ML20084S483
| ML20084S483 | |
| Person / Time | |
|---|---|
| Site: | Quad Cities |
| Issue date: | 09/21/1976 |
| From: | Kalivianakis N COMMONWEALTH EDISON CO. |
| To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| Shared Package | |
| ML20084S480 | List: |
| References | |
| NJK-76-351, NUDOCS 8306170054 | |
| Download: ML20084S483 (2) | |
Text
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b h Edison O
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OdacCrics t car Power Sto'ca
(%(iQN,.dW'7 Cordova. I! boo:s G1242 PoM Omce Dot ?)G Telephone 3D9/054-2241 '
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J. Keppler, Regional' Director
, Office of Inspectfon; and. Enforcement 2'
Reglon !Il' U. S. Nucicar Regulatory Commission 799 Roosevelt Road Glen.Ellyn, 111tnois.60137 Referencet-quad-Cities Nuclear Power Station, Unit 17 Docket Ho-. 50-254, DPR-29 Appendir A,. Sections 3 2.C Il; 6.6.1LI ht Dear Mr. Keppler-The purpose of this letter is to provida you with notification of a Reportable Occurrence as required by Technical-Specification 6.6.B. T' i
within,24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the occurrence.
The General Electric Company has notified.Cournonwealth' Edicon's Rucicar Fuel Services department, who has in. turn. notified the station, of an-
' oversight in the Quad-Cities Unit One Reload Two Licensing Submittal j
iesding to possible non-conservative operation of the unit during cycle 3.
For a. Rod Block. Monitor (UDH) rod block line setpoint of IIO% at rated flow, the !! censing submittal shows the Rod Withdrawal Error (RVE).
to be the liraiting: Minlaum Critica1' Power-Ratio-(MCPR)' transient.. This.
was apparently overlocked when determining. the MCPRcoperating limits for
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i Cycie 3 In order to-be able to. apply-tI>e MCPit 1imits. specified in, the 1 Tcensing. submittal' and our current Technical Specifications, the. RBM-5 rod block setpoint at fut t ' flow.n;ust be lowered to 107%.
r We' have. Initlated n. work request to-Iower the RBM rod: block line to;1073 at full flow,. and have verified that a Technical Specification: change request has been initiated. This action..wi ll' eliminate-the RWE as ' a-IYmiting transient and'will place us conservatively withih.the analysis i
of the submittal.
Rod ' movement has been. procedurally < Ilmited so-as to; j
minimize the possibil'ity.of. an P.VE and! ensure: safe unit operation.
8306170054 761004 gDRADOCK-05000254 PDR ui.
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This. occurrence was discussed by telephone with Mr.
C'. Feierabendtof your office on September 21. 1976.
Further inforr.ution. will'ba provided.
by. Reportable Occurrence Report RO 50-254/76-31:which will be submitted.
within 14 days of the date of this occurrence.
Very truly yours, COMMONVEALTH. E0 5 SON: COMPANY' QUA06 CITIES NBCLEAR POWER. STATION:-
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J. Kaifvfanakis Station Superintendent NJK/GS/Ik cc:
G. A. Abrell
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