ML20071C785

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Monthly Operating Repts for Dec 1982
ML20071C785
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 01/14/1983
From: Mayweather L
SOUTHERN CALIFORNIA EDISON CO.
To:
Shared Package
ML20071C784 List:
References
NUDOCS 8303080097
Download: ML20071C785 (10)


Text

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'I NRC MONTHLY OPERATING REPORT 50-361 DOCKET NO DATE 14 danuary 1983 COMPLETED BY L. Mayweather TELEPHOSE 714/4 W -7700 ExtS6223 OPERATING STATUS

1. Uni Name:

San Onofre Nuclear Generatina Station Unit 2 1 December 1982 through 31 December 1982

2. Reporting Period:
3. Licensed Thermal Power (MWti:

lI27

4. Nameplate Rating (Gross MWe):

1 OU

5. Design Electrical Rating (Net MWe):

1127

6. Maximum Dependable Capacity (Gross MWe):
7. Mnimum Dependable Capwity (Net MWe): 1087
8. If Changes Occur in Capacity Ratings (items Number 3 Through Since Last Report.Give Reasons:
9. Power Lesel To Which Restricted.lf Any(Net MWe):
10. Reasons For Kestrictions. If Any: g This Month Yr. to.Date Cumulative 744 7,656 7,656
11. Hours in Reporting Perici 297 1,/62 1,762
12. Number Of Hours Reactor has Critical
13. Resetor Reserse Shutdown Hour, 0 0 0 269 824 824
14. IMers Generator On-Line 0 0 0
15. Unit Reserve Shutdown Hours 474,700 964,700 964,700
16. Gross Thermal Energy Genersted (MWH) 128,600 195,000 195,000 17 Gross Electrical Energy Generated (MWH) 108,620 126,020 126,020 lb. Net Electrical Energy Generated iMWill NA NA NA
19. Unit Sersice Factor fiA NA NA
20. Unit Availability Factor NA NA NA
21. Unit Capacity Factor (Using MDC Net t NA NA NA
22. Unit Capacity Factor (Using DER Net)

NA HA na

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Nest 6 Months (Type.Date,and Duration of Each t:

None

25. If Shat Down At End Of Report Period. Estimated Date of Startuis.
26. Unin in Test Status (Prior o Commercial Operatior 1: Forecast Achieved 7/17/82 7/26/82 INITI AL CRITICALITY INITI4L ELECTRICITY 9/82 9/20/82 COMMERCIAL OPER ATION Under review 8303OIiOO97 830114 PDR ADOCK 05000361 PDR R

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' AVER AGL DAILY UNIT POWER LEVEL i

DOCKET NO.

~0 SONGS-2 WIT l 4 January 1983 DATE COMPLETED BY L. Mayweather TELEPHONE 714/492-7700 Ext. 56223 DECEMBER 1982 MONTH DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (Mhe Net) IMwe Neti 3

245 g7 0 2 447 18 g 3 440 l, 0 4 430 20 0 5 458 0

6 442 0 22 7 454 0 23 8 437 24 0 9 446 25 0 10 463 0 26 11 433 0 2,

12 199 28 0 i3 0 0 29 0 0 14 30 is 0 31 0

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DOCKET NO.

50 -361 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME DUM'D - d DATE 1 4 .la nua ry 1983 REPORT MON Hf DECEMBER 1982 COMPLETED BY I Maywpather TELEPHONE 71a/dQ7 77nn Ext. 56223

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.E s E 1.icensee Event

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93 Cause A Correceive Action to

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}L Pievens Recurrence 5

1 12/12/82 F 447 A 3 82-168 IA INSTRU Trip on high LPD/ low DNBR signal caused by faulty reed switch. Faulty reed switch replaced. Unit remained

, down for repair of RCP seals and turbine valves.

I 2 1 4 I Forced Reason : Method:

S Scheduled 1.shibii F . instructions A 1:quipment Failure (Explain) 1 -Manual for Preparation or DJfJ R. Maintenance or Test '

. . Manual Scram.

r Refueling Entr> Sheets for Iicensee

4. Automatic Scram. lient Repnet Il 1 MlI ile (NI!RI G D-Regniator) Restriction 4-Olher (E xplam l 0161) 1 -Opeutor iraining & l.it ense I.xanonation F. Administ rative 5 G-Oguatinnal I nor (liplain) ITinbiell Sanw S.imce ll Olhee (I xplam)

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SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH 6

50-361 DOCKET NO. _

SONGS - 2 UNIT 14 January 1983 DATE COMPLETED BY L. Mayweather TELEPHONE 714/492-7700 Ext.56223 December 1 0001 Unit in Mode 1 and power is approximately 12%.

December 1 0333 Synchronized generator and applied block load of 100 MWe gross.

i December 1 0345 Raised reactor power to 25%.

December 1 0425 Raised turbine load to 170 MWe gross.

December l 1120 Reactor power at 50% and turbine load approximately 500 MWe gross. Testing at 50% power began.

December 12 0801 Reactor trip caused by high LPD/ low DNBR signal resulting from faulty reed switch. Cooldown to Mode 5 in progress for RCP seal and turbine valve work.

December 13 0830 Entered Mode 4.

Decemb.er 13 1325 Entered Mode 5.

December 27 2130 Entered Mode 4. All outage activities completed.

December 29 1530 Entered Mode 3.

December 30 2240 Entered Mode 2.

December 30 2255 Reactor critical.

December 31 0200 Reactor power at 1%.

December 31 2359 Reactor power at 1% and preparations to raise power to 50% for resumption of testing.

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REFUELING INFORMATION DOCKET ic 50-361 UNIT SONGS - 2 DATE 14 January 1983 COMPLETED BYL. Hayweather TELEPHONE 714/492-7700 Ext. 56223

1. Scheduled date for next refueling shutdown.

Not yet detcrmined.

2. Scheduled date for restart following refueling.

Not yet determined.

3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

Not yet determined.

What will these be?

Not yet determined.

4. Scheduled date for submitting proposed licensing action and supporting information.

Not yet determined.

5. Important licensing considerations associated with refueling, e.g.

new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.

, Not yet determined.

6. The number of fuel assemblies.

a) In the core b) In the spent fuel storage pool.

7. Licensed spent fuel storage capacity. ann Intended change in spent fuel storage capacity. NA
8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity. NA

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NRC MONTHLY OPERATING REPORT DOCKET NO. 50-362 DATE 14 January 1983 COMPLETED BY L. Mayweather TELEPHOSE 714/492-7700 Ext. 56223 OPERATING ST A TUS

1. Unit Name:

San Onofre Nuclear Generatina Station, Unit 3 1 December 1982 through 31 December,1982.

2. Reporting Period:

169.5

3. Licensed Thermal Power (MWt):

I32#

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe): 10R7
6. Maximum Dependable Capacity (Gross MWe): 1"
7. Maximum Dependable Capaity (Net MWe):

N

8. If Qanges Occur in Capacity Ratings (Items Number Thmugh 7)Since Last Report.Gi+e Reasons:

NA

9. Power Level To Which Restricted,if Any (Net MWeJ:
10. Reawns for Restrictions.lf Any: Ifnit le etill in initial etartun_p.haen_nf tactinn. _

This Month Yr..to Date Cumulative 744 1128 1128 I1. Hours in Reporting Period 0 0 0

12. Number Of Hours Reactor was Critical 0 0 0 1.1. Resctor Reserve Shutdown Hours 0 0 0
14. Hours Generator On.Line 0 0 0
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 0 O n 17 Gross Electrical Energy Generated (MWH) 0 0 0 Ili. Net Electrical Energy Generated (MWH)

NA NA NA

19. Unit Senice Factor NA NA NA

! 20. Unit Asailability Factor NA NA NA

21. Unit Capacity Factor (Using MDC Net)

NA NA NA 2.' Unit Capacity Factor (Using DER Net) NA NA NA

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Nest 6 Months (Type. Date.and Duration of Each//0NE l

NA

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

1 26. Units in Test Status (Prior o Commercial Operation): Forecast Achiewd Under Review i INITI AL CRITICALITY Under Review INITI AL ELECTRICITY

' Under Review COMMERCI AL OPER ATION i

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AVER 4GE DAILY UNIT POWER LEVEL 50-362 DOCKET NO.

UNIT SONGS - 3 DATE I'4 January 1982 COMPLETED gy L. Mayweather TELEPHONE 714/492-7700 Ext. 56223 MONTH DFFFMRFR 1982 DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE D AILY POWER LEVEL (MWe Neti IMWe Net)

I 17 0

2 IN 0 0

3 19 0

0 0 4 20 0 .

0 5 23 0

22 0

0 0 7 23 <

8 0 0 24 0 0 9 25 10 0 26 0 0

11 27 0 12 0 0 l 28 0

i 33 29 0

i 14 0 0 1 30 15 0 0 s 31 b

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50-362 UNIT SHUTDOWNS AND POWER RFDUCTIONS

' DOCKET UNIT NAMENO. W"" - A "

DATE l9 January IyuJ ECEMBER 1982 COMFt_ETED BY L. Mayweather

' MPORT MONTH TELEPHONE 714/492-7700 Ext. 56223

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53 E [* 5 - RePo't " y' Prevent Recurrente 6

NA NA NA NA NA NA NA NA NA i

I 2 1 4 I Torced Reaven : Method I.shibit F. Insienctions S Scheduleti A I:qmpment Failure (Explain) 1. Manual for Prepar.ition of Da.ta R. Maintenance or Test 2-Manual Scram. Entry Sheets for I Acusee l' Rcheeling 4 Automate S r.im. I went Repois el I Ril etc INI!RI G D.Regulatoss Resivittion 4-01her li'splaml 01611

  • I -Opci.itos Traming & l.a eme I sammation F- Adnunnt rative 5 G-Opes. stomal I s tor li' uplain ! I sInbit il S.eme Smite ll Olhee ll splaint

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SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO. 50-362 UNIT SONGS - 3 DATE COMPLETED BY L. Mayweather TELEPHONE 714/492-7700 Ext.56223

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December 1 0001 Unit in Mode 5. Post core hot functional testing in progress.

December 9 1325 Completed venting reactor coolant pump seals.

December 10 0015 Completed venting reactor head.

December 10 2230 Completed main generdtor leak test.

December 12 2200 Completed filling steam generators to 95% (narrow range).

December 31 2359 Unit in Mode 5,180 F. Preparations for Mode 4 entry in progress.

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REFUELING INFORMATION DOCKET NO. 50-362 UNIT SONGS - 3 DATE 14 January 1983 COMPLETED BY L. Mayweather TELEPHONE 714/492-7700 Ext. 56223,

1. Scheduled date for next refueling shutdown.

Not yet determined.

2. Scheduled date for restart following refueling.

Not yet determined.

3. Will refueling or resumption of operation thereafter require a Technical Specificetion change or other license amendment?

Not yet determined.

What will these be?

Not yet detennined.

4. Scheduled date fry submitting proposed licensing action and supporting information.

Not yet de'termined.

5. Important licensing considerations associated with refueling, e.g.

new or different fuel design or supplier, unreviewed design or perfgrmance analysis methods, significant changes in fuel design, new ope. rating procedures.

4, Not yet determined.

6. The number of fuel assemblies.

a) In the core 217 b) In-the spent fuel storage pool. , 0

7. Licensed spent fuel storage capacity. 800 Intended change in spent fuel storage capacity. NA
8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.

NA n.ot : n .. . .n.

_ _ . , . .