ML20072P883
ML20072P883 | |
Person / Time | |
---|---|
Site: | Wolf Creek |
Issue date: | 03/30/1983 |
From: | Moriarty J COLT INDUSTRIES, INC. |
To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
References | |
REF-PT21-83 NUDOCS 8304040406 | |
Download: ML20072P883 (1) | |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
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Text
SiH/12 Colt Industries lf'jn*,"$}f,7l*n' 701 Lawton Avenue
@ Beloit. Wisconsin 53511 608/364-4411 March 30, 1983 ,
Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Ill. 60137 Attention: Mr. James G. Keppler, Director, Region III
Subject:
Colt Industries-Fairbanks Morse Engine Division Emergency Diesel Generators Possible Thermostatic Valve Malfunction Fail Safe To " Full Cooling Position" Part 21 Report Supplemental Report No. 5 - SNUPPS Kansas Gas & Electric - Wolf Creek
References:
May 25,1982; June 28,1982 and September 17, 1982 Part 21 Reports - Robertshaw Valves - same subject Gentlemen:
The lower overrun assemblies in the Robertshaw valves installed on the Diesel Generator Sets at the Kansas Gas & Electric, Wolf Creek Station have been replaced with overrun assemblies utilizing cotter pins to positively lock the nut to the stem.
The units are now free of the reported potential defect.
A copy of this report is being forwarded to the utility involved.
Very truly yours, n
Y M .
. toriarty V MANAGER UTIL Y ALES JMM:jc cc: Bechtel Power Corp.
P. O. Box 607 Gaithersburg, MD 20760 Attention: SNUPPS Project Engineer U. S. Nuclear Regulatory Commission c/o Document Management Branch Washington, D.C. 20555 Robertshaw Controls Company P. O. Box 400 Knoxville, TN 37901 Attention: T. T. Howell, Quality Mgr. _ ,