ML20076H764
| ML20076H764 | |
| Person / Time | |
|---|---|
| Site: | Point Beach |
| Issue date: | 06/06/1983 |
| From: | Fay C WISCONSIN ELECTRIC POWER CO. |
| To: | |
| References | |
| NUDOCS 8306200137 | |
| Download: ML20076H764 (9) | |
Text
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- ssco EEd OPERATING DATA REPORT 00 DOCKET NO. 50-266 EO DATE June 6, 1983 COMPLETED BY C. W. FAY If
-DM TELEPHONE 414 277 2811 Ef OPERATING STATUS
- 1. UNIT NAME: PUINT BEACH NUCLEAR PLANT UNIT 1
. NOTES
- 2. REPORTING PERIOD:
MAY 1983
- 3. LICENSED THERMAL POWER (MWT): 1518.
- 4. NAMEPLATE RATING (GROSS MUE):
523.8
- 5. DESIGN ELECTRICAL RATING (NET MWE): 497.
- 6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 519.
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 495.
- 8. IF RANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
NOT APPLICABLE
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE):
390.0
- 10. REASONS FOR RESTRICTIONS, (IF ANY):
Power level restricted because of self-imposed hot leg limitation in an attempt to limit steam generator tube corrosion.
THIS MONTH YR TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD 744 3,623 110,159
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 744.0 3,574.6 91,146.9
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 1.4 625.4
- 14. HOURS GENERATOR ON LINE 744.0 3,567.9 88,676.2
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 793.5
- 16. GROSS THERMAL ENERGY GENERATED (MWH) 869,323 4,157,849 120,106,838
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 290,650 1,387,130 40,262,920
- 18. NET ELECTRICAL ENERGY GENERATED (MWH) 274,967 1,314,039 38,295,757
- 19. UNIT SERVICE FACTOR 100.0 98.5 80.5
- 20. UNIT AVAILABILITY FACTOR 100.0 98.5 81.2
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 74.7 73.3 71.1 m
- 22. UNIT CAPACITY FACTOR (USING DER NET) 74.4 73.0 69.9
- 23. UNIT FORCED OUTAGE RATE 0.0 0.1 2.7 5-
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
Twenty-six week refueling and steam generator replacement outage scheduled to commence September 30, 1983.
- 25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NOT SHUTDOWN DATA REPORTED AND FACTORS CALCULATED AS REQUESTED IN HRC LETTER DATED SEPTEMBER 22, 1977
DOCKET NO.
50-266 UNIT NAME Point Beach Unit 1 DATE June 6, 1983 COMPLETED BY C.
W.
Fay TELEPHONE 414/277-2811 AVERAGE DAILY UNIT POWER LEVEL MONTH May, 1983 AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1
371 11 370 21 373 2
372 12 371 22 373 3
373 13 371 23 372 4
371 14 373 24 371 5
371 15 369 25 372 6
362 16 371 26 373 7
310 17 373 27 373 j
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8 371 18 372 28 372 9
372 19 373 29 373 10 372 20 373 30 372 31 372 s
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NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE Docket No.
50-266 Unit Name Point Beach Unit 1 Date June 6, 1983 Completed By C. W. Fay Phone 414-277-2811 Unit 1 operated at approximately 371 MWe net throughout the period with no major load reductions.
The primary-to-secondary leakage remains stable at less than ten gallons per day.
On May 16 at approximately 1405 hours0.0163 days <br />0.39 hours <br />0.00232 weeks <br />5.346025e-4 months <br />, contractor personnel accidentally spilled ten gallons of water, slightly contaminated from the rinsing of respirators.
The spill was isolated on a
(
15 ft. by 15 ft. area outside the Unit 1 facade, and cleaned up.
The NRC was notified via red phone.
On May 21 at 2336 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.88848e-4 months <br />, Unit 1 boric acid line to the blender became blocked restricting boric acid flow to the volume control tank.
The heat trace circuits were adjusted higher and the flow path was restored to operability at 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> on May 22.
The circuits were returned to normal and have been operating with no problems since.
On May 23 at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />, the 3D emergency diesel generator experienced a fast start pickup of bus 2A05 when personnel opened the door to 2A05 potential transformer inside the switchgear panel which resulted in an open circuit.
This event required reporting to the NRC via red phone.
On May 26 at approximately 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, Unit 1 "A" reactor coolant i
pump was experiencing oscillating leakage rates past the No. 2 j
seal.
The leakage returned to normal by 1316 hours0.0152 days <br />0.366 hours <br />0.00218 weeks <br />5.00738e-4 months <br /> and is currently being closely monitored.
Other safety-related maintenance completed during the period included the changeout of reactor trip relay 1RT-6B and repairs to a packing leak on the "A" steam generator steam line vent valve.
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s OPERATING DATA REPORT DOCKET NO. 50-301 DATE June 6, 1983 COMPLETED BY C. W. FAY TELEPHONE 414 277 2811 OPERATING STATUS
- 1. UNIT NAME: POINT BEACH NUCLEAR PLANT UNIT 2
. NOTES
- 2. REPORTING PERIOD:
MAY 1983
- 3. LICENSED THERMAL POWER (MWT): 1518.
- 4. NAMEPLATE RATING (GROSS MWE):
523.8
- 5. DESIGN ELECTRICAL RATING (NET MWE): 497.
- 4. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 519.
- 7. MAXIMUM DEPENDABLE CAPACITY (NET NWE): 495.
- 8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
NOT APPLICABLE
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (HET MWE): NOT APPLICABLE
- 10. REASONS FOR RESTRICTIONS, (IF ANY): NOT APPLICABLE THIS MONTH YR TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD 744 3,623 94,944
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 0.0 2,003.6 84,061.7
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 196.8
- 14. HOURS GENERATOR ON LINE 0.0 1,992.9 82,648.1
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 181.2
- 16. GROSS THERMAL ENERGY GENERATED (MUH) 0 3,007,255 114,522,849
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 0 1,009,260 38,810,660
- 18. NET ELECTRICAL ENERGY GENERATED (MWH) 0 962,348 36,951,315
- 19. UNIT SERVICE FACTOR 0.0 55.0 87.0
- 20. UNIT AVAILABILITY FACTOR 0.0 55.0 87.2
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 0.0 53.7 79.2
- 22. UNIT CAPACITY FACTOR (USING DER NET) 0.0 53.4 78.3
- 23. UNIT FORCED OUTAGE RATE 0.0 0.0 1.5
- 24. SHUTDOWNS SCHEDULED DVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
NONE
- 25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: JULY 1, 1983 4
DATA REPORTED AND FACTORS CALCULATED AS REQUESTED IN NRC LETTER DATED SEPTEMBER 22, 1977
l DOCKET NOo 50-301 UNIT NAME Point Beach Unit 2 i
)
DATE June 6, 1983 COMPLETED BY C.
W.
Fay TELEPHONE 414/277-2811
,l AVERAGE DAILY UNIT POWER LEVEL MONTH May, 1983 AVERAGE AVERAGE-AVERAGE DAILY DAILY DAILY i
POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1
-2 11
-2 21
-2 2
-2 12
-2 22
-2 3
-2 13
-2 23
-2 4
-2 14
-2 24
-2 5
-2 15
-2 25
-2 6
-2 16
-2 26
-2 7
-2 17
-2 27
-2 8
-2 18
-2 28
-2 9
-2 19
-3 29
-2 10
-2 2d
-2 30
-2 31
-2 AD-28A (1-77)
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-301 UNIT NAME Point Beach Unie 2 DATE June 6, 1983 REPORT MONTH May. 1983 COMPLETE D BY C.
W.
Fay TELEPHONE 414-277-2811 m
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1 N/A ZZ ZZZZZ2 Completed week 10 of the continuing 14-week refueling and steam gener-ator sleeving outage.
F: Forced Reason:
3 4
Method:
Exhibit G-Instruc-S: Scheduled A-Equipment Failure (explain) l-Manual tions for Prepar-B-Maintenance or Test 2-Manual Scram ation of Data Entry C-Refueling 3-Automatic Scram Sheets for LER File D-Regulatory Restriction 4-Other (explain)
E-Operator Training & License Exam F-Administrative 5
AD-28B Exhibit I-Same G-Operational Error (explain)
Source (01-78)
H-Other (explain)
NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE Docket No.
50-301 Unit Name Point Beach Unit 2 Date June 6, 1983 Completed By C. W. Fay Phone 414-277-2811 Unit 2 was shut down during the entire report period as it completed the tenth week of the scheduled 14-week refueling and steam generator sleeving outage.
Outage-related work included the installation of replacement tube bundles for "A",
"B",
"C",
and "D" moisture-separator-reheaters, the installation of replace-ment feedwater heaters 4A and 4B, the turbine overhaul, the installation of pressurizer relief valve header supports, refueling calibrations, the changeout and testing of NBFD reactor protection system relays, repairs to various diaphragm valves in the chemical and volume control system, cleaning of the incore thimbles, cleaning of the existing Nos. 5A and 5B feedwater heaters, and the changeout of radiation monitors 2Rll/R12.
Inspection of optimized fuel assembly ZD3 has identified at least nine rodlets with through-clad defects.
These defects are all at the first (lowest) grid elevation.
At other locations, not necessarily at grid elevations, through-wall penetrations and zircaloy hydriding were noted.
This damage appeared to have been initiated from the inside of the rod.
It is believed that these through-wall penetrations were the result of secondary zircaloy hydriding caused by the inleakage of reactor coolant via the fretting induced penetrat. ions at the first grid elevation.
ZD3 is one of our optimized fuel assemblies in Unit 2 for testing purposes.
The other three assemblies, as well as the 69 reload standard assemblies, have been wet and dry sipped for possible leakage.
No other assemblies had indications of leakage.
In addition to sipping, the other three optimized fuel assemblies were visually inspected with no anomalies noted.
Additionally, a sampling of rods were measured for breakaway forces and visually inspected to add further assurance of no similar degradation of the clad.
No abnormal readings were recorded.
A 24-hour notice has been filed with the NRC.
The sleeving work scheduled during this outage has been completed in "B" steam generator and is approximately 59% complete in "A"
l
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insconsin Electnc MWER COMPANY 231 W. MICHIGAN, P.O. BOX 2046, MILWAUKEE, WI 53201 June 13, 1983 Director of Regulatory Operations U.
S.
NUCLEAR REGULATORY COMMISSION Washington, D.
C.
20555 Gentlemen:
MONTHLY OPERATING REPORTS POINT BEACH NUCLEAR PLANT Attached are monthly operating reports for Units 1 and 2, Point Beach Nuclear Plant, for the calendar month of May 1983.
Very truly yours, W
j
/
(,
Vice President-Nuclear Power C. W.
Fay Attachments Copies to J.
G.
Keppler - NRC, Region III NRC Resident Inspector C.
F.
Riederer - PSCW t
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