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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084F1431975-12-22022 December 1975 AO 251-75-12:on 751212,boron Concentration in Boron Injection Tank Measured 2% Below Lower Limit.Caused by Dilution of Unit 3 Bit W/Water from Safety Injection Sys Accumulator C Followed by Dilution of Boric Acid Tank ML20084F7031975-12-11011 December 1975 Supplementary Rept 3 to AO 251-75-4:on 750312,lateral Restraints for Spent Fuel Racks Found Broken.Cause Not Stated.All Spent Fuel Rack Seismic Restraint Springs Replaced ML20084F3451975-11-28028 November 1975 AO 250-75-9:on 751119,pressure Switch PS-3-2058 Setpoint Exceeded Max Limit.Caused by Setpoint Drift.Pressure Switch Recalibr & Setpoint Returned to Proper Value ML20084F1441975-11-21021 November 1975 AO 251-75-11:on 751112,boron Concentration in Boric Acid Storage Tank C Discovered Above Upper Limit.Caused by Addition of Concentrated Boric Acid Solution to Tank.Primary Grade Water Added to Tanks & Contents Diluted ML20084F4151975-11-0505 November 1975 AO 250-75-8:on 751026,MSIV C Malfunctioned.Cause Not Determined.Msiv Stem Packing & Pneumatic Cylinder Inspected. Investigation of Cause Continuing ML20084F3351975-10-31031 October 1975 AO 251-75-10:on 751021,unplanned Release of 880 G Radioactive Liquid to Underground Area Outside Plant Radiation Controlled Boundary Occurred.Caused by Personnel Error.Floor Drains to Be Labeled ML20084F3971975-10-13013 October 1975 AO 251-75-8:on 750525,diesel Generator Breaker 4A & Bus Stripping 4B Relay Malfunctioned During Engineered Safeguards & Emergency Power Sys Integrated Test. Intermittent Open Circuit Caused by Electrolytic Corrosion ML20084F4371975-10-0303 October 1975 AO 250-75-7:on 750924,high Pressure Comparator in Pressurizer Protection Sys Channel III Malfunctioned.Caused by Two Failed Capacitors in Dc Power Supply.Comparator PC-3-457A Replaced ML20084F5561975-08-0101 August 1975 AO 250-75-6:on 750623,during Rotation of Operating Equipment,Intake Cooling Water Pump 3A Malfunctioned.Rept Incomplete ML20084F5181975-07-24024 July 1975 Supplementary AO 251-75-9:on 750613,airlock Equalizing Valve Opened Breaching Containment Integrity.Operating Procedure 0202.1 Reactor Startup-Cold Condition to Hot Shutdown Condition, Will Be Revised ML20084F5991975-06-0606 June 1975 AO 250-75-4:on 750522,intake Cooling Water Pump Breaker 3A Malfunctioned.Cause Not Yet Determined.Pump Breaker Racked Out & Inspected for Damage ML20084F6081975-05-27027 May 1975 AO 250-75-3:on 750517,battery Charger Transformer 3A Failed. Caused by Unsatisfactory Original Insulation.Transformer Replaced.Vendor Examined Failed Transformer & Repaired Charger.Charger 3A Placed Back in Svc ML20084F6501975-05-0606 May 1975 AO 251-75-7:on 750426,during Refueling Operations,Fuel Assembly P41 Damaged.Caused by Procedural Deficiencies. Procedures Revised to Specify Fuel Assembly Must Be Lifted to full-up Position Before SFP Bridge Moved Away ML20084F6441975-05-0101 May 1975 AO 251-75-6:on 750422,during Valve & Steam Generator Maint, Containment Integrity Breached.Caused by Procedural Deficiencies.Administrative & Maint Procedures Will Be Revised ML20084F7291975-05-0101 May 1975 Supplemental AO 251-75-4:on 750312,broken Lateral Restraints for Spent Fuel Racks Discovered.Caused by Stress Corrosion. Original Springs Replaced.On 750321,broken Restraint Found on Unit 3.Insp Underway ML20084F7671975-04-23023 April 1975 AO 250-75-2:on 750414,steam Generator Protection Sys Channel II Low Level Comparator Failed.Caused by Failed Capacitor in 15-volt Dc Instrument Power Supply.Comparator Replaced ML20084G0771975-04-22022 April 1975 AO 251-75-1:on 750413,spent Fuel Pit Cooling Pump Bearing Failed.Caused by Procedural Deficiencies.Areas Affected Cleaned,Pump Repaired & Off-Normal-Condition Procedure 3508 Revised ML20084F6691975-04-22022 April 1975 AO 251-75-5:on 750413,unplanned Release of Liquid Radioactive Matl Occurred.Rept Incomplete ML20084F7451975-03-21021 March 1975 AO 251-75-4:on 750312,lateral Restraints for Spent Fuel Racks Discovered Broken.Cause Under Investigation.Springs Will Be Replaced ML20084F7881975-03-14014 March 1975 AO 251-75-3:on 750304,steam Generator Protection Sys Channel II Low Steam Line Pressure Comparator Failed.Caused by Failed Capacitor in 15-volt Dc Instrument Power Supply. Comparator Replaced ML20084F8041975-03-12012 March 1975 AO 250-75-1:on 750302,reactor Operated Outside Indicated Axial Flux Difference Target Band.Cause Attributed to Operators Not Understanding Tech Specs.New Procedures Will Be Discussed in Detail W/Operating Personnel ML20084G0811975-02-14014 February 1975 AO 251-75-1A:on 750103,zero Shift in Pressurizer Lead/Lag Controller PM-456A Occurred.Caused by Failure of Capacitor in Amplifier of Lead/Lag Controller.Controller Replaced W/ Calibr Spare Controller ML20084F8241975-01-30030 January 1975 AO 251-75-2:on 750120,low Boron Concentration Found in Boron Injection & Boric Acid Storage Tanks.Caused by Demineralized Water Being Used to Flush Temporary Hoses.Blocked Recirculation Line Will Be Cleared or Renewed ML20084C4961975-01-28028 January 1975 Supplemental AO 251-74-7:on 741108,leak Found in 3/4-inch Vent Line Assembly Upstream of Safety Injection Sys 10-inch Check Valve.Possibly Caused by Presence of Defect at Weld Root or Poor fit-up Between Pipe & Coupling ML20084G0861975-01-13013 January 1975 AO 251-75-1:on 750103,pressurizer Pressure Protection Channel II Lead/Lag Controller Failed.Caused by Zero Shift in Pressurizer Low Pressure Lead/Lag Controller.Controller Adjusted to Correct Zero Shift ML20084C1251975-01-0606 January 1975 AO 251-74-9:on 741227,newly Installed Digital Data Processing Sys Revealed Feedwater Temp Reading of Sys About 10 F Lower than Feedwater Temp Shown on Feedwater Temp Recorder.Caused by Incorrect Calibr Procedure ML20084C1171975-01-0606 January 1975 AO 250-74-12:on 741227,newly Installed Digital Data Processing Sys Revealed Feedwater Temp Reading Used by Sys About 10 F Lower than Feedwater Temp Shown on Feedwater Temp Recorder.Caused by Incorrect Calibr Procedure ML20084C1341974-12-12012 December 1974 AO 251-74-11:on 741203,while RCS Pressure Being Increased, Pressure Control Valve Indicated Closed & Pressure Reached Setpoint Above Tech Spec Limits Before Valve Opened.Caused by Automatic Closure of RHR Sys Valves ML20084C1701974-12-0202 December 1974 AO 251-74-8:on 741123,indication of Low Boric Acid Flow in Flow Path from Boric Acid Tanks to RCS Observed.Caused by Accumulation or Buildup of Boric Crystals in Line.Boric Acid Flow Path Isolated from RCS ML20084C5281974-11-0808 November 1974 AO 251-74-7:on 741029,routine Visual Insp of RCS Revealed Steam Leaking from 3/4-inch Vent Line Assembly Upstream of Safety Injection Sys.Cause Unknown.Vent Assembly Removed & Sent for Metallurgical Analysis.Supplemental AO Will Follow ML20084C5351974-10-23023 October 1974 AO 251-74-6:on 741013,analysis of Boron Injection Tank Boron Content Revealed Concentration Below Tech Spec Limit.Caused by Insufficient Recirculation Coupled W/Minor Inleakage. Boron Injection Tank Recirculated ML20084C5501974-09-23023 September 1974 AO 251-74-4:on 740913,routine Boron Analysis of Boric Acid Storage Tanks Revealed Tank C Boron Concentration Below Tech Spec Limit.Caused by Partially Open Primary Water Flush Valve.Valve Alignment Procedure Will Be Revised ML20084C5551974-09-16016 September 1974 AO 250-74-10:on 740906,one Steam Generator C lo-lo Water Level Comparator Would Not Trip at Required Value.Caused by Failure of 15 Volt Dc Power Supply Filter Capacitor. Comparator Replaced W/Calibr Spare Unit ML20084C5951974-08-22022 August 1974 AO 251-74-3:on 740812,counting of Daily Composite Steam Generator Secondary Sys Water Sample Revealed Significant Increase in Radiation Level.Caused by Plugged Sample Line to 4-R-19 Detector.Sampling Sys Being Evaluated ML20084C5781974-08-22022 August 1974 AO 251-74-2:on 740812,counting of Daily Composite Steam Generator Secondary Sys Water Sample Revealed Significant Increase in Radiation Level.Cause Unknown.Steam Generator a Will Be Examined by Reactor Vendor to Identify Source ML20084C6051974-08-0101 August 1974 AO 250-74-8:on 740219,personnel Overexposure Occurred While Attempting Maint on E Detector of Flux Mapping Equipment. Caused by Failure to Comply W/Radiation Work Permit ML20084C6231974-07-0505 July 1974 AO 251-74-8:on 740627,0701 & 02,boron Injection Tank Boron Concentration Found Below Tech Specs Limit.Caused by Insufficient Recirculation Coupled W/Minor Leakage. Investigation Continuing ML20084C7191974-05-17017 May 1974 AO 250-74-7:on 740508,while Attempting to Start Three Auxiliary Feedwater Pumps,Pumps a & B Failed to Start & C Started But Tripped When Attempt Made to Feed Steam Generators.Caused by Packing Too Tight.Packing Loosened ML20084C7441974-05-10010 May 1974 AO 250-74-6:on 740503,after Safety Injection Sys Pump 3A Started to Add Water to Safety Injection Accumulators,Pump Indicated Abnormally Low Running Current & Discharge Pressure.Cause Unknown.No Abnormalities Found ML20084C8811974-04-19019 April 1974 AO 250-74-5:on 740411,routine Boron Analysis of Boron Injection Tank Contents Indicated Boron Concentration Below Lower Tech Spec Limit.Cause Unknown.Contents Recirculated Through Boric Acid Storage Tank ML20084M2961974-03-15015 March 1974 Suppl to AO 3-73-1:on 730106,reactor Coolant Leaked Into Reactor Containment from Differential Pressure Cell.Caused by Flange Bolt Failure.Bolts Replaced ML20084C9941974-02-27027 February 1974 AO 250-74-4:on 740218,recent Monthly in-core Detector Flux Map Found to Not Meet Requirements of Change 11 to Tech Spec for Power Level Greater than 75%.Caused by Failure to Comply W/Recent Changes in Tech Specs ML20084M2511974-02-22022 February 1974 Suppl to AO 3-73-3:on 730319,emergency Diesel Generator a Failed to Automatically Start.Caused by Malfunctioned Starting Air Solenoid Valve.Valve Replaced & Defective Valve Subjected to Tests.Valve Spring Assemblies Replaced ML20084D0051974-02-15015 February 1974 AO 250-74-3:on 740206,engineered Safeguards Sys Energized & Reactor Tripped from Safety Injection Sys Signal.Caused by Improper Engaging of Two Air Driven Starting Motor Pinion Gears W/Engine Flywheel Ring Gear ML20084D0161974-02-15015 February 1974 AO 250-74-2:on 740205,safety Injection Pump 3A Failed to Start.Caused by Closing Spring Mechanical Indicator of Safety Injection Pump 3A Motor Circuit Breaker Being in Intermediate Position & Not Closed.Spring Mechanism Tested ML20084M3711973-11-26026 November 1973 Suppl to AO 3-72-8:on 721216,small Fire Discovered in Battery Charger Cubicle 3.Caused by Winding Short in Transformer.New Transformers Installed ML20084M1361973-11-24024 November 1973 Suppl to AO 4-73-3:on 730509,pump 4A Discovered Leaking.Insp Determined Pump in Satisfactory Condition.Components of Mechanical Seal Assembly Replaced ML20084D2371973-10-26026 October 1973 AO 3-73-10:on 731018,review of Chemistry Analysis Log Sheets for Boric Acid Storage Tanks & Boron Injection Tanks Indicated Boric Acid Storage Tank a Concentration in Excess of Tech Spec Limits.Caused by Personnel Oversight ML20084D2431973-10-16016 October 1973 AO 4-73-12:on 731007,approx 50 to 75 Gallons of Reactor Coolant Released to Charging Pump Room in Auxiliary Bldg Via Failed Bellows in Relief Valve 4-209.Caused by Increased Pressure on Bellows & Opening in Valve Bonnet ML20084D2491973-09-20020 September 1973 AO 4-73-11:on 730920,sample from Inlet Piping to Boron Injection Tank Analyzed & Found to Contain Less than Specified Min in Tech Specs.Caused by Valve Leaking in Suction of Boric Acid Transfer Pumps 1975-08-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
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Text
P O box 3100 M1AMI. FLOROA 33101 e
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, FLORIDA POWER & LIGHT COY.PANY July 13, 1973
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Mr. John F. O' Leary Directorate of Reactor Licensing 3 \
U. S. Atomic Energy Commission Y b(.(u Pi o
Washington, D. C.
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. r'.G L;v TURKEY POINT UNIT NO. 3 at g,s DOCKET No. 50 - 250 ABNORMAL OCCURRENCE NO. 3-73-5 g,hy.. g 7'
/
- % L14 FAILURE TO AUTO TRANSFER AUXILIARY POWER TO STARTUP TRANSFORMER
Dear Mr. O' Leary:
I. INTRODUCTION This report is submitted in accorduce with Technical Specification 6.6.2a for Turkey Point Unit No. 3, Operating License No. DPR-31. This Abnormal Occurrence Report No. 3-73-5, describes an abnormal occurrence which was identified on July 4, 1973. The Directorate of Regulatory Operations, Region II, was notified on July 4, 1973.
II. DESCRIPTION OF OCCURRENCE On July 4, 19,73, Turkey Point Unit No. 3, was operating at a power level of 600 mwe while calibration of steam line pressure transmitters was being performed in accordance with approved test and calibration procedures. About 4:12 a.m., Unit No. 3 reactor and turbine-generator tripped as a result of Safety Injection System actuation caused by coincident trips of two out of three channels No. 3C steam line high differential pressure. One steam line differential pressure channel was in the trip position for calibration of the associated steam pressure transmitter.
One of the other steam line differential pressure channels in service received a transient or spurious signal to trip and this provided the necessary coincident two out of three channels to trip. Following the trip,all of J
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t Mr. John F. O ry July 13, 1973 the Engineered Safeguards Systems were verified to be operating normally. Automatic transfer to auxiliary power supply from No. 3 auxiliary transformer to No. 3 startup transformer did not occur. Nuclear Control Operators performed the immediate operator actions specified in approved emergency operating procedures for a controlled shutdown of the unit and with a complete loss of off-site power thus placing the reactor in a safe condition.
Observation of significant nuclear steam supply system parameters indicated that symptoms of an incident which would have caused a Safety Injection System actuation were not present. Accordingly, subsequent operator action was directed toward shutdown of all Engineered Safeguard System equipment not required for a controlled shutdown of the reactor.
About 4:25 a.m., Nos. 3A and 3B startup transformer breakers were manually closed to supply Unit Nos. 3A and 3B, 4160 volt buses. Unit No. 3 was then placed in hot shutdown condition pending review, analysis and evaluation of the cause of the reactor trip and failure to automatically transfer auxiliary power supply to the startup transformer.
III. ANALYSIS OF THE OCCURRENCE An investigation by plant personnel to determine the cause of the failure to automatically transfer auxiliary power supply to the startup transformer, revealed that the circuitry to the relay that closes Nos. 3A and 3B startup transformer breaker had not been completed.
The original circuit design was changed during construction of Unit No. 3 to provide for automatic transfer of auxiliary power supply to the startup transformer when the Safety Injection System was actuated.
IV. CORRECTIVE ACTION TO PREVENT RECURRENCE The immediate corrective action was to install the connecting wire to complete the automatic circuitry that closes Nos. 3A and 3B startup transformer breakers. The completed circuit was then tested to demonstrate continuity.
The circuit revision that was involved in this occurrence was mado prior to licensing and implementation of the Quality Assurance Program for Operating Nuclear Power Plants. The presently implemented procedures would pre-vent a repetition of this type of occurrence. This program provides a means for documenting proposed plant changes and modifications from initial proposal to completed installation including the utilization of approved pro-cedures, in-progress inspections and a final functional verification by test. This program is implemented by Administrative Procedure 0190.15.
1
c Mr. John F. enry (' July 13, 1973 ,-
. . x/ ,1 V. ANALYSIS AMD EVALUATION OF SAFETY IMPLICATIONS OF THE OCCURRENCE Unit Nos. 3 and 4 are designed to accept a reactor trip while operating at power levels up to 100% of full power without adversely affecting the safe operation of the reactor. Further, Unit Nos. 3 and 4 are designed to accept a complete loss of off-site power supply and a turbine trip at full power operation without adversely affecting the safe operation of the reactor. These analyses are presented in FSAR, Section 14.1.10.
The reactor was protected by prompt insertion of the control rods to reduce reactor power. Trip of reactor coolant pumps did not adversely affect the safe operation of reactor due to the continued circulation of reactor coolant as a result of the inertia of the coolant and the reactor coolant pumps. Natural circulation maintianed an adequate coolant flow through the core. Prompt closure of the turbine main steam stop valves and control valves, prevented an undesireable cooldown of the reactor coolant. Automatic start and continued operation of the steam driven auxiliary feedwater pumps provided assurance that the steam generators were available as a heat sink if required.
Comparison of the actual conditions during the incident described above, with the analysis presented in the Turkey Point Unit Nos. 3 and 4 Final Safety Analysis Report shows that the condition assumed for Loss of External Load Incident and the Complete Loss of Off-Site Power Incident are significantly more conservative than the conditions described above. Based on this comparison, the failure of the automatic transfer of auxiliary power supply to the startup transformer did not adversely affect the safe operation of Unit No. 3.
VI. CONCLUSIONS
- a. The failure of the automatic transfer of auxiliary power supply to the startup transformer was the result of a connecting wire in the automatic circuitry between the Safety Injection System actuation relay and the relay that closes the Nos. 3A and 3B startup transformer breakers not being instailed.
/
-.-r.L
', Mr. J::hn F. cry ( July 13, 1973 l,
- b. The circuit change involved in this occurrence was made prior to licensing the unit. Strict adherence
, . to the program established for processing plant changes and modifications implemented by Administrative Procedure 0190.15 will prevent recurrence of this and similar incidents.
- c. The Safety Injection System nozzles and piping acre not subjectec to thermal stresses.since no flow occurred in this system.
- d. Operation of the Engineered Saf7 guards System equipment to provide emergency power to Gait Do. 3 ensured that the unit was shutdown in a controlled manner and the reactor was placed in a safe condition during the x loss of off-site powe,r.
- e. This failure to automatically transfer auxiliary power supply to No. 3 startup transformer did not adversely affect the safe operation of Unit No. 3.
- f. This abnormal occurrence did not present any danger 1
to the public health or' safety.
4 Very truly yours, W'
A. D. Schmidt Director of Power Resources ADS /VTC/ GEL /UNP/paz cc: Norman C. Moseley, Director Region II, Directorate of Regulator Operation U. S. Atomic Energy Commission Suite 818, 230 Peachtree Street, N.W.
Atlanta, Georgia Mr. G. A. Olson Edison Electric Institute I 90 Park Avenue
.New York New York 10016 Dr., James Coughlin J. W. Williams, Jr.
- J . 4t . Bensen J. B. Olmstead W. H., Rogers, Jr. S. G. Brain G. E. Liebler Plant Supervisors J. K. Hays Plant Nuclear Committee
,' C. E. Branning Documentary Files D. W. Jones