ML20071F982
| ML20071F982 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 06/30/1994 |
| From: | David Jones, Noonan T DUQUESNE LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9407110303 | |
| Download: ML20071F982 (11) | |
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sn,eemm.no a u n a u July 8,1994 licaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Gentlemen:
In accordance w; Appendix A,
Technical SpeciGeations, the Monthly Operating Report is submitted for Uni: I and Unit 2 for the month of June,1994.
Respectfully, 4
toned T. P. N(( man x
Division Vice President, Nuclear Operations /
Plant Manager DTJ/mmg linclosures cc: NRC Regional Office King of Prussia, PA s
4 The Nuclear Professionals j
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9407110303 940630 PDR ADCCK 05000334
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1 I
1 NATGATIVE SLIMM1Y OF M0!fI1(LY OPIRATI!G EXPD1IDiCE UNIT 1 JU!TE 1994 June 1
'Iho Unit continued to operate at a nomrul value of 100% output until 1455 hours0.0168 days <br />0.404 hours <br />0.00241 weeks <br />5.536275e-4 months <br /> when a reactor trip occurred due to a turbino ard generator trip cauced by a fault in the Main Transformer.
'1ho Unit was sutxx.quently stabilized in 14cde 3.
June 2 At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> the Unit commenced a cooldown to Modo 5 to facilitato other outago mainterum ard testing durirg replacement of the Main Transfonner.
thio 4 was entered at 2252 houro.
June 3 Modo 5 was entercd at 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br />.
June 4
'lho Unit remaincd in Mode 5 during the remairder of the report through period to facilitate other outage maintenanco and testirg June 30 durirg replacement of the thin Transformer.
t l-l 1
I f
AVERAGE DAILY WIT POWER IREL DOCKET NO.
50-334 UNIT TNPS Unit 1 DATE _ July 5, 1994 00MPLETED BY David T. Jones TELEEHONE (412) 393-7113_
MOfflH June 1994 t%Y AVERAGE DAILY RMER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 503 17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 0
14 0
30 0
15 0
31 16 0
D4SIRUC1' IONS On this fonn, list the average daily unit power level NWe-Net for each day in the reportirg Inonth. Conpute to the nearest whole megawatt.
s
't '
OPERATING DATA REPORT DOCKET No.:
50 334
-REPORT DATE:
07/05/94 COMPLETED BY: DAVID T. JONES TELEPil0NEi (412) 393 7553 OPERATING STATUS
- 1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 1 Notes
- 2. REPORTING PERIOD: JUNE 1994 3, LICENSED THERMAL POWER (MVt):
2652
- 4. NAMEPLATE RATING (Cross MVe)-
923
- 5. DESIGN ELECTRICAL RATING (Net MWe):
835 6, MAX DEPEND.tBLE CAPACITY (Cross MWe):
860
- 7. MAX. DEPENDABLE CAPACITY (Net MWe):
810 8.
IF CHANGES OCCUR IN CAPACITY RATINGS SINCE IAST REPORT, GIVE REASONS:
- 9. POWER LEVEL TO WHICH RESYRICTED, IF ANY (Net MWe):
None
- 10. _ REASONS FOR RESTRICTIONS, IF ANY:
N/A THIS MONTH YEAR TO DATE CUMUIATIVE' 11,110URS IN REPORTING PERIOD: -
720.0 4343,0 159239,0-
- 12. No, OF llRS. REACTOR WAS CRITICAL:
14.9 3093.1 102624.0 13,_ REACTOR RESERVE SHUTDOWN HOURS:
0,0 0,0 4482.8
- 14. HOURS CENERATOR WAS ON LINE:
14.9 3079,2
.100622,4 l
- 15. UNIT. RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 16. CROSS THERMAL ENERGY GEN. (MVH):
39682.0 7993202.0 241398678.5
- 17. CROSS ELECT. ENERGY GEN. (MWH):
12980.0 2506540.0 77764063.0
- 18. NET-ELECTRICAL ENERGY GEN. (MWH):
7270,0 2441100',0 72660620.0 19, UNIT SERVICE FACTOR: (PERCENT) 2.1-
_70,9 65.1 20, UNIT. AVAILABILITY FACTOR:(PERCENT) 2.1
,70,9 65,1
- 21. UNIT CAPACITY FACTOR (MDC): PCT-
"1. 2 69.4 58,8
- 22. UNIT CAPACITY' FACTOR (DER): PCT 1.2 67.3 57,1 23.~ UNIT TORCED_ OUTAGE RATE: (PERCENT)
"97.9 29,1 16.3
- 24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE DATE,AND DURATION.0F_EACH):
THE UNIT IS SCHEDULED TO SHUTDOWN FOR=ITS TENTH REFUELING OUTAGE ON OCTOBER 14. 1994.
THE REFUELING OUTAGE IS SCHEDULED TO LAST FOR 70 DAYS.
=25. IF SHUT DOWN AT END OF REPORT PERIOD,-ESTIMATED-DATE OF STARTUP:
07/08/94 26, UNITS IN TE!I' STATUS (PRIOR TO COMMERCIAL OPERATION):
l-FORECAST ACHIEVED l
INITIAL CRITICALITi N/A-N/A
~ INITIAL" ELECTRICITY
,_, N/A N/A 1
-COMMERCIAL OPERATION N/A N/A
?-
t UNIT SMUTDouuS AhD POWER REDUCTID=S (120%)
Docket ma.
50-334 Unit name Sves Unit #1 Date
- tty 5. 1994 Completed By David T.
Jew s REPORT MONTH Jtti 1C94 T eleph one (412) 393-7553 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action to No.
Date Typel (Hours)
Reason 2 Ocwn Reactor 3 Report i Code 4 Code 5 Prevent R ec ur r enc e 7
940601 F
705.1 A
3 1-94-005 EC TRANSF A reactor trip occuired while at 190% output due io a turbine and te. era or trip caused by a fault in t
the Main Transformer. The Main Transformer is being replaced.
I I
1 2
3 4
F-Forced Reason:
Method:
Eahibit F-Instructions for S-Schedul ed A-Equipment Feiture (Emplain) 1-Manuat Preparation of Data Entry Sheets B-Maintenance or Test 2-Manual Scree f or Licensee Event Report (LER) Fite C-Refueling 3-Automatic Scram (huREG0161).
D-Regulatory Restriction 4-Cont'd. f rom Previous Month E-operator Training & License Enam 5-R educ t i on S
F-Administrative 9-Other Exhibit H-Same Source.
G-operationat arror (Emplain)
H-Other (Emplain) v
+--
4 NARRATIVE Sl M ARY OF loffll!LY OPERATIl0 EXPDtIDJCE INIT 2 JUNE 1994 June 1
'Iho Unit continucd to operate at a nomimi value of 100%
mtput until 1455 hours0.0168 days <br />0.404 hours <br />0.00241 weeks <br />5.536275e-4 months <br /> when a reactor trip occurred due to a Reactor Coolant Pump (RCP) bus underfrequency. A fault in the Unit 1 Main Transforner caused a substation disturbanco which resulted in the subsequent RCP bus urderfrequency and reactor trip.
The Unit was subsequently stabilized in Mode 3.
At 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> Source Range Detector N31 was declared inoperable due to a higher than expected count rate.
June 2
'Ihe Unit remined in Mode 3 while preparations were being mde to replace Source Range Detector N31.
June 3
'1he Unit remained in Mode 3 shile replacement of Source Range Detector N31 continucd.
At 1842 hcurs an Auxiliary Foodwater System (AIM) header d.ack valve was declared inoperable due to a leak rate greater than allowed per Technical Specifications.
At 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br /> the Unit comenced a craoldown to Modo 5 to facilitate repairs to the check valvo.
June 4 Modo 4 was entered at 0634 hcurs. Mode 5 was entered at 1844 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.01642e-4 months <br />.
June 5
'Iho Jnit remained in Mode 5 to repair the AIM header check valvo.
Source Range Detector N31 was repla d and returnal to service at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />.
June 6
'Ihe Unit rtmained in Mode 5 to complete repairs to two other through AIM header check valves.
June 9 Juno 10 Following ccmpletion of repairs to the AIM header check
- valves, the Unit ccrimenced to heatup and enten-1 Mode 4 at 1257 hour0.0145 days <br />0.349 hours <br />0.00208 weeks <br />4.782885e-4 months <br />'s.
Juno 11 Mode 3 was entered at 0535 hours0.00619 days <br />0.149 hours <br />8.845899e-4 weeks <br />2.035675e-4 months <br />.
Juna 12 Made 2 was entered at 1604 hours0.0186 days <br />0.446 hours <br />0.00265 weeks <br />6.10322e-4 months <br /> and the reactor was taken critical at 1646 hours0.0191 days <br />0.457 hours <br />0.00272 weeks <br />6.26303e-4 months <br />. Mode 1 was entered at 2017 hours0.0233 days <br />0.56 hours <br />0.00333 weeks <br />7.674685e-4 months <br />.
June 13 At 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> the Main Unit Generator was synchronized to the electrical grid and a gradual increase in power was cantienced.
The Unit stabilized at approximately 29% _ output to permit improvements to Steam Generator secxniu,f water chemistry.
.5 4
NARRATIVE Stw3Ri OF 10mILY OPDMTING EXPERIDICE LNIT 2 JUNE 1994 (Continued)
June 14 At 0015 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> an increase to full pcuer was commenced. We Unit achievcd approximtely 100% output at 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />.
June 15 he Unit operated at a ncminal value of 100% output.
June 16 With unusually wam atmcspheric conditions present, a load reduction to approximately 98% output was ccumenced at 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br /> to stabilize condenser hotwn11 conditions. Once corditions in the aandenser hotwell had improved, the Unit returned to full power at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />.
June 17 With continuing warm atmacpheric corditions still present, periodic load reductions to a
minimum output of approximately 97% were ccanenced at 1537 hours0.0178 days <br />0.427 hours <br />0.00254 weeks <br />5.848285e-4 months <br /> to stabilize condenser hotwell conditions.
June 18 Once conditions in the conderwer hotwell had inproved, the Unit was retumed to full power at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />.
With continuing wam atmospheric conditions present later in the
- day, periodic load reductions to a minima output of approximately 97% were ocenenced at 1404 hours0.0163 days <br />0.39 hours <br />0.00232 weeks <br />5.34222e-4 months <br /> to stabilize condenser hotwell conditions.
Once conditions in the cc.ndenser hotwell had improved, the. Unit was returned to full power at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />.
June 19 With continuing warm atmospheric conditions still present, periodic load reductions
.to a
mininum output of approximately 97% were ocmnerced at 1336 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.08348e-4 months <br /> to stabilize condenser hotwell conditions.
Once conditions.in the condenser hotwell had inproved, the Unit was returned to full power at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />..
L June 20 With continuing warm atmospheric conditions still present, l
periodic load reductions to a
minimum output of-approximately 98% were ocenenced at 1529 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.817845e-4 months <br /> to stabilize condenser hotwell conditions.
Once conditions in the cordenser hotwell had improved, the Unit was returned to full power at 2056 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.82308e-4 months <br />.
June 21 he Unit. operated at a ncminal value of 100% output, through June 23 June 24 With unusually warm atmospheric conditions present again, a load reduction to approximately 99% output was ocmnenced at-1737 hours to stabilize condenser hotwell conditicris. Once conditions in the cordenser hotwell had improved, the Unit returned to full pcNer at 1958 hours0.0227 days <br />0.544 hours <br />0.00324 weeks <br />7.45019e-4 months <br />, i
i
==
NARRATIVE SLM %RY OF
!OmILY OPERATDC EXPERID4CE UNTT' 2 JUNE 1994 (Continued)
June 25
'Ihe Unit operated tt a ncxnimi value of 100% output for the through rcnninder of the remrt period.
June 30 i
i l
AVERAGE DAILY UlfIT KMER LEVEL DOCKET No.
50-412 U?IIT BVPS Unit 2 DATE July 5, 1994 CmPLETED BY _Qav_id T. Jones TELEPilONE (412) 393-7553 M0flIll June 1994 DAY AVERAGE DAILY FCWIR LEVEL DAY AVN;E DAILY POWER IlV, dL (MWe-Net)
(MWe-Net) 1 50c 17 804 2
0 18 802 3
0 19 809 4
0 20 815 5
0 21 820 6
0 22 8 12 7
0 23 821 8
0 24 818 9
0 25 828 10 0
26 825 11 0
27 826 12 0
28 825 13 89 29 820 14 678 30 827 15 8Q2 31 16 800 INSIRUCTICNS On this fom, list the average daily unit pwer level MWe-Net for each day in the reportirg nonth. Ccrrpute to the nearest stiols megawatt.
A OPERATING DATA REPORT DOCKET NO.:
50-412 REPORT DATE:
07/05/94 i
COMPLETED BY: DAVID T. JONES TELEPHONE:
(412) 39.$-7553 OPEPATING STATUS
- 1. UNIT NAME: BEAVER VALLEY POWER STATION, UNIT 2 Notes
- 2. REPORTING PERIOD: JUNE 1994
- 3. LICENSED THERMAL POWER (HWt):
2652
- 4. NAMEPLATE RATING (Gross MWe):
923
- 5. DESIGN ELECTRICAL RATING (Net MWe):
836
- 6. uAX. DEPENDABLE CAPACITY (Gross MWe):
870
- 7. MAX DEPENDABLE CAPACITY (Net MWe):
820 8.
IF CHANGES OCCUR IN CAPACITY RATINGS SINCE LAST REPORT, GIVE REASONS:
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (Net MWe):
None
- 10. REASGNS FOR RESTRICTIONS, IF ANY:
N/A THIS MONTH YEAR TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD:
720.0 4343.0 58022.0
- 12. NO. OF HRS. REACTOP, WAS CRITICAL:
454.2 4077,2 49407.5
- 13. REACTOR RESERVE SHUTDOVN HOURS:
0.0 0.0 0.0
- 14. HOURS GENERATOR WAS ON LINE:
441.0 4064.0 49060.6
- 15. UNIT RESERVE SHUTDOWN HOURS:
0.0 0.0 0.0
- 16. GROSS THERMAL ENERGY GEN. (MVH):
1121998.0 10659467.0 120891352.0
- 17. GROSS ELECT. ENERGY GEN. (MVH):
364016.0 3563877.0 39215882.0
- 18. NET ELECTRICAL ENERGY GEN. (MWH):
337406.0 3380961.0 37031240,0
- 19. UNIT SERVICE FACTOR: (PERCENT) 61.3 93.6 84.6
- 20. UNIT AVAIIABILITY FACTOR:(PERCENT) 61.3 93.6 84.6
- 22. UNIT CAPACITY FACTOR (DER): PCT 56.1 93.1 76.3
- 23. UNIT FORCED OUTAGE RATE: (PERCENT) 38.8 6.4 3.3
- 24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE,DATE,AND DURATION OF EACH):
- 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A
a UN!f SMUYDOWNS AND POWER REDUCT10NS (t201)
Do<ket No.
50-412 Unit Name SVPS Urit 82 Date July S.
1994 Completed By David T.
J ones REPORT MONTH JUNE 1994 Telephone (412) 3o3-7553
_T Met 5sc of Lt6'nsee Cause & Corrective Duration Shutt ng Evsnt System Component Action to No.
Date Typel (Nours)
Reason 2 Down Reactor 3 Report #
C odes Code 5 Prevent R ecurrenc e 1
940601 F
52.6 H
3 2-94-005 EA ELECON A reactor trip occurred white at 100% output due to a Reactor Coolant Pump (RCP) bus underfrequency. A fault in the Unit 1 Main Transformer caused a substation disturbance which resulted in the subsequent RCP bus underf requency and reactor trip.
2 940603 F
226.4 H
9 N/A SD VALVEX The Unit remained shutdown to repair Auxiliary Feedwater System header check valves which were declared inoperable due to teak rates greater than attowed per Technical Specifications.
1 2
3 4
F-Forced Reason:
Method:
Exhibit F-Instructions for S-Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data Entry Sheets B-Maintenance or Test 2-Manual Scram for Licensee Event Report (LER) File C-Refueling 3-Automatic Scram (NUREG0161).
D Regulatory Restriction 4-Cont'd. from Previous Month E-Operator Training & License Exam 5-Reduction 5
F-Administrative 0-Other Exhibit H-Same Source.
G-operational Error (Explain)
H-Other (Explain)
.e
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