ML20072G643

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Special Rept:On 940812,discovered That Plant Vent Radition Monitor Had Been Inoperable for More than 72 Hours.Cause Under Investigation.Technicians Counselled Re Procedural Compliance
ML20072G643
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 08/19/1994
From: Hovey R
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9408250046
Download: ML20072G643 (2)


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Pubhc Service Elecinc and Gas Company P O. Box 236 Hancocks Bridge, New Jersey 08038 Hopo Creek Generating Station j

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l August 19, 1994 U.S.

Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

Hope Creek Generating Station Docket No. 50-354 Unit No. 1 Special Report 94-02 This Special Report is being submitted pursuant to the requirements of Hope Creek Technical Specification 3.3.7.5 -

action 81, due to the South Plant Vent Radiation Monitor being inoperable for more than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

On 8/12/94, a Radiation Protection department supervisor performing a review of a radiation monitoring system (RMS) mismatch report noticed that the South Plant Vent (SPV) mid and high range noble gas detectors were out of service.

The supervisor initiated corrective actions to place the detectors in service and initiated a root cause investigation into the event.

The cause of the monitors coming out of service has not be determined and is currently being investigated.

The skid had been taken out of service, on 8/3/94, to perform a weekly grab sample and may not have been properly restored.

On 8/4/94 a technician, performing a daily review of a RMS data base mismatch report, had noticed the out of service condition but had assumed that an l

unrelated work order for repairs to a separate detector on the skid was tracking and resolving the mid and high range monitors being out of service.

Radiation protection technicians continued to identify and track the out of service detectors each day, against the incorrect work order, until the supervisor detected the problem on 8/12/94.

Procedural non-compliance was identified as the root cause of l

the detectors-not being returned to service on 8/4/94.

Procedural requirements for initial notification of the out of service condition were not performed as specified.

A less than adequate procedure was identified as the root cause of the delay in corrective actions not being implemented until 8/12/94.

The procedure did not clearly address actions to be taken for a previously identified data mismatch.

It should be noted that the daily checks of the {RMS) mismatch report were imposed and performed administratively and the technical specification surveillance requirements for these detectors were met.

ff2 2-The Energy People 9408250046 940819

/!0 ADOC/, 05000354 PDR "3"'"

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i Corrective actions for this event include counseling for the technicians in regard to procedure compliance.

Additionally, the procedure is being revised to review the status report with the nuclear shift supervisor each time a discrepancy is

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noted to ensure the problem has been identified and corrective actions are being implemented.

Additional corrective actions will be implemented as necessary following i

the completion of the root cause investigation for the skid not being returned to service following sampling.

Sincerely, Hovey,

R.J.

General Manager -

Hope Creek Operations LLA/

C Distribution

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