ML20070F050
| ML20070F050 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 12/02/1982 |
| From: | Gillett W INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | |
| Shared Package | |
| ML20070F022 | List: |
| References | |
| NUDOCS 8212200065 | |
| Download: ML20070F050 (6) | |
Text
.___ __.
CPER.tT NC DATA REPORT 50-316 DCC:CTNO.
DATI 17-2-82 W.T. Gillett Co.v:'.t---- - v.
T" :HCNg 616 aAs_sq01 C???rNC 5"ATUS Donald C. Cook
?
Nous
- 1. Uni:Ns==:
November-1982
.,. R
- o.,- 3.a.= :
r 3391
- 3. U---w h---! ?:wer (5tw:;:
1133
- 4. N==e:h:: ?-M (C:::s 51we):
1100
- 3. Desig: E===i=! R:==;(Nec 51We):
III8
- 6. V-".== Depted.his C27::i:7 (Cr:ss 51Fe):
1OS?
- 7. 512 m.-, C :::d:h!: t -- =:7 (Net 31we;:
S. If F-- ;rs C:
is C:pz=i y h:is,s (1:=:s Nc=her 3 Thr q.h 7) SI :: Lu: Reper:. Cive Re:s= s:
- 9. hower Leve! To p.hh R:s=:= d.If Any (N:: SIWE):
- 10. R=sens.Ter R=:.-.=i=:s.1f Asy:
This 31or.:h Yr.<o.Ca::
Cu=u!::iw 720 8016 43,080
- 11. H:::s I: R:;:r. :; ?=i:d 481 5 6.788.4 30.813.4 11 Nu=her Cf H:c:s R--- r'*:s Cri==.1
- 13. Rc=:r R=se:se sh::d:wn E.=2 1.:. H:::s Cc---* r C=.U:,
481.5 6,740.7
?9,461.7
- 15. U:i: R.-se-ve 5' =:d=w H:==
- 16. Cr:ss h===.1 E==::y Cen:=::d OtwH) 1.575,311
??.183,410 96,P64.231
- 17. Gr:ss Ee=.=:! E== ;7 Gent =::d G.tWH) 519.680 __.
7.?40.770 30.057.470
- 13. N : E :=i=!I:=r;y Cecen::d C.;W -a 501,917 6,995,651 Po 839.7o?
66.9 84.1 73.9
- 19. U::i: Se:Ti=.:.=:r O. U:1: Av:il:hiH.r.:::::r 66.9 84.1 73.4
- 21. Uni: C::::d:7 f::::r(Usin; >!OC Net) 64.4 80.6 69.S 63.4.
/9.3 68./
- 2. Uni: C. :::ity. :=:r (Usis: CIR Ne:1 0
13.3 14.0
- 23. Uni:.:=rer:f C:::ge R::e
- 24. Sh::do Ans Schedu!:d Over Ner.: 5 31cc:hs (Type. 0:::. :::10 :::i== of I::h1:
- 25. If Sh:: Down A: Ind Cf ?. ; :: ?:-icd. E:ti==:ed D te c 5::-::::
.25. Units != Tes: 5::::s P::=r to C r====i:i C;::::ica s:
Foreest Accieved INIT'.A1. CRIT *CA UTY IN TIA u..,_,-..,..,,..,
C 0... :.:.,.,..,,. A...
.. a
.w.
tut;;g 0$hof{
PDR l
i
..-_,_.._,.._,.._,,___.__._,_,,~..,_._m_
l
AVERAGE DAILY UNIT POWER LEVEL 00CKET NO. 50-316 UNIT 2
DATE 12-2-82 CCMPLETED BY A. Might TELEPHONE 616-465-5901-j MONTH November '1982 DAY AVERAGE DAILY PCWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)
(MWe-Net) 1 1080 17 1084 2
1080 18 1083 3
1080 19 958 4
1086 20 455 5
1085 i
21 5
6 1088 22 7
1086 23 I
a 1085 24
~
g 1082 25 10 1072 25
~
11 1077 27 12 1083 28 13 1087 29 14 1086 30 15 1087 31 15 1087 INSTRUCTIONS On this femat list the average daily unit pcwer level in MWe-Net for each day in the repo r.ing month.
Ccmoute to the nearest whole megawatt.
50-316 II llNil Silllll> OWNS AND POWI.it itt lillC~llONS I Ij T2;T4.ook - Unit 2 D.C.C r
~-82 nA si: T.A7Svensson COMPl l IEp ity November,1982 gj g,qgg ill Polt i MONill PAGE 1 of 1 I
a.
t I i. cnsc e
[j,,
h:,
yE
'(
.?, !" f; ranse a r.e.c uve No luie
<f, T. g 3sa 1 ve.
ay
<>g A. i....i i.,
$6 g2 af, 6 Itrgunt #
tN U U
Psevcsig l(conscia.c P
6 119 821121 S
238.5 B&C 1
N.A.
ZZ ZZZZZZ The Unit was removed from service at 0127 hours0.00147 days <br />0.0353 hours <br />2.099868e-4 weeks <br />4.83235e-5 months <br /> on 821121 for scheduled Cycle III - IV refueling / maintenance outage.
Several major TMI Action Plan related design changes are also being installed. The power reduction was started at 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> on 821119 at 2% per hour when a marked increase in the calculated S.G. primary to secondary leak rate was experienced.
At the end of the month the Unit was in Cold Shutdown Mode 5 with the RCS at half loop.
i
.I l
l-l n cil itcason,
kica hn.1:
1 minius G. Inssinisi.wis S. N l cilutc.l A l.;nipnics.: 1.nine e ll. mplain) 1 Manual ins Pacpasan u of flata 11 Maintonatwc ns 'Ic>I
.! Manual S saen.
I nasy $hces den i kcuscc C-Itclucting i Antonuth S s.sen i sen Itcp.no il l'lt i i alc lNiliti G-li Itet "Id'"'F 3(CS8' k l8'"'
-l Oihes ll aplanil 016ll l Opceatoi leae.iing a li.cnw I maininanon 5
1: Aihnans>tiaerec isint.itI S2.nc Snn c G Opceanonal I es.n li splanin C#f//l 11 Olhee il splini)
UNIT SMUTDOWNS AND POWER REDUCTIONS LNSTRUC IONS Th:s report s culd desen:e 211 pan: inutic*ns : nn; me a n::r:an:e At:h the :aie ac:estmg an :he re: ort for n re: ort penoc. L. 2ddinan. ;t saccid be de soar:e ciex;!2n.
!f n:e; cry 4 tust te used. sunpi> er:ei :mtnen:s.
anon of s:pn 2nt dips a ase:2ge ;cwer ; eve:s. na:n s:p-
.a,.t r.4.....cn,n.e.,. t..yet (3. 2:e. a an -v..e.u..e.
Reference :ne app:,ast!e
.a LICENSEE EVENT REPORT :.
- n aerne dady power :evei f:r me ;te:etng 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />)
" E C'*W 0.CO2U' C8 7 "!2010i 3 0' Jut 2P Of FC * *'
780WEC 3-W8' C*f3 '0* 72M3 * "!1822idU' P
(
4:o.!d :: :::ed. even mea;n te an:: =2y :ct have :een saut cown ::=ple:eivl For suen :e =nens :n ;ower lesel.
report num:e:. ce=:ren:e ::de and report :);e; or me ::ve tne dunnon meuld :e 'ds:ed u : era. the memod airedu:ncn pan des:panon u des = bed 3 Item 0 or, Insances u, t Pn:2:2non of Data Entiv Shee:r. for Laensee Event Re:ct:
snould be 'ds:ed as 4 iCdert. 2nd me Cause 2nd C : :enve A:ncn t ? even: Re:unen:e ::!;=n should ex;120.. The (LER) Fde tNUREC41:U. Das mformanon may act a Csuse 2.
b.,
. Ve 4..,n.o p..,e..
..n:.
- .Lur.3
- n:meda:eiy eMdent for 20 sui.h shu Co*ns. Ol' oufse. sinEf w
A a
t 7;:tner m'estgauCn mav De req"::e2 to asee :212 enetnef wr
.e..se to rance any eede ex,.2:2t;cn.o...:ty If the Qu:2{t Jr mou: 4 n
o g
net 2 re:orta:le c::urren:e was.nvolved.)
4ese a.e m...e
...s:...s.31... ou..,;. a.t,-cw e..gs......,n.
- ower
- ec=non wtil not resuit ;n 2 repor:2:te c:=r en:.
the ;csinve :ndt:21:Cn of this lack of : rreist:or: ihcuid :e
%. s c.it a sn a : a, m....J.e se+ e..,...
.N '
t ter ass: ped :a enn shutd:*n or s:psd 2nt redue'ucn:n power noted as not 2;;!i:2bie iN, A,.
J for m2t m.endar year. When a sautscwn or s:pd:2nt power SYSTEM CODE. The system in wh= :he autsp or ec*er reduence begs = cne re:crt pen:d and +nds a 2nceer.
recuenen ar:;:nsted mould be acted :v tne t*o d;p ::ce of an ent:v maul.:e ma:e :or :cta report :enods to :e sure
'*'"" O 'I"5'""C"*I"' D'?"#2"0" ' U2" e*'O * **'
a s...,,wns a s. '...... ow e. ~.. -"....s 2:e. e;crie.d..
a 6*r : se Eve-' 'b o-f L*R) Fe 6LREC4 ' 51) m
- ~
"e Latd 2 ::u: n22 n:neve: ns ::::: pcwe: une:2::en. no num.
ter snould te us:pec :s e2:n en:o.
Sys: ems :h2t to not 6: 2ny exisung =de mouic :e des:ps.
- e: XX. The oce ZZ saculd te use: fct mose events waere l
DATE. Das niumn 2:uid md:cs:e de date af de start 2 sys:em.s not appiu23;e.
af es:. snatican er sign.;d:2n: ;ower redanen. Repcrt i
- s ye2:. menth, ed :2t A;ps: la.10
- cud :e re:cred COM.*CSENT CODE. Seie:::ne mos: 2:;r::na:e.cm;cnent i
u CSla. When a snu:2:*n or ng a:.=t ;cwer recun:n i::= Ex.ata [. Ins::u:nons fer ?:::2:2nce of Data En:.7
~
1 begs = ene re:or: pence 2nd ends = meter. 2n ent:y saould Shee:s f:r Li.ensee Event Report (LER) Fde (SUREC416i t e m2:e fer Octn re;ct: pences :o be sure til snutdowns usmi de f 1!cwmg :nt:ena:
ct upf=t ;cwer recun ns are repor:ed.
TYPE. Lse -F or -S
- o.ndi:2:e e:eer "Fer:ec" or "S ne.
1 du:ecf' res:e:nvely, f:r e= snu: dawn er upS=t ;cwer 3.
If not 2 mm:enent fadure. 2se ce re:2::: am:ccent.
red =uen.
Fer:ed cu:d:*ns.n:iude 2:se requ;;ed :o te e g.. *reng v21ve operated intoup er cr. ':s: valve 24
.nn:2tec :y no 12:er man de weesend failc*=g dis =very
- mt.,cnent.
l
- ( 2n off. normal :endincn. I: :s re: g.::ed :nst seme ;u:g-men: :s requ red ut n:ept:=g shu:dswns in nus usy, in C.
If 2 =2m of fattures ec:urs. :ne nrst :ct :cr:ent :o ::i.
pne:2!. 2 for:ed snut: awn :s sne :n2: would act have been f2n:nce should :e lis:ec. The secuence of even:s. me:::.
=mpie:ec in me asence of me =nc:non for w n a ::r e:nve
- ng tne other
- mpenents wha:h fad. snou.d te dennbec un:n wu :2xen.
uncer :ne Cause 2nd Carre:nve A:::en :o ? event Ruur.
rence :ciumn.
i DURATION. Self.expia.2:civ. When 2 mu:dewn ex: ends Com:enea.:s that do net at any ex:s:ma : ce sncu d be de.
4
.:eyor.1 me enc of 2 te;crt pened. :oun: only de n=e to the ggg g p.7
.f g
g enc af me reecrt penod md ;10.4 :: :ne ensu=g down ::=e i
events waere 2 :cm:cnent des:pance :s not 2:;tt= !e.
.n me tv cwma reecrt :ences. Re ort duranen af cutages ruunced :o me ne: rest :entn oim neur :s fa::li:ste summanen.
CAUSE i CORRECTIVE ACTION TO PREVENT RECUR.
.::e sum at me total uutsp neurs ;tus :ne hcurs me pners.
C.e.. L.se me : lumn m a narranve fastuon :o am:uiy ar
- or au en..ane sncu!d ecusi :ne p:ss : tours.n de re ortmg ex:ia:n :ne n :umstances of :ne sautdown or 'cwer recucten.
-e -'"
The ciu:.= snould ac!uce de s:ee:de ause for e2:n mut-down or sierdent power redu:non and tne :mmeciate anc REASON. Catezonze n-. ner.,eup2 nun a accrdan:e antern:ntec lung term corre:nve acnen :2xen. f :;ercer:.
.e wun me t.:ie 2::earmg vn me 'e: ort fst n. If :steprv H ste.
- ns niumn snoul.,. also :e used,ar a des =: tan of :ne must e use.,. sue:ty tr:e: aur ments.
m2ict safety.re!sted ;ctre:nve mamtenance ;er:ct-ec danna the outsp at ;own acuenca.nduceg 2n dennkten a*
METHOD OF SHUTTISG DOWN THE REACTOR OR me mn.:1 m utny 2nd 2 m; n at any sm mesie e' REDUCING P0wER. Cateannze v numr er des esten r:ctosenvu> vr anz;e r:dist:en exp:sure s:ea:n.2dy ;;se.:.
Nie :nat m:s differs renm t. e Edison E:e :n: Ins::tu:e 2:ec vun me out:p ura:n ae :unt: for more m;n 'O :er.e--
(EEI) dedninens as "For:ed P: nal Out:ge" anc "Sene.
di de 2ilo*20'e mnuai v21ues.
l
- u.ed ?:rt:;;l Outau
- For tres,r renm. eel uses 4,. nap or For leng :ex:usi re:cr:s son:mue n2 :2::ve an se:2r:te 2:er l
JOM% 2s me =rea mnt. For :2rpr >=<r resciurs. 30 MW
.nJ re:erena rue m ur.'ow n ar ;cwer re:u. nun aa a
l
.s w call 4.nang to wars.nt ewiananon.
r'arrat;ve.
i l
..r --
e
.3+
gp
---.-,y
.---,,-,,..,,.e_.,.._-.s-_,...m m,,.
_.-__o.._
.-7 7
____,_..___.p
Dockst No.:
50-316 Unit Name:
D. C. Cook Unit 2 Completed By:
C. E. Murphy Telephone:
(616) 465-5901 Date:
12/9/82 Page:
1 of 1 MONTHLY OPERATING ACTIVITIES - NOVEMBER 1982_
Highlights:
The Unit entered the reporting period operating at 100% power. At 0553 on Friday, November 19 a Unit shutdown was commenced to perform the Unit's third refueling outage. At 0127 on November 21, the Reactor power level was lowered to less than 10% and the Reactor /
Turbine manually tripped off the grid. The Unit for the remainder of this reporting period is cooled down to 1460F in Mode 5 and the Reactor Coolant System drained to half loop.
The gross electrical generation for the month was 519,860 MWH.
Summary:
11/16/82 AB Diesel was inoperable for a period of 6.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> for maintenance repairs.
11/19/82 At 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> started Unit shutdown for refueling outage.
11/21/82 0127 hours0.00147 days <br />0.0353 hours <br />2.099868e-4 weeks <br />4.83235e-5 months <br />, removed Reactor / Turbine from service.
0330 hours0.00382 days <br />0.0917 hours <br />5.456349e-4 weeks <br />1.25565e-4 months <br />, RCS Degas in progress.
1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, entered Mode 4.
1747 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.647335e-4 months <br />, entered Mode 5.
2253.huurs, Containment Purge started.
11/22/82 CD Diesel was inoperable for a period of 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> for work on the Starting Air Check Valves.
11/26/82 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />, all R.C. Pumps off.
0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, began depressurizing RCS.
11/27/82 0001 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, began draining RCS.
0709 hours0.00821 days <br />0.197 hours <br />0.00117 weeks <br />2.697745e-4 months <br />, RCS at half loop.
DOCKET N0.
50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 12-14-82 4
COMPLETED BY
- 8. A. Svensson 4
TELEPHONE (616) 465-5901 PAGE 1 of 1 i
MAJOR SAFETY-RELATED MAINTENANCE NOVEMBER,1982 M-1 Steam generator No. 4 power operated relief valve,- MRV-243, had a body-to-bonnet leak. Disassembled and cleaned the valve. Re-assembled using new gaskets and had the valve tested.
M-2 No.1 steam generator blowdown sample containment isolation valve, DCR-301, was leaking by. Replaced the valve and had the new valve tested.
M-3 Following disassembly of the East centrifugal charging pump, non-destructive examination identified several indications on the i
internal cladding of the pump casing at the suction nozzle. The indications were removed by grinding to a maximum depth of 3/32".
NDE fellowing excavation revealed no further indications.
C&I-l Emergency boration flow indicator, QFI-420, was inoperable. The problem was traced to a defective 80 VDC power supply diode solder i
connection on the indication loop E to I converter. Repair of the solder connection and recalibration of the loop returned the indicator to operability.
C&I-2 Upper containment volume sampling isolation valve, ECR-21, would not open. A defective "asco" solenoid valve coil was replaced, and the actuator piston o-rings were changed to provide proper operation of ECR-21.
4 C&I-3 Steam generator No. I sample isolation valve, DCR-301, was leaking by. The valve operator was removed and replaced and the valve stroke was reset.
Proper operation was verified.
C&I-4 Volume control tank valve to vent header asco solenoid actuator, RS0-300, was not cycling the vent valve. The asco valve diaphragm 4
was discovered to have several perforations in it. An overhaul kit was installed to replace the diaphragm. Correct valve op-eration was verified after repairs.
C&I-5~
Source range nuclear instrumentation channel, N32, was indicating ten (10) counts with no power applied to the associated electronics i
drawer. The detector cable connector on the preamplifier was re-placed to eliminate the spurious reading.
- _ _ - _ _ _, _, _ _ _ _.. _.. _, _. _., _ _. _ _ _, _., _ _. -.... -. _ _,.. _ - _ _ _