ML20071F982

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Monthly Operating Repts for June 1994 for Beaver Valley Power Station
ML20071F982
Person / Time
Site: Beaver Valley
Issue date: 06/30/1994
From: David Jones, Noonan T
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9407110303
Download: ML20071F982 (11)


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sn,eemm.no a u n a u July 8,1994 licaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Gentlemen:

In accordance w; Appendix A,

Technical SpeciGeations, the Monthly Operating Report is submitted for Uni: I and Unit 2 for the month of June,1994.

Respectfully, 4

toned T. P. N(( man x

Division Vice President, Nuclear Operations /

Plant Manager DTJ/mmg linclosures cc: NRC Regional Office King of Prussia, PA s

4 The Nuclear Professionals j

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9407110303 940630 PDR ADCCK 05000334

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1 I

1 NATGATIVE SLIMM1Y OF M0!fI1(LY OPIRATI!G EXPD1IDiCE UNIT 1 JU!TE 1994 June 1

'Iho Unit continued to operate at a nomrul value of 100% output until 1455 hours0.0168 days <br />0.404 hours <br />0.00241 weeks <br />5.536275e-4 months <br /> when a reactor trip occurred due to a turbino ard generator trip cauced by a fault in the Main Transformer.

'1ho Unit was sutxx.quently stabilized in 14cde 3.

June 2 At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> the Unit commenced a cooldown to Modo 5 to facilitato other outago mainterum ard testing durirg replacement of the Main Transfonner.

thio 4 was entered at 2252 houro.

June 3 Modo 5 was entercd at 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br />.

June 4

'lho Unit remaincd in Mode 5 during the remairder of the report through period to facilitate other outage maintenanco and testirg June 30 durirg replacement of the thin Transformer.

t l-l 1

I f

AVERAGE DAILY WIT POWER IREL DOCKET NO.

50-334 UNIT TNPS Unit 1 DATE _ July 5, 1994 00MPLETED BY David T. Jones TELEEHONE (412) 393-7113_

MOfflH June 1994 t%Y AVERAGE DAILY RMER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 503 17 0

2 0

18 0

3 0

19 0

4 0

20 0

5 0

21 0

6 0

22 0

7 0

23 0

8 0

24 0

9 0

25 0

10 0

26 0

11 0

27 0

12 0

28 0

13 0

29 0

14 0

30 0

15 0

31 16 0

D4SIRUC1' IONS On this fonn, list the average daily unit power level NWe-Net for each day in the reportirg Inonth. Conpute to the nearest whole megawatt.

s

't '

OPERATING DATA REPORT DOCKET No.:

50 334

-REPORT DATE:

07/05/94 COMPLETED BY: DAVID T. JONES TELEPil0NEi (412) 393 7553 OPERATING STATUS

1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 1 Notes
2. REPORTING PERIOD: JUNE 1994 3, LICENSED THERMAL POWER (MVt):

2652

4. NAMEPLATE RATING (Cross MVe)-

923

5. DESIGN ELECTRICAL RATING (Net MWe):

835 6, MAX DEPEND.tBLE CAPACITY (Cross MWe):

860

7. MAX. DEPENDABLE CAPACITY (Net MWe):

810 8.

IF CHANGES OCCUR IN CAPACITY RATINGS SINCE IAST REPORT, GIVE REASONS:

9. POWER LEVEL TO WHICH RESYRICTED, IF ANY (Net MWe):

None

10. _ REASONS FOR RESTRICTIONS, IF ANY:

N/A THIS MONTH YEAR TO DATE CUMUIATIVE' 11,110URS IN REPORTING PERIOD: -

720.0 4343,0 159239,0-

12. No, OF llRS. REACTOR WAS CRITICAL:

14.9 3093.1 102624.0 13,_ REACTOR RESERVE SHUTDOWN HOURS:

0,0 0,0 4482.8

14. HOURS CENERATOR WAS ON LINE:

14.9 3079,2

.100622,4 l

15. UNIT. RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0

16. CROSS THERMAL ENERGY GEN. (MVH):

39682.0 7993202.0 241398678.5

17. CROSS ELECT. ENERGY GEN. (MWH):

12980.0 2506540.0 77764063.0

18. NET-ELECTRICAL ENERGY GEN. (MWH):

7270,0 2441100',0 72660620.0 19, UNIT SERVICE FACTOR: (PERCENT) 2.1-

_70,9 65.1 20, UNIT. AVAILABILITY FACTOR:(PERCENT) 2.1

,70,9 65,1

21. UNIT CAPACITY FACTOR (MDC): PCT-

"1. 2 69.4 58,8

22. UNIT CAPACITY' FACTOR (DER): PCT 1.2 67.3 57,1 23.~ UNIT TORCED_ OUTAGE RATE: (PERCENT)

"97.9 29,1 16.3

24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE DATE,AND DURATION.0F_EACH):

THE UNIT IS SCHEDULED TO SHUTDOWN FOR=ITS TENTH REFUELING OUTAGE ON OCTOBER 14. 1994.

THE REFUELING OUTAGE IS SCHEDULED TO LAST FOR 70 DAYS.

=25. IF SHUT DOWN AT END OF REPORT PERIOD,-ESTIMATED-DATE OF STARTUP:

07/08/94 26, UNITS IN TE!I' STATUS (PRIOR TO COMMERCIAL OPERATION):

l-FORECAST ACHIEVED l

INITIAL CRITICALITi N/A-N/A

~ INITIAL" ELECTRICITY

,_, N/A N/A 1

-COMMERCIAL OPERATION N/A N/A

?-

t UNIT SMUTDouuS AhD POWER REDUCTID=S (120%)

Docket ma.

50-334 Unit name Sves Unit #1 Date

tty 5. 1994 Completed By David T.

Jew s REPORT MONTH Jtti 1C94 T eleph one (412) 393-7553 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action to No.

Date Typel (Hours)

Reason 2 Ocwn Reactor 3 Report i Code 4 Code 5 Prevent R ec ur r enc e 7

940601 F

705.1 A

3 1-94-005 EC TRANSF A reactor trip occuired while at 190% output due io a turbine and te. era or trip caused by a fault in t

the Main Transformer. The Main Transformer is being replaced.

I I

1 2

3 4

F-Forced Reason:

Method:

Eahibit F-Instructions for S-Schedul ed A-Equipment Feiture (Emplain) 1-Manuat Preparation of Data Entry Sheets B-Maintenance or Test 2-Manual Scree f or Licensee Event Report (LER) Fite C-Refueling 3-Automatic Scram (huREG0161).

D-Regulatory Restriction 4-Cont'd. f rom Previous Month E-operator Training & License Enam 5-R educ t i on S

F-Administrative 9-Other Exhibit H-Same Source.

G-operationat arror (Emplain)

H-Other (Emplain) v

+--

4 NARRATIVE Sl M ARY OF loffll!LY OPERATIl0 EXPDtIDJCE INIT 2 JUNE 1994 June 1

'Iho Unit continucd to operate at a nomimi value of 100%

mtput until 1455 hours0.0168 days <br />0.404 hours <br />0.00241 weeks <br />5.536275e-4 months <br /> when a reactor trip occurred due to a Reactor Coolant Pump (RCP) bus underfrequency. A fault in the Unit 1 Main Transforner caused a substation disturbanco which resulted in the subsequent RCP bus urderfrequency and reactor trip.

The Unit was subsequently stabilized in Mode 3.

At 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> Source Range Detector N31 was declared inoperable due to a higher than expected count rate.

June 2

'Ihe Unit remined in Mode 3 while preparations were being mde to replace Source Range Detector N31.

June 3

'1he Unit remained in Mode 3 shile replacement of Source Range Detector N31 continucd.

At 1842 hcurs an Auxiliary Foodwater System (AIM) header d.ack valve was declared inoperable due to a leak rate greater than allowed per Technical Specifications.

At 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br /> the Unit comenced a craoldown to Modo 5 to facilitate repairs to the check valvo.

June 4 Modo 4 was entered at 0634 hcurs. Mode 5 was entered at 1844 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.01642e-4 months <br />.

June 5

'Iho Jnit remained in Mode 5 to repair the AIM header check valvo.

Source Range Detector N31 was repla d and returnal to service at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />.

June 6

'Ihe Unit rtmained in Mode 5 to complete repairs to two other through AIM header check valves.

June 9 Juno 10 Following ccmpletion of repairs to the AIM header check

valves, the Unit ccrimenced to heatup and enten-1 Mode 4 at 1257 hour0.0145 days <br />0.349 hours <br />0.00208 weeks <br />4.782885e-4 months <br />'s.

Juno 11 Mode 3 was entered at 0535 hours0.00619 days <br />0.149 hours <br />8.845899e-4 weeks <br />2.035675e-4 months <br />.

Juna 12 Made 2 was entered at 1604 hours0.0186 days <br />0.446 hours <br />0.00265 weeks <br />6.10322e-4 months <br /> and the reactor was taken critical at 1646 hours0.0191 days <br />0.457 hours <br />0.00272 weeks <br />6.26303e-4 months <br />. Mode 1 was entered at 2017 hours0.0233 days <br />0.56 hours <br />0.00333 weeks <br />7.674685e-4 months <br />.

June 13 At 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> the Main Unit Generator was synchronized to the electrical grid and a gradual increase in power was cantienced.

The Unit stabilized at approximately 29% _ output to permit improvements to Steam Generator secxniu,f water chemistry.

.5 4

NARRATIVE Stw3Ri OF 10mILY OPDMTING EXPERIDICE LNIT 2 JUNE 1994 (Continued)

June 14 At 0015 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> an increase to full pcuer was commenced. We Unit achievcd approximtely 100% output at 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />.

June 15 he Unit operated at a ncminal value of 100% output.

June 16 With unusually wam atmcspheric conditions present, a load reduction to approximately 98% output was ccumenced at 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br /> to stabilize condenser hotwn11 conditions. Once corditions in the aandenser hotwell had improved, the Unit returned to full power at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />.

June 17 With continuing warm atmacpheric corditions still present, periodic load reductions to a

minimum output of approximately 97% were ccanenced at 1537 hours0.0178 days <br />0.427 hours <br />0.00254 weeks <br />5.848285e-4 months <br /> to stabilize condenser hotwell conditions.

June 18 Once conditions in the conderwer hotwell had inproved, the Unit was retumed to full power at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />.

With continuing wam atmospheric conditions present later in the

day, periodic load reductions to a minima output of approximately 97% were ocenenced at 1404 hours0.0163 days <br />0.39 hours <br />0.00232 weeks <br />5.34222e-4 months <br /> to stabilize condenser hotwell conditions.

Once conditions in the cc.ndenser hotwell had improved, the. Unit was returned to full power at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />.

June 19 With continuing warm atmospheric conditions still present, periodic load reductions

.to a

mininum output of approximately 97% were ocmnerced at 1336 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.08348e-4 months <br /> to stabilize condenser hotwell conditions.

Once conditions.in the condenser hotwell had inproved, the Unit was returned to full power at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />..

L June 20 With continuing warm atmospheric conditions still present, l

periodic load reductions to a

minimum output of-approximately 98% were ocenenced at 1529 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.817845e-4 months <br /> to stabilize condenser hotwell conditions.

Once conditions in the cordenser hotwell had improved, the Unit was returned to full power at 2056 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.82308e-4 months <br />.

June 21 he Unit. operated at a ncminal value of 100% output, through June 23 June 24 With unusually warm atmospheric conditions present again, a load reduction to approximately 99% output was ocmnenced at-1737 hours to stabilize condenser hotwell conditicris. Once conditions in the cordenser hotwell had improved, the Unit returned to full pcNer at 1958 hours0.0227 days <br />0.544 hours <br />0.00324 weeks <br />7.45019e-4 months <br />, i

i

==

NARRATIVE SLM %RY OF

!OmILY OPERATDC EXPERID4CE UNTT' 2 JUNE 1994 (Continued)

June 25

'Ihe Unit operated tt a ncxnimi value of 100% output for the through rcnninder of the remrt period.

June 30 i

i l

AVERAGE DAILY UlfIT KMER LEVEL DOCKET No.

50-412 U?IIT BVPS Unit 2 DATE July 5, 1994 CmPLETED BY _Qav_id T. Jones TELEPilONE (412) 393-7553 M0flIll June 1994 DAY AVERAGE DAILY FCWIR LEVEL DAY AVN;E DAILY POWER IlV, dL (MWe-Net)

(MWe-Net) 1 50c 17 804 2

0 18 802 3

0 19 809 4

0 20 815 5

0 21 820 6

0 22 8 12 7

0 23 821 8

0 24 818 9

0 25 828 10 0

26 825 11 0

27 826 12 0

28 825 13 89 29 820 14 678 30 827 15 8Q2 31 16 800 INSIRUCTICNS On this fom, list the average daily unit pwer level MWe-Net for each day in the reportirg nonth. Ccrrpute to the nearest stiols megawatt.

A OPERATING DATA REPORT DOCKET NO.:

50-412 REPORT DATE:

07/05/94 i

COMPLETED BY: DAVID T. JONES TELEPHONE:

(412) 39.$-7553 OPEPATING STATUS

1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 2 Notes
2. REPORTING PERIOD: JUNE 1994
3. LICENSED THERMAL POWER (HWt):

2652

4. NAMEPLATE RATING (Gross MWe):

923

5. DESIGN ELECTRICAL RATING (Net MWe):

836

6. uAX. DEPENDABLE CAPACITY (Gross MWe):

870

7. MAX DEPENDABLE CAPACITY (Net MWe):

820 8.

IF CHANGES OCCUR IN CAPACITY RATINGS SINCE LAST REPORT, GIVE REASONS:

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (Net MWe):

None

10. REASGNS FOR RESTRICTIONS, IF ANY:

N/A THIS MONTH YEAR TO DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD:

720.0 4343.0 58022.0

12. NO. OF HRS. REACTOP, WAS CRITICAL:

454.2 4077,2 49407.5

13. REACTOR RESERVE SHUTDOVN HOURS:

0.0 0.0 0.0

14. HOURS GENERATOR WAS ON LINE:

441.0 4064.0 49060.6

15. UNIT RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0

16. GROSS THERMAL ENERGY GEN. (MVH):

1121998.0 10659467.0 120891352.0

17. GROSS ELECT. ENERGY GEN. (MVH):

364016.0 3563877.0 39215882.0

18. NET ELECTRICAL ENERGY GEN. (MWH):

337406.0 3380961.0 37031240,0

19. UNIT SERVICE FACTOR: (PERCENT) 61.3 93.6 84.6
20. UNIT AVAIIABILITY FACTOR:(PERCENT) 61.3 93.6 84.6
21. UNIT CAPACITY FACTOR (MDC): PCT 57.1 94.9 77.3
22. UNIT CAPACITY FACTOR (DER): PCT 56.1 93.1 76.3
23. UNIT FORCED OUTAGE RATE: (PERCENT) 38.8 6.4 3.3
24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE,DATE,AND DURATION OF EACH):
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A

a UN!f SMUYDOWNS AND POWER REDUCT10NS (t201)

Do<ket No.

50-412 Unit Name SVPS Urit 82 Date July S.

1994 Completed By David T.

J ones REPORT MONTH JUNE 1994 Telephone (412) 3o3-7553

_T Met 5sc of Lt6'nsee Cause & Corrective Duration Shutt ng Evsnt System Component Action to No.

Date Typel (Nours)

Reason 2 Down Reactor 3 Report #

C odes Code 5 Prevent R ecurrenc e 1

940601 F

52.6 H

3 2-94-005 EA ELECON A reactor trip occurred white at 100% output due to a Reactor Coolant Pump (RCP) bus underfrequency. A fault in the Unit 1 Main Transformer caused a substation disturbance which resulted in the subsequent RCP bus underf requency and reactor trip.

2 940603 F

226.4 H

9 N/A SD VALVEX The Unit remained shutdown to repair Auxiliary Feedwater System header check valves which were declared inoperable due to teak rates greater than attowed per Technical Specifications.

1 2

3 4

F-Forced Reason:

Method:

Exhibit F-Instructions for S-Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data Entry Sheets B-Maintenance or Test 2-Manual Scram for Licensee Event Report (LER) File C-Refueling 3-Automatic Scram (NUREG0161).

D Regulatory Restriction 4-Cont'd. from Previous Month E-Operator Training & License Exam 5-Reduction 5

F-Administrative 0-Other Exhibit H-Same Source.

G-operational Error (Explain)

H-Other (Explain)

.e

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