ML20084Q099

From kanterella
Jump to navigation Jump to search
RO Re Problem Encountered During Repair of Bent Stem on RHR HX 2B Svc Water Discharge Valve Mo 2-1001-5B.Problem Being Referred for Review & Request for Piping Mod to Alleviate Condition Will Be Initiated
ML20084Q099
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 03/08/1974
From: Stephenson B
COMMONWEALTH EDISON CO.
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
References
BBS-74-49, NUDOCS 8306130122
Download: ML20084Q099 (2)


Text

. _ _ _ _ _ _ _

Commohlth Edison h

A Outd-Citia ven:r: ting Station l

1 Post Office Box 216

.h5 Cordova, Illinois 61242 Telephone 309/654-2241

/g /)[ k);

/

4 BBS-74-49

[,

\\i.

'4'

[.?'/

' G.% *..,

John F.

O' Leary, Director 6

e Directorate of Licensing

"'l'N Regulation U. S. Atomic Energy Commission Washington, D.

C.

20545

Subject:

Quad-Citics Nuclear Power Station Docket No. 50-254 & 50-265 DPR-29 & 30, Appendix A, Section G.6.B.2.c

Dear Mr. O' Leary:

As reported to you in my letter of February 7, 1974 a problem was encountered recently while performing maintenance on a Re-sidual Heat Removal (RHR). service wa.ter. system valve.- In

' 'fifwirig. thisl event we havkconcitid'ect"thist'the'-as-bnili. co.f.re-nditi6n.-

f f

of this system should be reported as an unusual event as described in section 6.6.B.2.c of the Technical Specifications since a possible single failure could result in a failure of the con-tainment cooling system to perform its intended function.

The maintenance referred to above was the repair of a bent stem on the 2B RHR heat exchanger service water discharge valve, MO 2-1001-5B.

The 14" discharge from the 2B heat exchanger joins the discharge from the 2A heat exchanger downstream of the 5B valve.

This 18" header from the heat exchangers goes to a 30" header and,then to.the 48" service water.sys. tem river discharge headei.* It. appear.s. that if.a. piping: failure were postulated to-occur downstream of the SB valve in the reactor building, oper-

)

ation of either containment cooling subsystem would be limited by the discharge of river water within the station.

SAFETY IMPLICATIONS The probability of such a failure occurring simultaneously with the analyzed loss of coolant accident is remote.

Any failure occurring during unit operation would be immediately obvious and necessitate a shutdown.

CORRECTIVE ACTION This problem is being referred to the Offsite Review and Investi-gation Function for review in accordance with section 6.1.G.l.a.

(3) of the Technical Speci'fications.

A reciues for a piping h

V'O{ fQPY SENTREGIOT

)t -

8306130122 740300 C#

p gDRADOCK05000g I{0

$a

r 3-

=

(.

()

()

Mr. J. F. O' Leary March 8, 1974 modification to alleviate this condition will also be initiated in accordance with Procedure 3-51 of the Commonwealth Edison Com-pany Quality Assurance Manual.

Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION i

D An B.

B.

St henson Station Superintendent BBS/lk cc:

Regional Director Directorate of Regulatory Operations-Region III

. ~....

f..%.

8*.**

- I

e =*k

  • ,,,g.

l

.