ML20081F848

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/03L-0:on 830930,APRMs 2,3,4 & 5 Gain Adjustment Factor Exceeded Tech Spec Requirements.Caused by Failure to Follow Shutdown Procedures.Personnel Involved Reinstructed Re Adherence to Procedure
ML20081F848
Person / Time
Site: Dresden Constellation icon.png
Issue date: 10/27/1983
From: Bergan G, Scott D
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
83-1039, LER-830-036-03L, LER-830-36-3L, NUDOCS 8311040005
Download: ML20081F848 (3)


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3 60 63 GCCXET NUMBER 6a 69 EVENT CATE 74 75 REPCRT CATE 40 CVENT CESCRIPTION AND PRCSA8LE CCNSECUENCES h 6o62I l During a normal unit shutdown, the APRM gain adjustment factor (AGAF) for APRM's 2, 3, l

l i o 131 14 and 5 exceeded 1.03 Because both scram channels had less than the minimum numbel of l.

o i A; joperable APRM channels, Tech Spec Table 3.1.1 action B was invoked.

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Safety significance was minimal since IRM's were fully inserted and opera-g 1loisI itional.

There was no effect on health or safety of the public.

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42 43 44 47 CAuSE DESCalPTICN AND CCRRECTIVE ACTICNS h itoll The event was caused by failure to follow shutdown procedure DGP 2-1 Which reouires an 1

itill instrument mechanic be ' utilized for gain adjustments.

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i621 l compliance with Tech Specs was achieved within an hour.

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o NAME CF PREPARER PHCNE:

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Telephone 815/942-2920 October 27, 1983 DJS.Ltr #83-1039 James G. Keppler, Regional Administrator

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U.S. Nuclear Regulatory Comaission 799 Roosevelt Road Glen Ellyn, IL 60137 Reportable Occurrence Report #83-36/03L-0, Docket #050-249 is being submitted to your office In accordance with Dresden Nuclear Power Station Technical Specification' 6.6.B.2.(b), conditions leading to operation in a degraded mode permitted by a. limiting condition for operation or plant shutdown required by a 1imiting condition for operatlon.

M D.. Scott Station Superintendent Dresden Nuclear Power Station l-DJS/kJ1 Enclosure cc: Director of Inspection & Enforcement Director of Management Information & Program Control U.S. NRC, Document Management Branch File /NRC U

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,.'a DEVIATION REPORT

)C V";No 12.

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72 STA UNIT YEAR NO.

P ART 1 l-TITLE OF,Dt.eATION OCCURREO 9/30/83 2314 U-3 APRM Gains Greater Than 1.03 cart rivr SYSTEM AFFECTED 0700 PLANT STATUS AT TIME O/ EVENT TESTING Run 428 0

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CESCRIPTION OF EVENT g

was 1.153, APRM #3's gain was 1.122, APRM #4's gain was 1.102 and APRM #5's gain was 1.156.

Since the unit was coming down for the refueling outage, action B from Table 3 1.1 of the Tech Spec was followed by reducing power level to IRM range and olacina mode switch in the startup/ hot standby position within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

10 CFR50.72 NRC RED PHONE C

NOTIFICATION MADE YES NO EOUIPMENT FAILURE N/A OYES O NO

.ORx ReOuEsT NO.

aEsPcNsietE suPERvisO, Gary L. N G IMM g,rg P ART 2 l OPER ATI NG ENGINEER'S COMMENTS The unit was placed in a condition where the APRM's were not required. The APRM gains will be adjusted, as required, prior to the unit startup after the current refueling outage.

O EVENT OF PUBLIC I N TE R E ST O 24* HOUR NRC NOTIFICATION REO'D O TECH. SPEC. VIOLATION TELEPH REGION III DATE TIME O NON REPORTABLE OCCURRENCE TELEGM/TELECOPy N/A O 14 OAY REPORTABLE /T.S.

REGION ll1 DATE TIME G 30 DAY REPORTAstE/T.S 6.6. B. 2.b CECO CORPOR ATE NOTIFIC ATION MADE O ANNUAL /SPECL REPORT REQ'O IF ABOVE NOTIFICATION IS PER IOCFR21 A.I.R.

] 5-DAY WRITTEN REPORT REC'D PER 10CFR21

,83-36/03L-0 Telecopy L.E.R.

gg Dennis P. Galle 10/20/83 1359 CECO CORPORATE CFFICE9 DATE TIME PRELIMINARY REPORT T.A. Ciesta 10/20/83 COMPLETED AND REVIEnED WMING ENGINEER DATE E E Y T T ON R c2e L,

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AUTHORIZEO FOR OISTRIBUTION

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INTENDENT DATE I e6 5174 (F04w 15 52-1) 10-81