ML20084P534

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/03L-0:on 760709,two Control Rods Withdrawn Simultaneously.Caused by Personnel Not Following Established Procedures.Rods Inserted to 00.Procedural Changes Initiated
ML20084P534
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 08/07/1976
From: Kalivianakis N, Spedl G
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20084P514 List:
References
LER-RO-760807, NJK-76-292, NUDOCS 8306100306
Download: ML20084P534 (2)


Text

_ _ _ _ _ _ _ _ -

Com

lth Edison Quad-Cities Nuclear Power Stat on Post Office Box 216 Corcova, Ilknois 61242 Telepnone 309/654-2241 W

f NJ K-76-293 August 7, 1976

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J. Keppler, Regional Director g'2-ce E

  • ' 4 Office of Inspection and Enforcement Region ill (N'/

U. S. Nuclear Regulatory Commission 4

799 Roosevelt Road Glen Ellyn, Illinois 60137

Reference:

Quad-Cities Nuclear Power Station Docket No. 50-254, DPR-29, Unit 1 Appendix A, Sections 6.6.8.2.c.

Enclosed please find Reportable Occurrence Report No. 50-254/76-21 for Quad-Cities Nuclear Power Station.

This report is submitted to you in accordance with the requirements of Tech-nical Specification 6.6.B.2.

Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION

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, !..'I 8 Wh N. J. Kallvianakis Station Superintendent l

l NJK/GS/vmb g

cc:

G. A. Abrell R

8306100306 760929 PDR ADOCK 05000254 g

PDR 3301 AUG e 1976

kENSEE EVENT REPORT O CONTROL BLOCK:l l

l l

l l

l (PLEASE PRINT ALL REQUIRED INFORMATION) 1 8

AME LCENSE NUMBER E

YPE O1 liIt10lA I Dl1l l 0 l 0 l-l0 l 0 l 0 l 0 l 0 l-l0 l0 l l4 l1 l0 l0 l0 l l0l3l 7 89 14 15 25 26 30 31 32 CAftGORY TP E

DOCKET NUMBER EVENT DATE REPORT DATE 01 CONT l l

l lLl l 0l 51 01-l 0 l 215 l 41 l 01 7l 01 9l 7l 6 l l0l81017l716l 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCAIPTION HE lWith Unit One shutdown in the REFUEL mode, control rod drive replacement was l

7 89 80 SE l scheduled for five rods. The drive replacement was to be performed on the five rods l

7 89 80

- 35 l consecutively and not simultaneously on any two rods.

Because established procedures l 7 89 80 HE l were not adhered to, two rods were withdrawn simultaneously.

Shutdown margin was l

7 89 80 H(i l maintained during this occurrence.

(R0 50-254/76-21) l 7 89 80 pays CE CODE COMPONENT CODE ACTURER VOLATON O

lZl Zl W lZ l Z l Z l ZI Zl Z]

W lZl9l919l lN l 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION O

l 0oerating personnel did not follow established procedures. When this condition was l

7 e9 80 HE Idiscovered, all rods were inserted to 00.

Procedural changes were initiated to l

7 89 80 1

lorevent recurrence.

l S

U

% POWER OTHER STATUS OSCOVERY DISCOVERY DESCRIPTON W

l0l0l0l l NA l

lAl l

NA l

7 8 9

10 12 13 44 45 46 80 CTM CONTENT OFRELEASEl l

l NA l

RELEASED AMOUNT OF ACTMTV LOCATON OF RELEASE O

NA O

i 7 8 9

10 11 44 45 80 PEASONNEL EXPOSURES NUMBER TYPE DESCAPTION BE l 010l 0l W]

NA l

7 89 11 12 13 80 PERSONNEL INJURIES NUMBER CESCRIPTON DE I O! 0l 01 i

NA l

7 89 11 12 80 OFFSITE CONSEOUENCES BE I na l

7 89 80 LOSS OR DAMAGE TO FACILITY TYPE CEsCRIPTON dl NA l

9 7 89 10 80 PUBUCITY l

NA l

1 7 89 80 ADOITIONAL FACTOAS 1

l The second of the two rods withdrawn was done so wi th the mode switch in STARTUP.

l 7 89 80 l

l l The status of the plant was such that a unit startup could have commenced.

l 3g l

7 89 80 Gary Sped 1 l

NAME:

PHONE:

GPO 889 667