ML20084J143

From kanterella
Jump to navigation Jump to search
Ro:On 721201,RCIC Sys Outboard Containment Isolation Valve MO2-1301-17 Failed to Operate.Caused by Faulty Torque Switch SMP-00.Switch Replaced
ML20084J143
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 12/06/1972
From: Stephenson B
COMMONWEALTH EDISON CO.
To: Giambusso A
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084J139 List:
References
BBS-72-15, NUDOCS 8305120191
Download: ML20084J143 (2)


Text

e

.k'

,- /'\

Comm zith Edison . -

(_,! gg ,.

Outd-Cities Nuc!sar Pow:r Station f) t L , ,

Poet Office Box 216 Aj).,'

f Gj'/ Cordova,ilknois 61242 Telephone 309/654-2241

//. ( ,,r7 l' yth % /p ',j).

'O el cn u.rn Cfs?[72

~

BBS-72-15 2, ,QTi D /

December 6, 1972 50-265 Mr. A. Giambusso Deputy Director for Reactor Projects Directorate of Licensing U. S. Atomic Energy Commission Washington, D. C . 20545 Ref: Quad-Cities Nuclear Power Station, Unit 2 License DPR-30, Appendix A Sections 1. 0. A . 2 . , 3.7.D.l., and 6.6.B.3.

Dear Mr. Giambusso:

The purpose of this letter is to inform you of the details regarding the failure of the outboard containment isolation valve, M02-1301-17, of the Reactor Core Isolation Cooling System (RCIC) to operate. This incident occurred on Unit 2 at Quad-Cities on December 1, 1972. _

Description of Incident At 10:00 pm on December 1, 1972, the Unit 2 reactor was in the Run mode at 90% power. While performing the routine monthly valve operability surveillance, valve 2-1301-17 failed to close. ~

Several attempts to close the valve from the control 3 room were unsuccessful. Therefore, the inboard

'I containment isolation valve 2-1301-16 was closed to

- /[ comply with Technical Specification 3.7.D.2 and RCIC was declared inoperable. Immediately the HPCI system was demonstrated to be operable in l' d '

accordance with Technical Specification 4.5.E.2.6.

dlN .

Investigation and Corrective Action An investigation performed by Station Electrical Maintenanc r&Vea{ed that the torque switch, (type RED 'SMB-00") series , Limitorque Valve Control by Philade phia, Gear) for the valve motor was faulyt .

fl) M ,w ,I ,

8305120191 730105 COPY SENT REGION

! PDR ADOCK 05000254

!- O PDR

~ ~

6811 1

r , ,  ;

. Q + 0*

  • o O

A. Giambusso December 6, 1972 The return spring failed to reset the switch, thus preventing the valve motor to operate.

The torque switch was replaced with a new WHITE "SMB-00" (Philadelphia Gear ) series and adjusted.

The valve was openned and closed three times after the repair prior to declaring the RCIC system operable.

Conclusion The failure of this particular torque switch is similar to those occurrences reported in letters dated July 10, August 3, and September 3, 1972.

The new WHITE SMB-00 series which replaces the RED SMB-00 series torque switch has a return spring with a higher modulus of elasticity.

Furthermore, the Edison station Electrical Eng-ineering Department is conducting an investigation of failures of this type.

The safety aspects of this particular failure have been analyzed. With the valve failed in the open position, the RCIC system could have performed its intended function. Also, the system was still capable of isolating' on an RCIC line break signal since the inboard isolation valve was operable and outboard isolation valve could be -

manually closed if necessary.

~1r-

,uJMAou '~

B. B. tep enson BBS/lk J

^ _

! -- . i .J b