ML20071L839

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Monthly Operating Rept for Jul 1982
ML20071L839
Person / Time
Site: Cook 
Issue date: 08/04/1982
From: Might A
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20071L837 List:
References
NUDOCS 8209240117
Download: ML20071L839 (6)


Text

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CPERAT:NC DATA REPORT DCC's".II' NO.

50-316 DATI 8/4/R?

Cost?LETED EY A Muht TE1.I? SONG (616 ) 465-5901 OPERAT!NG S ATUS Notes Dona 1d C. C00k 2

1. Unit Nacte:

Ju1y 1982

2. Reporting Ps:fod:

3391

3. U~M Th :=:1 Power (StWt):

1133

4. N2=entat's asci=;(Cross atWe):

1100 S. Design Ele==i=1 R:: int (Net 51We):

1118

6. Sf'd-sum Depend:ble Capsci:y (Cross 51We):

1082 T. Siaxi=== Depe=d:b!: C:::ci:y (Net 31We):

S. If Ch:nges Oc:ar in Cap 2ci.y Rati:gs (1::=s Nu=ther 3 Through 7) Sine: I.:st R=por:. Give Rusons:

9. ?ower L vel To Which Res=::::d,If Any (Net 31We):
10. Resons For R:st:.=: foes.lf Asy:

This 5tonth Yrao-Data Cu=u!::ive 744 5087 40.151

11. Hou:s != Repor:ia: P::fod 744 4593.1 28.61R.1
12. Numb =r of Hou:s R==:or W:s C:i:i=1 0

0 0

i

13. Rese:or Rese:ve Shn::iown Hou=

744 4572.3 27.793.3

14. Hours Genen:sr Cn.U:,

0 o

n

15. Unic R: serve Shutdown Hot:=

2.496.782 15.061.R50 89.122.671

16. Cross The=n:1 E:::::y Cane :t=d (31WH) 801,930 4,938.010 28.645.810
17. Cross Elec:n=l Eser;y Gen ::::d (5tWH) 3'938 4.765.474 27.604 616
13. Net E2e==i=1 E r;y Genen::t C.tWH) 100 89.9 73.9
19. Unit Senic=.::::or 100 89.9 73.9
20. Uni: Av:112biE:y F:c:or 96.1 96 6 69.5
21. Uni: C:psci:7 :::=r(Usi=; MDC Net)

F 94:.6 85.2 68.6

22. Unit Capscity F:::or(Using DER Net) 0 10.1 13.5
23. Unic Fore:d Cu:sge R:te
24. Shutdouts Scheduled Over Nec 5 Stonths (Type. Date.:nd Du=:fon of.:ch1:
25. If ihn: Down At End Of Report Period. Esti==:ed D:te of Star: p:

. 25. Units in Tes: 5:::us (Prior to Ce==e cial Ope =:fon1:

Fore =st Achieved

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INITIA L CRIT *CAUTY INITIA L I:.ICTR:C;~Y CO?.i.*.:E?.C:A :. 0?SRA 7:0N l'8/~ l 8209240117 820810 PDR ADOCK 05000316 g

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AVERAGE DAILY UNIT POWER LEVEL OGCKET NO. 50-316 UNIT 2

DATE 8/3/82 CCMPLETED BY A. Might TELEPHONE (6161465-5901 MONTH July, 1982

^

~ DAY AVERAGE DAIt'l POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (if>E-Net) -

(MWe-Net) 1 1069 17 1039 2

1063 18 1042 3

1062 19 1043 4

1061 20 1044 5

1063 21 1049 6

1059 1065

'~

22 _

7 1053 23 1080 8

1054 24 1076

~

9 1047 25 1059 10 1036 25 1046 11 1051 27 1047 12 1053 28 1057 13 1039 29 1063 L

14 1049 30 1003 15 1045 31 696 16 1036 l

INSTRUCTIONS On this format list the average daily unit power level in MWe-Net for each l

day in the reporting month. Comoute to the nearest whole megawatt.

l

50-316

!)OCKE l NO.

llNil~ SiltillH)WNS ANil POWI H HEllllCllONS 3.C. Cook - Unit 2 UNII N AhlE DAll 8-10-82 ruslPli.ll:liliv Lklowf1LeL_

July,1982 616-465-5901 141POltI h!ONill

.I El.U'llONI:

PAGE 1 of 1 "E

a.

beg:ns m ene report per:od and ends :n :no6er. an entry should Sheets for Licensee Event Report (LER) Fde (NCREG4161 L be mace for both report pencds to be sure all snutdowns usmg de icilomng enuena:

cr ugmReant power redu:uons are reported.

TYPE. Lse "F" or "S" to mdic..e e:ther "For:ed" or "Sene.

daied." respe:nve:y. for each shutdown or sipiScut power B.

If not 2 :omconent failure, use 1e reisted ;om:enent.

reduenon. Fer:ed shutdowns.n:!ude those required to be e.g.. wrcng valve operated throup error: hst vatve 2s atuated by no later than the weekend to;lowmg dis cvery comocnent.

of an off-normal :endinon. It is re:cpt:ed that some judg-ment :s required m :stegonzmg shutdowns in th:s usy. In C.

If a cham of failures o :urs. :ne fint com enent to nai.

general. 2 for:ed snutdown is one that would not have been funeuen should be listed. The secuence ot" events.meiud.

ecmpicted in the icsen:e oide =ndit:en for which :orie:nve ing the other components wh::h fail. should be des = bed 2cuen was taken.

under the Cause 2nd Correenve Acuan to Prevent Recur.

rence column.

DURATION. Self explanatory. When a shutdown extends Components that.4o not fit any ex:stmg : ode should ce de.

beyond the end of 2 report per:od. count ortly de tme to the signated XXXXXX. The code ZZZZZZ should be used for end or the recort renod and : tex un the ensumg down t:=e events where 2 component des:rnation :s not 2;pii:2:le.

.n the fvCowmg report pences. Report dursuon of outages rounced to me nearest tenth of an hout to facditate summation.

CAUSE & CORRECTIVE ACTION TO PREVENT RECUR.

6he sum of tne total outsae hours plus the hours the geners.

RENC.,.. L.se t.,.e ceiumn m a narranve fastuon to ampaiy or tot was un h.oe should equal tne pcss hours in the reportma expiam the ctr umstances of de sautdown or power recucnon.

penod.

The column should me!ude the spec:il: :suse for each snut.

down or uitmde:nt power reducnon 2nd the :mmediate anc REASON. Catepnee M :etter deugnanun m acordan:e centernoisted lunt term corre:Uve 2cuen taken, if appropn.

witn the racie 2:;earmg on tne re: ort form. If :stegory H ste. ims ciumn snould also :e used,or a descr:: con of:ne must be used.su ;tv Or:el eumments.

maior s (ety.re!sted ;orreenve mamtenaner penor'mec dunna stETHOD OF SHUTTING DOwN THE REACTOR OR omsse or p we reduchen m !udgg an idenude: tion of REDUCING power. Catepnze ?y numner des:panun the mn.21 pam 2=q and 2 repen or any nnpe wue or radiosenvity ur smgie radistron exacsure spe.tnestly usee:.

1%e that this differs trom the Edisen E:e tr:: Insntute 4t'd "ith me out:2e wtuen secounts for more than 10 per.ent t EED denntacns of -Forced ?2rnal Outage" mc "Sene.

Vide 2110*2c;e annual v21ues.

au;ed Parnal Outm ' For these termi. eel uses 4 hange ut For long textus! reports eent:nue narrative an se:2rste :.2:er 10 MW as the creas pomt. For :arger puwer resetors.30 MW

.n.i reter n e the snutcown or power recu. nun roi "m

s em > mail a hange to war: ant espian2iton.

narranve.

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Docket No.:

50-316 Unit Name:

D. C. Cook Unit #2 Completed By:

C. E. Murphy TelerSone:

(616) 465-5901 Date: August 5, 1982 Page:

1 of 1 MONTHLY OPERATING ACTIVITIES - JULY, 1982 Highlights:

The Unit operated at 100% power for the entire reporting period except as detailed in the sumary.

The electrical generation for the month was 801,930 MWH.

Sumary:

7-02-82 The "AB" Diesel Generator was inoperable for a 2.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for the ICS Calibration.

7-09-82 The flow path for the Boric Acid Storage Tank via the transfer pumps and charging pumps to the Reactor Coolant System was made inoperable for a 1.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period to repair a body to bonnet leak on a manual isolation valve for Emergency Boration.

7-14-82 The North Rod Drive M.G. Set was out of sert ice for a 7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> period to replace a defective trip relay in the output breaker.

7-15-82 The Turbine Driven Auxiliary Feedpump was inoperable for a 1.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period to replace a coil in the Trip and Throttle Valve.

7-24-82 The Loop 3 over temperature AT instrument was inoperable for 6.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> to replace the set-point module.

7-30-82 At 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> a power reduction to 95% was started to perform a Moderator Temperature Coefficient Test. The test was completed at 1548 hours0.0179 days <br />0.43 hours <br />0.00256 weeks <br />5.89014e-4 months <br /> and the power level was returned to 100% at 0020 on July 31.

7-31-82 At 0145 the primary to secondary leak rate was calculated to be 0.17 gpm and at 0315 a controlled unit shutdown was started, with the Reactor being made sub-cirtical at 0211 on August 1,1982. The Unit is presently cooled down to Mode 5.

The RCS is degassed, depressurized, and at h loop being cooled by the RHP, System.

Preparations are being made to inspect #21 Steam Generator, for locating and plugging of any tubes that indicate leakage.

.s O'

DOCKET N0.

50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 8-10-82 COMPLETED BY B. A. Svensson TELEPHGNE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTENANCE JULY,1982 M-1 No. 2 steam generator power-operated relief valve, MRV-223, had a body-to-bonnet leak. Replaced the bonnet gasket and seal ring and had the valve retested.

M-2 Boric acid system isolatien valve, CS-485, was leaking. Replaced the valve diaphragm.

M-3 The discharge check valve for 2CD2 diesel fuel oil transfer pump, DF-ll5C, leaked by. Cleaned the discharge check valve for both 2002 and 2C01 fuel oil transfer pumps.

C&I-l Reactor Coolant Pump No. 3 motor air cooler non-essential service water inlet flowmeter, WFA-953, was intermittently failing high.

This caused flow mismatch alarms to be received. The problem was traced to a defective circuit board in WFA-953. After replacement of the circuit board, the transmitter was recalibrated.

C&I-2 ABT-5 Feeder to CRP-3 failed to transfer automatically when lighting transformer 2 "N" was taken out of service for breaker cleaning. The lockout relay was adjusted and the ABT was cycled several times to verify correct operation.

C&I-3 Steam generator No. 21 blowdown radiation monitor, R-19, had no flow indication. Replacement of the flow regulator diaphragm restored the flow to normal. The sight glass was also cleaned.

C&I-4 Turbine-driven auxiliary feedwater pump control bus, distribution cabinet 2 DCN circuit 6, was inoperable. The trip and throttle valve coil was found to have shorted. The defective coil was replaced and the control bus was returned to service with no further incident.

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