ML20083J520

From kanterella
Jump to navigation Jump to search
Responds to NRC Re Violations Noted in IE Insp Repts 50-317/83-26 & 50-318/83-26.Corrective Actions: Surveillance Test Procedure STP 0-7-1 Re Svc Water Inlet Valve Revised Per Operating Instruction 15
ML20083J520
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 12/06/1983
From: Lundvall A
BALTIMORE GAS & ELECTRIC CO.
To: Martin T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20083J510 List:
References
NUDOCS 8401100176
Download: ML20083J520 (2)


Text

_. _ - - _.

t..

BALTIM ORE GAS AND ELECTRIC CHARLES CENTER.P. O. BOX 1475 BALTIMORE, MARYLAND 21203 AN' Hun E. LUNDVALL. Jn.

VICE PRLS8 DENT SUPPLY U. S. Nuclear Regulatory Commission Docket Nos.

50-317 Region I 50-318 631 Park Avenue License Nos.

DPR-53 King of Prussia, PA 19406 DPR-69 ATTENTION: Mr. Thomas T. Martin, Director Division of Engineering & Technical Programs Gentlemen:

This refers to Inspection Report 50-317/83-26, 50-318/83-26; which transmitted an item of apparent noncompliance with NRC requirements. Enclosure (1) to this letter is a written statement in reply to the item noted in your letter of November 9,1983.

Should you have further question regarding this reply, we will be pleased to discuss them with you.

Very truly you

/

, /

j c

b f.

, w)d&

x

/

AEL/ LOW /gla Enclosure cc:

3. A. Biddison, Esquire G. F. Trcwbridge, Esquire D. H. Jaffe, NRC R. E. Architzel, NRC j

l 9401100176 831223 PDR ADOCK 05000317 G

PDR l

I

,e.

s ENCLOSURE (1)

REPLY TO APPENDIX A OF NRC INSPECTION REPORT 50-317/83-26; 50-318/83-26 We have completed our review of the subject noncompliance item involving failure to properly reposition the Spent Fuel Pool Cooler (SFPC) service water valves following performance of Surveillance Test Procedure (STP) 0-7-1.

This incident involved two areas where failure to fully implement a portion of an existing procedure and procedural inadequacies resulted in the identified item of noncompliance. As a result of our review, we have taken corrective actions specified below to ensure that incidents similar to those described are not repeated in the future.

1.

STP 0-7-1 has been revised to meet the requirements of Operating Instruction-15. This revision has resulted in changes ensuring that:

(a) the service water inlet valve to #11 SFPC is returned to its pretest position when the Containment Spray Actuation System (CSAS) testing is completed, and (b) the service water outlet valve from #11 SFPC is placed in the open position when CSAS testing is completed. To ensure proper implementation of the STP, the operator performing the test is now required to initial and date each step of the procedure as it is performed. Full compliance was achieved on November 1,1983.

2.

All operational STPs are being reviewed by Senior Licensed personnel to ensure that similar. incidents do not occur. The purpose of this review will be to detect any inconsistencies and initiate revisions similar to those performed on STP 0-7-1.

We anticipate that this review will be completed by June 30,1984.

3.

Regarding the failure to implement a portion of approved procedures, following the incident, the General Supervisor - Operations counseled the operator involved in the incident relaying management concerns as to the necessity for proper procedure implementation. To emphasize those concerns, the individual involved was required to prepare a Personnel incident Report describing the incident and suggesting corrective actions.

This report has been distributed as " required reading" to all Operations personnel.

1

,