ML20071H565

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Final Deficiency Rept Re Remote Shutdown Panels,Initially Reported 810922.All Defective Terminations Will Be Remade According to Constructors Field Stds,Broken Terminal Blocks Will Be Replaced & Screws Retightened by 820315
ML20071H565
Person / Time
Site: Grand Gulf  
Issue date: 02/19/1982
From: Mcgaughy J
MISSISSIPPI POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
10CFR-050.55E, 10CFR-50.55E, AECM-82-66, PDR-81-39, NUDOCS 8203080457
Download: ML20071H565 (3)


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MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi- - ;

EulMilMidd5 P. O. BOX 1640 J ACKSON, MISSISSIPPI 39205 0"

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February 19,}1982 Office of Inspection & Enforcement C

U. S. Nuclear Regulatory Commission Q

Region II f

RECElVED Atlanta, Georgia 30303

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101 darietta Street, N.W.

Suite 3100 MAR 0 51982> $u

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pg yg.m gzw vco1T se Attention:

Mr. J. P. O'Reilly, Director 9

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Dear Mr. O'Reilly:

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SUBJECT:

Grand Gulf Nuclenc Station Units 1 and 2 Docket Nos. 50-416/417 File 0260/15525/15526 PRD-81/39, Final Reprt,

Remote Shutdown Panels AECM-82/66

References:

AECM-81/418, 10/22/81 AECM-82/07, 1/8/82 On September 22, 1981, Mississippi Power & Light Company notified Mr. P.

A. Taylor, of your office, of a Potentially Reportable Deficiency (PRD) at the Grand Gulf Nuclear Station (GGNS) construction site.

The deficiency concerns wiring terminations in the Remote Shutdown Panels supplied by the Reliance Electric Company.

We have completed our investigation and have determined that this deficiency is reportable under the provisions of 10CFR50.55(e) but not under 10CFR21 for Mississippi Power and Light. All details are included in our attached Final Report.

l Yours truly, r

J. P. McGaughy, Jr.

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ATTACHMENT

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See Page 2 8203000457 820219 PDR ADOCK 05000416 S

PDR OFFICIAL COPY D m2.

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Member Middle South Utilities System t

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Attachment to AECM-82/66

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Page 1 of 1 FINAL REPORT FOR PRD-81/39 I.

Description of the Deficiency An inspection of the wiring terminations in the Remote Shutdown Panea.s (IH22-P150 and 1H22-P151) detected numerous loose connections, improper wire crimps, and wire size to terminal lug size discrepancies.

The Remote Shutdown System provides controls for reactor systems needed to carry out the shutdown function from outside the Control Room and bring the reactor to a safe shutdown condition in an orderly manner.

These reactor systems are the Reactor Core Isolation Cooling (RCIC),

Residual Heat Removal (RHR) A & B, Standby Service Water (SSW) A & B, and the Nuclear Boiler (Safety-Relief Valves).

The deficiency is known to affect only Unit 1.

Inspections will be

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performed to determine applicability to Unit 2.

It does not apply to the NSSS vendor.

II.

Analysis of Safety Implications When the panels were originally inspected at the jobsite, it was noted that numerous discrepancies due to poor workmanship existed.

The condition, at this time, was evaluated as not reportable.

However, due to the numerous inspections that were performed during the investigation, the condition of the terminations deteriorated.

Some of the screws loosened further, wires were pulled loose from crimps, and some terminal points became broken.

When the poor workmanship was originally documented, steps were taken to rebuild the panels. This is presently being done. Therefore, MP&L has no way to determine what the " worst case" condition of the panels was, or to evaluate its reportability. Therefore, we have determined that this deficiency is reportable under 10CFR50.55(e)(iii), since an extensive evaluation would be required to establish the adequacy of the component to perform its intended safety function.

III. Corrective Actions Taken All defective terminations will be remade according to our Constructor's field standards.

Broken terminal blocks will be replaced and. loose screws will be retightened. Work should be completed by March 15,1982.

Since this is an isolated occurrence no actions to prevent recurrence are necessary. The Unit 2 remote shutdown panels will be inspected and reworked if necessary i

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- Mr. J. P. O'Reilly AECM-82/66

  • NRC Pags 2 occ:

Mr. N. L. Stampley Mr. ' R. B. McGehee Mr. T. B. Conner Mr. Richard C. DeYoung, Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. B. Taylor South Miss. Electric Power Association P. O. Box 1589 i

Hattiesburg, MS 39401 1

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