified as being correct by both the control room operator and the Shift Engineer
- and subsequent rod withdrawals were verifled,by a Nuclear Engineer. , Unit One was not made critical on August 3,1976,. but had control rods withdrawn to Just short of critical. At 10:45 A.M. on August 4, 1976 all control rods were fully inserted due to delays in the primary containment purge line repair. The unit remained with all rods fully inserted until 6:33 A.M. on August 5, 1976 when control rod withdrawal again commenced in anti-cipation of starting up the unit. After successful completion of the pipe repair, Unit One was made critical on August 6,1976 at 4:33 a.m.
On August 4 the computer technician had repaired the rod worth minimizer and declared it operable for the startup on August 5, 1976. In the course of his maintenance repair work, however, he had brought the rod worth minimizer off line, repaired it, and reinitialized it with the wrong con-trol rod sequence loaded. The control rod sequence which should have been loaded, and the one which was loaded, were identical sequences through control rod group 6. Groups 7 and 8 on the improper sequence were identical to groups 7 and 8 on the proper sequence, but were in reverse order.
Both sequences were substantially different from Groups 9 and up.
After the reactor criticality on August 6, 1976, which occurred in rod group 5, control rod withdrawal continued through group six with the rod worth minimizer functioning properly. Then, the operator failed to follow the specified sequence and skipped group 7 and went on to withdraw group 8.
The rod wor.th minimizer followed the withdrawal of group 8 instead of 7 as proper insequence rod withdrawals. The operator then discovered that a group had been skipped and returned to group 7 to complete the rod with-drawals. The rod worth minimizer followed the withdrawal of group 7 after l
group 8 as proper Insequence rod withdrawals. But when the operator moved on to group 9, the rod worth minimizer properly applied rod blocks. The rod worth minimizer was subsequently bypassed with control rod withdrawal continuing with an extra control room operator verifying the rod withdrawals.
The sequence was loaded and the rod worth minimizer was reinitialized at l 11:00 a.m. on August 6, 1976.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
Equipment Failure On August 3,1976, af ter withdrawal of the sixth rod in group one, a diode in the rod position / error message output window display circuitry of the rod worth minimizer failed. This overload failure was detected as a distributor error by the multiple output distributor error detection circuitry, and a signal was sent to apply rod insert and withdrawal blocks as part of the fall-safe design of the rod worth minimizer. The rod insert and withdrawal blocks were never applied, however, because a wire run on relay card KHSK2 was burned out and discontinuous.
The rod worth minimizer program itself, upon detection of a multiple output distributor error, is designed to display the appropriate error message in the control room. When an overload error is detected in a circuit whose function is to display messages in the control room, the rod worth minimizer program goes into an Iterative loop and indicates on the displays in the control room that there is a hardwa.re failure. .This is accomplished by lighting the red alarm light but' not displaying a particula,r message *. The rod selected display remains in the mode of display that was present when the hardware failure occurred. An attributing cause to this occur'rence was the control room operator's failure to notice that the rod worth minimizer was not following the selection and movement of the 7th rod in group one on August 3, 1976. Had he done so, control rod movement could have been halted until the rod worth minimizer was repaired.
The loading of the rod worth minimizer on August 4, 1976 with the incorrect sequence may be attributed to poor communication between the Nuclear Engineers of the Technical Staff and the computer technician, as well as poor documen-tation and filing of rod worth minimizer sequences. There is also a pro-cedural Inadequacy apparent in the operating procedure dealing with verifi-cation that the proper sequence has been loaded into the rod worth minimizer, by checking only the first five groups of the minimizer's sequence against that supplied to the unit operator.
ANALYSIS OF OCCURRENCE:
At'no time during this occurrence did there exist an unsafe condition. On August 3, 1976 the control rod sequence was properly followed and implemented.
On August 6, 1976, even though the wrong sequence was loaded in the rod worth minimizer, it was an approved sequence and one used previously at quad-Cities Station. Even though the operator skipped a group on the control rod sequence supplied to him, the rod worth minimizer was performing its function in making sure that the operator did not make an unsafe rod with-d rawa l . The actual sequence of control rod withdrawals used on August 6, 1976 was a completely safe one.
u
I .. ". l That which was experienced was a fall-safe failure of the rod worth minimizer, a subsequent defeating of the computer fall-safe ability, and then a failure on August 3, 1976. With the burned out wire run on the relay card KHSK2,
,a subsequent hardware failure of the type experienced does not result in the safe application of rod insert and withdrawal blocks.
CORRECTIVE ACTION:
After the initial action by the operator and the Shif t Engineer on August 3, 1976 to verify that all the control rods were in their proper-Insequence location, the computer hardware technician was notified that the rod worth minimizer was inoperable. His investigation revealed the burned out relay board, the failed diode, and also a bad power supply to the rod worth minimizer.
The rod worth minimizer circuitry responsible for applying rod insert and withdrawal blocks is powered by a 28 volt D.C. power supply. The rod worth minimizer multiple output distributor is powered by a separate 28 volt D.C.
power supply. If a multiple output distributor error occurs, the K-15 relay picks up and seals in, and applies rod insert and withdrawal blocks.
This function parallels the two 28 volt D.C. power supplies, and, as long as both power supplies are putting ou. an accurate 28 volts D.C., everything a
functions safely and normally. However, if one of the power supplies drif ts significantly and the two power supplies are at different potentials, a current flow is established between the two power supplies. If the power supply drift is significant enough, the current flowing can exceed what certain relay board wire runs can handle, and the runs burn up. Since the K-15' rod block initiatin.g relay l's.a. seal-in relay capable. of being powered
- by either of the 28 volt D.C. power supplies, the' rod' blocks remain safely applied until the Error-Clear b'utton is pushed in the process of reinitializing the rod worth minimizer. This de-energizes the K-15 relay and, upon subsequent multiple output distributor errors with the relay card wire runs burned out, the error is detected. However, the rod blocks are not applied because the current signal to the K-15 relay does not get through the burned out wire run. This occurred on Unit One on August 3, 1976.
At some previous time, a power supply drift was experienced at the instant an error message was received. This paralleled the two mis-matched power supplies, burning up some relay board wire runs. The burned up relay boards went undetected and the rod worth minimizer was reinitialized after pushing the Error Clear pushbutton foliowing correction of the initiating problem.
Then, on August 3,1976, an error message was again received, this time from a faulty diode. The control room display panel remained unchanged from what was displayed at the time of the diode failure, and the rod blocks were not received because of the burned out relay board.
The faulty power supply has been replaced and the preventive maintenance schedule has been changed for these power supplies to increase surveillance of their performance. The burned out relay board has been replaced as well as the bad diode. Access to the Error Clear pushbutton in the computer room will be restricted by keeping the rod worth minimizer panel in the computer room locked with only the computer hardware technician, computer engineering assistant, and the Shif t Engineer possessing a key. The operating procedure for the rod worth minimizer will be revised to caution the operators in the control room to only interface with the rod worth minimizer from the panel r -
r in the control room. If an error condition cannot be achknowledged and cleared from the control room, it is an indication of a serious type failure requiring the presence of the computer hardware technician. The computer hardware technician, aware of the potential for burned out relay boards, will always check for such failures each time he clears an error condition on the rod worth minimizer before returning to operation. Such actions should be sufficient to prevent this type of occurrence from happening again.
Additional corrective actions taken to improve station performance in this area are as follows:
- 1. Company computer systems personnel have been requested to mod!fy the rod worth minimizer software to place the rod worth minimizer in a STALL condition upon receipt of an overload type multiple output dis-tributor error. This will provide an independent and redundant rod block signal in the event of an overload error.
- 2. The procedure for checking out the rod worth minimizer prior to startup will be changed to require verification of the rod worth minimizer's first ten rod groups to insure the proper sequence is loaded.
3 A rod worth minimizer log book will be instituted which will document any maintenance work performed on the rod worth minimizer. Operational information, such as which sequence is presently loaded in each unit's rod worth minimizer, will also be documented.-
- 4. The computer hardware t'echnician will require station work requests to accompany any work he performs on the rod worth minimizers, which he feels requires documentation and testing by operations personnel before placing it back in service.
5 The computer hardware technician will investigate wiring changes to the rod worth minimizer in an attempt to supply the special error detection 28 volt D.C. Input to the relay buffer from the same power supply that supplies the relay buffer. This change will eliminate the difference in potential in the relay buffer if a power supply were to faII.
These added measures are expected to improve upon the performance of the rod worth minimizers.
FAILURE DATA:
This is the first occurrence of this type at quad-Cities Station. The power supply that drifted was a 28 voit D.C. peripheral power supply, G.E. part number 68A8451Pil2. The diode which failed and initialed the circumstances !
of this occurrence was a G.E. part number 68A201P3 diode. There are no safety implications based on cumulative experience.