ML20082T150

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Monthly Operating Rept for Oct 1983
ML20082T150
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 11/01/1983
From: Brons J, Kelly L
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
IP-LK-3467, NUDOCS 8312150182
Download: ML20082T150 (7)


Text

{{#Wiki_filter:, ~ - r 4 OPERATING DATA REPORT DOCKET NO. 50-286 DATE 11/01/83 COMPLETED BY L. Kelly TELEPHONE (914) 739-8200 OPERATING STATUS

1. Unit Name:
  • Indian Point No. 3 Nuclear Power Plant Notes October 1983
2. Reporting Period:

-3. Licensed Thermal Power (MWt): 3025

4. Nameplate Rating (Gross MWe):

1013 '5. Design Electrical Rating (Net MWe): 965 2 6. Maximum Dependable Capacity (Gross MWe): 1000

7. Maximum Dependable Capacity (Net MWe):

965 - G. If Changes Occur in Capacity Ratingt (items Number 3 Through 7) Since Last Report. Give Reasons:

9. Power Level To Which Restricted,if Any (Net MWe):
10. Reasons For Restrictions. If Any:

This Month Yr to.Date Cumulative 745 7296.0 62,057.0

11. ~ Hours in Reporting Period
12. Number Of Hours Reactor Was Critical 0

333.7 34,424.5 - 13.' Reactor Reserve Shutdown Hours 0 0 0

14. Hours Generator On-Line 0

229.1 33,142.0 ~ 15. Unit Reserve Shutdown Hours 0 0 0

16. Gross Thermal Energy Generated (MWH) 0 282,244 86,425,645
17. Gross Electiical Energy Generated (MWH) 0 68,310 26,366,610
18. Net Electrical Energy Generated (MWH) 0 60,735 25,244,178

.19. Unit Service Factor 0 3.1 52.7

20. Unit Availability Factor 0

3.1 52.7 0 .9 41.6

21. Unit Capacity Factor (Using MDC Net).
22. Unit Capacity Factor (Using DER Net) 0

.9 41.6 100 93.4 20.9

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each1:

Januarv 1984

25 ' If Shut Down At End Of Report Period. Estimated Date of Startup:

26 = Units in Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMM ERCI A L OPER ATION 8312150182 831101 PDR ADOCK 05000286 R PDR _ _. ~ _ - _.., - - -. _. _ ~ _ _ _. - _ _ _ _.. _ _

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-286 Indian Point UNIT No. 3 DATE 11-1-83 COMPLETED BY L Kelly TELEPHONE (914) 739-8200 MONTH October 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 1MWe-Neti 1 0 37 0 2 0 0 jg 3 0 39 0 4 0 20 0 5 0 21 0 6 0 22 0 23 0 7 0 8 0 0 24 9 0 25 0 10 0 26 0 11 0 27 0 12 0 0 2g 13 0 0 29 14 0 0 30 !5 0 0 3g 16 0 INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the reportmg month. Compute to the nearest whole megawatt. '~ (9/77) a_. _ x.

DOCKET NO. _ 50-286 UNITSHUTDOWNS AND POWER REDUCTIONS UNIT NAME ' NO. 3 DATE 11/1/83 COMPLETED BY L-Kelly REPORT MONTH October 1983 TELEPHONE 914-739-8200 -l 's en 3 5* e -ei c Cause & Corrective .2 _e E 7.c X Licensee g% o No. Date g gg g ,g g 5 Event u? E3 Action to $E cE j5g Report er NG V Prevent Recurrence 6 03 830618 F 745 A 3 N/A N/A Electrical malfunction in the main generator. 1 1 2 3 4 F: Forced Reason: Method: Exhibit F Instructions S: Scheduled _ A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Reporn (LER) Fde(NUREG-D-Regulatory Restriction 4-Other (Explain) 0161) E-Operator Training & License Examination F-Administrative 5 G-Operational Error (Explain) Exhibit 11 Same Source (9/77) Il-Other (E xplain)

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SUMMARY

OF OPERATING EXPERIENCE f YJ y OCTOBER 19834 a s ^Y t [ Indian PSiNt'Uhitl3 remains. in 'a ' forced. outage ' caused,by a. malfunction, J Ein the' main electrich generator.- 71 _1 Repairs!are'now in' progress:dnd:it 'is estimated that the' unit will be [- e-freturnedtofserviceinJahuary1984. l1,a'- a ~:- a ~ b f T = N ~ ,I. -' s s ? Y -{^_, L -'h4+= 3 o w 'e ' e y-- ' ' ~,- 2 4 t 9 +% .. '1 ,\\m,' I J J ~ ,4,)' 1 W Y ' j.), J f ..;.e <, Ud , q., e ,.?4.

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k 3 MONTHLY MAINTENANCE REPORT. October 1983; ~ MONTH _Page 1 of 2 MWRf DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION 3716 10-04-83 Pressurizer Level valves valve packings'leake Repacked Valves 531, 532, 533, 534, 537 and 538 3729 10-04-83 Reactor Coolant Letdown Valve bonnet gasket leaks Replaced gasket Isolaticn Valve 204B 3871 10-04-83 Fuel Handling Platform Platform does-not move Tightened loose transformer wire 'i Hoist in Fuel Storage Building 3847 10-11-83

  1. 31 Steam Generator Blow-Dual indication Adjusted micro-switch down Valve 1.114 3826 10-14-83 Fan Cooler Unit #35 Motor Motor cooler leaks' Repaired leaks Cooler 3917 10-14-83 Fan Cooler Unit #31 Motor Motor cooler leaks Replaced cooler l

Cooler 3912 10-14-83 Fan Cooler Unit #32 itotor Motor cooler leaks Repaired leaks Cooler 3916 10-14-83 Fan Cooler Unit #33 Motor Motor coooler leaks Repaired leaks Cooler 3915 10-14-83 Fan Cooler-Unit #34 Motor Motor cooler leaks Repaired leaks Cooler 3927 10-17-83 Residual Heat Removal Pump Seal piping weld leak Replaced pipe and rewelded

  1. 32 Seal Cooler Piping l

l 3942 10-25-83 Residual Heat Removal Irr. proper valve indication Adjusted limit switch arm Valve 958

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MONTHLY I & C CATEGORY I REPORT October'1983 MONTH W.R. # DATE EQUIPMENT MALFUNCTICN CORRECTIVE ACTION IC-2002 7-18-83 Liquid Waste Line Flowmeter Inoperative digital display Replaced digital display unit IC-2059 9-12-83 Hydrogen Recombiners 31 and Alarm constantly up Corrt.cted improper wiring of alanr 32, High Temperature Alarm relay IC-2188 7-15-83 Reactor Protection Train B, Does not bring up test light Rewired relay to spare contacts Under Voltage Relay 27-lX-X1 IC-2313 9-21-83 Position Indicator for Service Improper valve position indication Corrected faulty connection on Water Valve 1276. light socket O -e

.O'~ ~ - Indien Point 3 Cluclear Power Plant . P.O. Box 215 Buchanan, Newwrt 10511 914 739.3200

  1. > NewWrkPbwer 4ff Authority November 10, 1983 IP-LK-3467 Docket No. 50-286 License No. DPR-64 Director, Nuclear Reactor Regulation office of Management Information and Program Control U. S. Nuclear Regulatory Commission Washington, D C. 20555

Dear Sir:

Enclosed you will find two copies of the monthly operating report relating to Indian Point 3 Nuclear Power Plant for the month of October, 1983. Very truly yours, Ifotm C. Brons b idencca.ager LK/88 J Enclosure cc: Director, Office of Inspection & Enforcement (40 copies) c/o Distribution Services Branch, DDC, ADM U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Dr. Thomas E. Murley, Regional Administrator Region 1 U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 IP3 Resident Inspector's Office George Wilverding (SRC), WPO J. P. Bayne, WPO S. V. Fuller, NYO W.-R. Yario, NYO j INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 -.}}