Applicant Exhibit A-13,consisting of to NRC Re Confirmation of Action LtrML20083C922 |
Person / Time |
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Site: |
Vogtle |
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Issue date: |
04/17/1995 |
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From: |
Hairston W GEORGIA POWER CO. |
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To: |
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References |
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CAL, OLA-3-A-013, OLA-3-A-13, NUDOCS 9505230086 |
Download: ML20083C922 (5) |
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Category:EXHIBITS (DOCKETING AND SERVICES BRANCH INFORMATION
MONTHYEARML20100B7601995-10-11011 October 1995 Intervenor Exhibit I-MOSBA-39A,consisting of Case Number 2-90-020R Re List of Exhibits ML20100B7631995-10-11011 October 1995 Intervenor Exhibit I-MOSBA-97,consisting of Case Number 90-ERA58 Transcript Re Deposition of K Mccoy ML20100B7641995-10-11011 October 1995 Intervenor Exhibit I-MOSBA-111,consisting of Procedure Number 00057-C Re 900711 Event Rept Entitled, DG 2A Start Failure ML20100B7651995-10-11011 October 1995 Intervenor Exhibit I-MOSBA-272,consisting of File Number 90-ERA-30 Transcript Re Deposition of LB Glenn ML20099L3881995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-23A,consisting of Transcipt Re Intervenor Exhibit 23A Tape 29 Side B, ML20099L3711995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-8A,consisting of Transcript Re Joint Exhibit 8A Tape 8 Side B, ML20099L3831995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-21A,consisting of Transcript Re Intervenor Exhibit 21 Tape 32-1,dtd 900404,TR 41-44 ML20099L4041995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-153,consisting of Cover Sheet & Page from CRC Handbook of Chemistry & Physics ML20100B6781995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-222,consisting of Cooper Outage Logbook ML20099L4311995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-216,consisting of 900511 Interoffice Memo Re Enterprise Engine S/N 76021 Loss of Offsite Power on 900320 ML20100B6821995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-225,consisting of Correspondence Re Jul 1990 Starting Air Valve Problem ML20099L4291995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-215,consisting of History Re Alnor Dewpointer Model 7200U Serial 24355 Calibr ML20099L4331995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-217,consisting of Handwritten Statement Re Events of 1A DG Loss of Offsite Power ML20099L4081995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-170A,consisting of Transcript Re Intervenor Exhibit II-170A Tape 207,dtd 900717 ML20099L4001995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-94B,consisting of Transcript Re Intervenor Exhibit 94B Tape 32,dtd 900404,TR 46-49 ML20099L3971995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-94A,consisting of Transcript Re Intervenor Exhibit 94A Tape 32,dtd 900404,TR 46-49 ML20100B6801995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-223,consisting of RA Johnston Personal Outage Notes ML20100B6831995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-227,consisting of Correspondence Re Pneumatic Control Component Testing ML20099L3801995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-9A,consisting of Transcript Re Intervenor Exhibit 9 Tape 10,dtd 900323,TR 22-23 ML20099L3891995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-51A,consisting of Transcript Re Joint Exhibit 51 Tape 7,dtd 900322,TR 20-21 ML20099L3691995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-4A,consisting of Transcript Re Intervenor Exhibit 4 Tape 99,dtd 900508,TR 43-53 ML20100B7001995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-237A,consisting of Tape 218 Re 900725 Conversation Between Mosbaugh & Horton ML20099L4031995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-118A,consisting of Transcript Re Intervenor Exhibit 118A Tape 24A,dtd 900330 ML20100B6901995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-232A,consisting of Tape 3,side a of 900223 Conversation Between Bockhold & Mosbaugh ML20099L3041995-10-0606 October 1995 Applicant Exhibit A-181A,consisting of 900404 Tape 34, Beginning of Side B ML20099L4131995-10-0606 October 1995 Intervenor Exhibit I-MOSBA-196,consisting of Nuclear Plant Maint Work Order Re DG 1A That Tripped Twice Following Two Actual Loss of Offsite Start Conditions ML20099L3821995-09-28028 September 1995 Intervenor Exhibit I-MOSBA-19A,consisting of Transcript Re Intervenor Exhibit 19 Tape 25,dtd 900330,TR 2 ML20099L3861995-09-28028 September 1995 Intervenor Exhibit I-MOSBA-22B-1,consisting of Transcript Re Intervenor Exhibit 22B Tape 89 Side A,50%,dtd 900502 ML20099L2111995-09-28028 September 1995 Applicant Exhibit A-120A,consisting of Transcript of Audiotape 72 ML20099L2121995-09-28028 September 1995 Applicant Exhibit A-133A,consisting of Transcript of Audiotape 69 ML20099L3581995-09-27027 September 1995 Applicant Exhibit A-202,consisting of Re Licensee Suppl Reply to NOV & Proposed Imposition of Civil Penalties ML20099L3601995-09-27027 September 1995 Applicant Exhibit A-203,consisting of Licensee on NRC Demand for Info Re G Bockhold ML20100B7541995-09-26026 September 1995 Intervenor Exhibit I-MOSBA-270,consisting of M&TE Traveler Re Alnor Derpointer W/Last Calibr Date of 890907 & Next Calibr Date of 900307,extended to 900407 ML20099L4111995-09-26026 September 1995 Intervenor Exhibit I-MOSBA-183A,consisting of Transcript Re Intervenor Exhibit II-183A (Joint Version) Tape 99 Side a, ML20099L4021995-09-22022 September 1995 Intervenor Exhibit I-MOSBA-95,consisting of 900823 Interoffice Correspondence Re NRC Areas of Concern, Log:SRBS-00044 Security Code:Nc ML20100B6991995-09-22022 September 1995 Intervenor Exhibit I-MOSBA-237,consisting of Tape 218,side B at 70% Re 900725 Conversation Between M Horton & Mosbaugh ML20099L1411995-09-22022 September 1995 Board Exhibit Bd-10,consisting of Drawing W/Related Info ML20099L4051995-09-21021 September 1995 Intervenor Exhibit I-MOSBA-169,consisting of Demonstrative Aid 4 (Rev 950713) Re Dew Point Data,Diesel Air Sys ML20100B6971995-09-21021 September 1995 Intervenor Exhibit I-MOSBA-235 Sup,Consisting of Transcript of Pages 83 & 84 Re OI Investigation ML20100B7501995-09-21021 September 1995 Intervenor Exhibit I-MOSBA-266,consisting of Final Rept, Enhancement on On-Site Emergency DG Reliability ML20100B6921995-09-21021 September 1995 Intervenor Exhibit I-MOSBA-233 Sup,Consisting of Transcript Re Page 689 ML20099L3541995-09-21021 September 1995 Applicant Exhibit A-199,consisting of Affidavit of Ja Bailey Re Vogtle Project ML20100B7431995-09-19019 September 1995 Intervenor Exhibit I-MOSBA-262,consisting of Amount of Water in Humid Air at Any Pressure ML20100B7411995-09-19019 September 1995 Intervenor Exhibit I-MOSBA-260,consisting of to NRC Document Control Desk Re Plant Special Rept Invalid DG Failure ML20100B7421995-09-19019 September 1995 Intervenor Exhibit I-MOSBA-261,consisting of Estimate of DG Daily Air Leakage ML20099L3461995-09-19019 September 1995 Applicant Exhibit A-195,consisting of Professional Resume Re Ht Hill ML20099L3481995-09-19019 September 1995 Applicant Exhibit A-196,consisting of Paper Re Vogtle Experience W/Calcon Sensors in DG Trip Circuits ML20099L3511995-09-19019 September 1995 Applicant Exhibit A-198,consisting of Rept Re Plant DGs Airstart Cap Evaluation,Log 95-MT 039 ML20100B7471995-09-19019 September 1995 Intervenor Exhibit I-MOSBA-264,consisting of Water Formation in Control Air Supply Typical Conditions (Early Apr 1990) ML20100B7461995-09-19019 September 1995 Intervenor Exhibit I-MOSBA-263,consisting of Amount of Water in Humid Air at 240 PSIG (17.3 Atm) 1995-09-28
[Table view] Category:LEGAL TRANSCRIPTS & ORDERS & PLEADINGS
MONTHYEARML20196J3291999-06-28028 June 1999 Comment Supporting Proposed Rule 10CFR50 Re Industry Codes & Standards ML20206M7291999-04-30030 April 1999 Comment Supporting Draft RG DG-1083, Content of UFSAR IAW 10CFR50.71(e). Licensee of Listed Plants in Total Agreement with Comments Provided to NRC by NEI HL-5717, Comment Supporting Proposed Rule 10CFR50,52 & 72 Re Changes, Tests & Experiments.Util in Total Agreement with NEI Comments to Be Provided to NRC1998-12-18018 December 1998 Comment Supporting Proposed Rule 10CFR50,52 & 72 Re Changes, Tests & Experiments.Util in Total Agreement with NEI Comments to Be Provided to NRC HL-5715, Comments on Proposed Rule 10CFR50 Re Monitoring Effectiveness of Maint at Nuclear Power Plants.Util Is in Total Agreement with NEI Comments1998-12-14014 December 1998 Comments on Proposed Rule 10CFR50 Re Monitoring Effectiveness of Maint at Nuclear Power Plants.Util Is in Total Agreement with NEI Comments HL-5702, Comment Supporting NEI Comments Totally on Proposed Draft RG DG-4005, Preparation of Supplemental Environmental Repts for Applications to Renew Nuclear Power Plant Ols1998-10-23023 October 1998 Comment Supporting NEI Comments Totally on Proposed Draft RG DG-4005, Preparation of Supplemental Environmental Repts for Applications to Renew Nuclear Power Plant Ols HL-5695, Comment Supporting Nuclear Energy Institute (NEI) Comments on 10CFR50.55(a) Pr, Streamlined Hearing Process for NRC Approval of License Transfers1998-10-13013 October 1998 Comment Supporting Nuclear Energy Institute (NEI) Comments on 10CFR50.55(a) Pr, Streamlined Hearing Process for NRC Approval of License Transfers HL-5690, Comment on Integrated Review of Assessment Process for Commercial Nuclear Plants. Util in Total Agreement with NEI Comments Provided to NRC1998-10-0505 October 1998 Comment on Integrated Review of Assessment Process for Commercial Nuclear Plants. Util in Total Agreement with NEI Comments Provided to NRC HL-5983, Comment on Proposed Rule 10CFR50 Re Reporting Requirements for Nuclear Power Reactors. Snoc in Total Agreement with NEI Comments,To Be Provided to Nrc.Requests That NRC Provide Guidance to Application of NUREG-1022,rev 1 as Listed1998-09-21021 September 1998 Comment on Proposed Rule 10CFR50 Re Reporting Requirements for Nuclear Power Reactors. Snoc in Total Agreement with NEI Comments,To Be Provided to Nrc.Requests That NRC Provide Guidance to Application of NUREG-1022,rev 1 as Listed ML20153B2391998-09-15015 September 1998 Comment on Draft NUREG-1633, Assessment of Use of Ki as Protective Action During Severe Reactor Accidents. Endorses NEI Comments HL-5682, Comment Opposing Draft NUREG-1633, Assessment of Use of Potassium Iodide (Ki) as Protective Action During Severe Reactor Accidents, & Endorsing Comments Submitted by Nuclear Energy Institute1998-09-15015 September 1998 Comment Opposing Draft NUREG-1633, Assessment of Use of Potassium Iodide (Ki) as Protective Action During Severe Reactor Accidents, & Endorsing Comments Submitted by Nuclear Energy Institute HL-5602, Comment Opposing Proposed Rule 10CFR50 Re Industry Codes & Stds1998-04-0303 April 1998 Comment Opposing Proposed Rule 10CFR50 Re Industry Codes & Stds HL-5586, Comment on Proposed Generic Ltr, Year 2000 Readiness of Computer Sys at Npps1998-03-0404 March 1998 Comment on Proposed Generic Ltr, Year 2000 Readiness of Computer Sys at Npps HL-5582, Comment on Draft Reg Guide DG-5008, Reporting of Safeguards Events1998-02-27027 February 1998 Comment on Draft Reg Guide DG-5008, Reporting of Safeguards Events HL-5564, Comment on Draft NUREG 1555, Updated Environ Standard Review Plan1998-01-30030 January 1998 Comment on Draft NUREG 1555, Updated Environ Standard Review Plan HL-5554, Comment Supporting NEI Comments on PRM 50-63A by P Crane Recommending Emergency Planning Standard for Protective Actions Be Changed to Require Explicit Consideration of Prophylactic Use of Potassium Iodide for General Public1998-01-15015 January 1998 Comment Supporting NEI Comments on PRM 50-63A by P Crane Recommending Emergency Planning Standard for Protective Actions Be Changed to Require Explicit Consideration of Prophylactic Use of Potassium Iodide for General Public HL-5546, Comment Supporting Proposed Rule & Direct Final Rule on 10CFR50.68 & 10CFR70.24, Criticality Accident Requirements1997-12-31031 December 1997 Comment Supporting Proposed Rule & Direct Final Rule on 10CFR50.68 & 10CFR70.24, Criticality Accident Requirements HL-5529, Comment Opposing Rule 10CFR50 Re Codes & Standards,Ieee National Consensus Standard1997-12-0101 December 1997 Comment Opposing Rule 10CFR50 Re Codes & Standards,Ieee National Consensus Standard ML20199J0031997-11-24024 November 1997 Comment Supporting Proposed Rule Re Financial Requirements for Decommissioning Nuclear Power Reactors & Draft RG 1060 HL-5424, Comment on NUREG-1606, Proposed Regulatory Guidance Re Implementation of 10CFR50.59 (Changes,Tests or Experiments). Encourages NRC Not to Abandon 30 Yrs of Effective Implementation of 10CFR.50.59 for New Positions1997-07-0707 July 1997 Comment on NUREG-1606, Proposed Regulatory Guidance Re Implementation of 10CFR50.59 (Changes,Tests or Experiments). Encourages NRC Not to Abandon 30 Yrs of Effective Implementation of 10CFR.50.59 for New Positions ML20148N0741997-06-19019 June 1997 Comment on Proposed Suppl to Bulletin 96-001 Re Control Rod Insertion Problems.Util in Complete Agreement That Incomplete Rcca Insertion Not Acceptable HL-5407, Comment Opposing NRC Proposed Strategies to Address Licensees Need to Establish & Maintain safety-conscious Work Environ1997-05-27027 May 1997 Comment Opposing NRC Proposed Strategies to Address Licensees Need to Establish & Maintain safety-conscious Work Environ ML20137C2581997-03-18018 March 1997 Summary of Director'S Decision Under 10CFR2.206 of Mb Hobby & AL Mosbaugh, ML20137C4261997-03-18018 March 1997 Director'S Decision Under 10CFR2.206 Re Petition Re Allegation of Illegal Transfer of OLs to Southern Nuclear Operating Co.Petitions Filed by Mb Hobby & AL Mosbaugh Denied HL-5268, Comment Supporting Draft RG DG-1047, Std Format & Content for Applications to Renew NPP Ols1996-11-27027 November 1996 Comment Supporting Draft RG DG-1047, Std Format & Content for Applications to Renew NPP Ols ML20133H1131996-11-25025 November 1996 Petition for Enforcement,Per 10CFR2.206,to Revoke Northeast Utils Operating Licenses for CT Nuclear Power Stations Due to Chronic,Systemic Mismanagement Resulting in Significant Violations of NRC Safety Regulations ML20129J5481996-10-30030 October 1996 Order.* Extends Time within Which Commission May Take Sua Sponte Review of Memorandum & Order LBP-96-16 to 961129. W/Certificate of Svc.Served on 961030 ML20129K4291996-10-0202 October 1996 Comment Supporting Proposed Rule 10CFR25 & 95, Access to & Protection of Classified Info HL-5247, Comment on Proposed Generic Communication, Primary Water Stress Corrosion Cracking of Control Rod Drive Mechanism & Other Vessel Head Penetrations1996-10-0101 October 1996 Comment on Proposed Generic Communication, Primary Water Stress Corrosion Cracking of Control Rod Drive Mechanism & Other Vessel Head Penetrations ML20128K2791996-09-30030 September 1996 Order.* Time within Which Commission May Take Sua Sponte Review of Memo & Order LBP-96-16 Extended Until 961030. W/Certificate of Svc.Served on 960930 ML20116J8921996-08-0202 August 1996 Withdrawal of AL Mosbaugh.* AL Mosbaugh Voluntarily Withdraws Intervention,Opposition & Contention in Proceedings.W/Certificate of Svc & Svc List ML20116J8551996-08-0202 August 1996 Joint Notice of Termination.* AL Mosbaugh Voluntarily Withdrew Intervention,Opposition & Contentions in Proceeding.W/Certificate of Svc & Svc List ML20116J8431996-08-0202 August 1996 Intervenor Response to Georgia Power Motion for Reconsideration.* Intervenor Supports Motion for Reconsideration.W/Certificate of Svc & Svc List ML20116N5881996-07-31031 July 1996 Comment Re Proposed Rule 10CFR26, Mods to Fitness-For-Duty Program Requirements. Supports NEI Comments ML20116A4931996-07-15015 July 1996 Georgia Power Company Motion for Reconsideration of 960628 Memorandum & Order Or,In Alternative,For Certification.* Gpc Requests That Board Not Require Submittal or Approval of Settlement Between Gpc & Mosbaugh.W/Certificate of Svc ML20115H2671996-07-0808 July 1996 Comment Supporting Final Rule 10CFR51, Environ Review of Renewal of Nuclear Power Plant Operating Licenses HL-5195, Comment Supporting Proposed Rule 10CFR50 Re Financial Assurance Requirements for Decommissioning Nuclear Power Reactors1996-06-24024 June 1996 Comment Supporting Proposed Rule 10CFR50 Re Financial Assurance Requirements for Decommissioning Nuclear Power Reactors ML20114E6491996-06-20020 June 1996 Joint Motion to Defer Issuance of Initial Decision.* Requests That ASLB Defer Issuance of Decision in Proceeding Until 960920,in Order to Allow Gpc & Mosbaugh to Reach Settlement Agreement.W/Certificate of Svc IA-95-211, Transcript of 920507 Interview of Mc Wilkins in Waynesboro, Ga.Pp 1-391996-05-0707 May 1996 Transcript of 920507 Interview of Mc Wilkins in Waynesboro, Ga.Pp 1-39 ML20129H7151996-05-0707 May 1996 Transcript of 920507 Interview of Mc Wilkins in Waynesboro, Ga.Pp 1-39 HL-5103, Comment Supporting NEI Comments on Petition for Rulemaking PRM-50-63 Re Planning Std for Protective Actions for General Public Includes Stockpile or Predistribution of Ki for Prophylactic Use1996-02-0606 February 1996 Comment Supporting NEI Comments on Petition for Rulemaking PRM-50-63 Re Planning Std for Protective Actions for General Public Includes Stockpile or Predistribution of Ki for Prophylactic Use ML20096A4911995-12-22022 December 1995 Georgia Power Co Reply to Intervenor & NRC Staff Proposed Findings of Facts & Conclusions of Law.* W/Certificate of Svc ML20095D9821995-12-12012 December 1995 Georgia Power Co Motion to Correct Record of Exhibits of Diesel Generator Reporting Issues Allegation Hearing.* W/Certificate of Svc ML20095D9771995-12-0808 December 1995 Comment on Proposed Generic Ltr Boraflex Degradation in Spent Fuel Pool Starage Racks. Request for Licensees to Demonstrate Subcriticality Margin in Unborated Water,Seems Inconsistent W/Stated Benefit of Borated Water ML20094S2751995-11-30030 November 1995 Intervenor Final Statement of Fact & Conclusions of Law.* Board Finds That Util & Applicant Failed to Meet Burden of Proof Re Ultimate Issue of Character,Competence & Integrity. W/Svc List ML20094S2411995-11-22022 November 1995 Georgia Power Co Response to Intervenors Motion for Continuance.* Intervenor Motion Unjustified & Prejudicial & Should Be Denied.W/Certificate of Svc & Svc List ML20094S2931995-11-21021 November 1995 Intervenor Motion for Continuance for Good Cause.* Requests Deadline for Filing Post Hearing Brief Be Extended Until 951130.W/Certificate of Svc & Svc List ML20094K1161995-11-0909 November 1995 Intervenor Motion to Admit Supplementary Exhibits.* Moves That Naslp Admit Encl Documents Into Evidence for Listed Reasons.W/Certificate of Svc & Svc List ML20094J9301995-11-0606 November 1995 Georgia Power Company Motion to Correct Record of Diesel Generator Reporting Issues Allegation Hearing.* Moves Licensing Board to Order That Corrections Be Made to Transcript.W/Certificate of Svc & Svc List ML20094J9281995-11-0606 November 1995 Gap Proposed Findings of Fact & Conclusions of Law on Diesel Generator Reporting Issues.* Findings of Fact & Conclusion Accepted.W/Certificate of Svc ML20094J9201995-11-0101 November 1995 Affidavit of Ck Mccoy to Correct Info Contained in Intervenor Exhibit II-97,which Consists of Portions of Deposition in a Mosbaugh Complaint Against Gap 1999-06-28
[Table view] |
Text
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April 9, 1990 0FFICE Of SECRETARY I Ee '
- w. a. s.i,. .m 00CKETING BRAHC &"@h sene ne eei.o.m w c w o ce<m ens ELV-01516 0012 Docket No. 50-424 U. S. Nuclear Regulatory Commission -
Region !!
101 Marietta Street, N. W.
Atlanta, GA 30323 ATTN: Mr. S. D. Ebneter
Dear Mr. Ebneter:
' V0GTLE ELECTRIC GENERATING PLANT CONFIRMATION OF ACTION LETTER On March 20, 1990, a site area emergency was declared due to a loss of offsite power concurrent with a loss of onsite emergency diesel generator capabil8ty. ,
Following the event, GPC received a Confirmation of Action Letter dated March i 23, 1990 concerning certain actions we were taking. We have reviewed the l March 20th event and the appropriate corrective actions necessary for entry into Mode 2 have been accomplished. Therefore, we are requesting approval to return Unit I to Moda 2 and subsequent power operation. The following discussion provides justification for this request.
In accordance with Vogtle Electric Generating Plant procedures, an event review team has investigated the events leading up to and following the site area emergency. The event review team has presented the results of it's review to management and those recoamendations considered important for continued safe plant operation have been implemented. These include establishment of a management >olicy on control and operation of vehicles (see attached letter from George Bock)old to site personnel); upgrading of emergency notification network communications (see attached letter from George Bockhold to Emergency Directors and Cosununicators); retesting and calibration of both Unit 1 emergency diesel generator control systems; temporary barricades to prevent unnecessary entry into low voltage switchyard areas; and communications of immediate corrective actions related to operations to licensed operators.
In addition, the event review team report also contains a number of longer-term recommendations which require additional management review and evaluation.
These include the sequencing of outage activities; plant conditions during mid-loop operations; post-maintenance diesel functional testing; emergency notification system upgrades; changing diesel generator control logic; and re-evaluating the duties and responsibilities of the Emergency Director.
9505230086 950417 DR ADOCK 0500 4 92 PROJECT 001623
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NUCLEAR REGULATORY COMMISSION re 9 a 9-o A 4 -1 DocketNo. fo var-oc4-1 Official Exh. No. '3 in the nutter of. Vo9 41e Lt a ' 4 5 1*1 Staff IEiNT!fCD /
Appi: cant 7 RECEIVED r inurvenor REJECTED Conro Ottr Con:ractor DATE O 'b i 7 - Q C Ottar Witness Ate (o y Reporter 7. 2 . l.'4 3 x . '
'8 d
GeorgiaPoner A U. S. Nuclear Regulatory Commission Region 11 ELV-01516 Paae Two The most significant occurrence during the event of March 20, 1990, involved the failure of Diesel Generator (OG) 1A to remain running to support shutdown cooling. Georgia Power Company, utilizing utility and vendor technical experts l has investigated the DG failure and has determined the following: '
- a. During bench testing, all three Jacket water temperature switches were found to be set high during the OG maintenance inspection in early March 1990 (by approximately 6-10 degrees F above the setpoint). All three were adjusted downward using a calibration technique that may have differed from that previously used. i
- b. Following the March 20 event, all three switches were again bench tested.
Switch TS 19110 was found to have a setpoint of 197 degrees F which was approximately 6 degrees F below its previous setting. Switch TS 19111 was I found to have a setpoint of 199 degrees F which was approximately the same i as the original setting. Switch T5 19112 was found to have a setpoint of {
186 degrees F which was approximately 17 degrees F below the previous.
setting and was readjusted. Switch TS 19112 also had a small leak which was judged to be acceptable to support diagnostic engine tests and was reinstalled,
- c. During the subsequent test run of the DG on March 30, one of the switches (TS 19111) tripped and would not reset. This appeared to be an ,
intermittent failure because it subsequently reset. This switch and the leaking switch (TS 19112) were replaced with new switches. All subsequent t testing has been conducted with no additional problems.
- d. The Unit 1 jacket water temperature switches have been recalibrated with the manufacturer's assistance to ensure a consistent calibration technique.
- e. Subsequent testing indicated that the diesel annunicator indication of March 20, 1990 is reproduced on a high jacket water temperature trip.
f.
A test of the jacket water system temperature transient during engine starts was conducted. The purpose of this test was to determine the actual I jacket water temperature at the switch locations with the engine in a nomal standby lineup, and then followed by a series of starts without air rolling the engine to replicate the starts of March 20. The test showed that jacket water temperature at the switch location decreased from a standby temperature of 163 degrees F to approximately 156 degrees F and remained steady.
'2 PRO'N oog24
GeorgiaPoner A U. S. Nuclear Regulatory Comission Region II ELV-01516 Paae Three
- g. Since March 20, 1990, GPC has performed numerous sensor calibrations (including jacket water temperatures , extensive logic testing, special pneumatic leak testing, and multiple) engine starts and runs under various 1 conditions. Since March 20, the 1A DG has been started 18 times, and the 18 DG has been started 19 times. No failures or problems have occurred {
during any of these starts. In addition, an undervoltage start test 1 l
without air roll was conducted on April 6,1990 and the 1A D/G started and loaded properly.
Based on the above facts, we have concluded that the jacket water high tamperature switches were the most probable cause of both trips on March 20, 1990.
In addition, the following actions have been or are being implemented to ensure a high state of diesel reliability.
- 1. Operators are being trained prior to their next shift to ensure that they understand that an emergency reset will override the high jacket water temperature trip. Alars response procedures will be revised to address emergency reset functions prior to April 30, 1990.
- 2. The undervoltage start feature of the Unit 1 DGs has been modified such that the non-essential engine trips are bypassed. However, alarms are still provided to inform the operators of off normal conditions. (This change will be implemented on Unit 2 prior to April 30,1990.)
- 3. GPC is evaluating the possibility of a design change and Technical Specification change to delete the jacket water high temperature trip as an essential engine trip.
- 4. GPC has reviewed air quality of the D/G air system including dewpoint l control and has concluded that air quality is satisfactory. Initial reports l of higher than expected dewpoints were later attributed to faulty instrumention. This was confirmed by internal inspection of one air receiver on April 6,1990, the periodic replacement of the contol air filters last done in March,1990 which showed no indication of corrosion and daily air receiver blowdowns with no significant water discharge.
- 5. Based on discussions with the NRC in Atlanta on April 9,1990, GPC will finish reviewing the event review team's long term recomendations and will transmit a summary and schedule of the actions taken or to be taken to the NRC by May 15, 1990. The administrative >rocedures that specify control of vehicles in the perimeter area will also >e revised by May 15.
92 PROJECT 001625
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l Georgia P0her b U. S. Nuclear Regulatory Commission Region 11 ELV-01516 Paae Four
- 6. GPC will continue to work with the IIT and an independent lab to evaluate the instruments currently under quarantine. Upon completion of the the lab test, calibration procedures will be revised as necessary to ensure ;
consistent performance.
Completion of these ' investigations, reviews, tests and corrective actions justify GPC's determination that the DG's are operable. GPC will continue to work with the Transamerica DeLaval Incorporated Owners Group to improve DG reliability. GPC will also review possi >1e improvements to protective instrumentation and controls.
Based on the above discussion, we have completed the appropriate corrective actions necessary to safely operate the unit. We request NRC approval to allow Unit 1 to return to operation.
Should you have any questions, please inquire.
Sincerely, N. . !$= M W. G. Hairston, III WGH,III/NJS/gm Attachment xc: Georaia Power Connany Mr. C. K. McCoy ;
Mr. G. Bockhold, Jr.
Mr. R. M. Odos I Mr. P. D. Rushton )
NORMS '
l U. S. Nuclear Reculatory Commission l
Document Control Desk i Mr. T. A. Reed, Licensing Project Manager, NRR Mr. R. F. Aiello, Senior Resident Inspector, Vogtle 92 PROJECT 001626
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