ML20069H958

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Monthly Operating Repts for May 1994 for Bvps,Units 1 & 2.W/
ML20069H958
Person / Time
Site: Beaver Valley
Issue date: 05/31/1994
From: David Jones, Noonan T
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9406140117
Download: ML20069H958 (10)


Text

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~%s Telephone (412) 393-6000 Nuclear Group P O Box 4 Shippingport. P A 150774KKJ4 June 8,1994 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Gentlemen:

In accordance with Appendix A,

Technical Specifications, the Monthly Operating Report is submitted for Unit I and Unit 2 for the month of May,1994.

Respectfully, C

T. P. Noonan Division Vice President, Nuclear Operations /

Plant Manager DTJ/mmg Enclosures cc: NRC Regional Office King of Prussia, PA

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The Nuclear Professionals w

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9406140117 94o531 1

PDR ADOCK 05000334 i

R PDR

r NARRATIVE SIPfiARY OF Moff1HLY OPERATDC EXPERIDiCE UNIT 1 MAY 1994 l

l May 1 n e Unit operated at a nominal value of 100% output.

through i

May 5 i

May 6 2e Unit continued to operate at a nominal value of 100%

output.

At 2120 hours0.0245 days <br />0.589 hours <br />0.00351 weeks <br />8.0666e-4 months <br /> a Unit shutdown was commenced due to the ongoing status of repair efforts to a small pipe leak on the "A"

Train Reactor Plant River Water Supply Line to the Diesel Generator.

t May 7 At 0828 hours0.00958 days <br />0.23 hours <br />0.00137 weeks <br />3.15054e-4 months <br /> the Unit was taken off-line. Mode 2 was entered at 0835 hours0.00966 days <br />0.232 hours <br />0.00138 weeks <br />3.177175e-4 months <br />, Mode 3 was entered at 0918 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.49299e-4 months <br /> and Mode 4 was entered at 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> as the Unit continued to cool down to Mode 5 while repair efforts ard inspections of the Reactor Plant River Water Line continued.

May 8 Mode 5 was entered at 1122 hours0.013 days <br />0.312 hours <br />0.00186 weeks <br />4.26921e-4 months <br /> while repair efforts and inspections of Reactor Plant River Water line continued.

May 9 h e Unit remained in Mode 5 while repair efforts and through inspections of the Reactor Plant River Water Line continued.

May 17 May 18 he Unit remained in Mode 5 until 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> when heatup commenced to Mode 4 following completion of repairs and inspections of the Reactor Plant River Water line. Mode 4 was i

entered at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />.

_)'

May 19 he Unit remained in Mode 4 until 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> when heatup commenced to Mode 3.

Mode 3 was entered at 0505 hours0.00584 days <br />0.14 hours <br />8.349868e-4 weeks <br />1.921525e-4 months <br />.

May 20 he reactor was taken critical at 0548 hours0.00634 days <br />0.152 hours <br />9.060847e-4 weeks <br />2.08514e-4 months <br />. At 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br /> the Main Unit Generator was synchronized to the electrical grid and a gradual increase in power was miercxd. With the Unit at approximately 55% output, the quadrant power tilt ratio (QPTR) was determined out of specification. At 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, the Unit reduced output to less than 50% per 'Dachnical Specifications.

May 21 he Unit remained at approximately 49% output while allowing xenon to build up in the reactor core to correct the QPTR.

At 1225 hours0.0142 days <br />0.34 hours <br />0.00203 weeks <br />4.661125e-4 months <br /> the Unit commenced an increase in output to 100%

following a satisfactory QPTR.

May 22 he Unit achieved approximately 100% output at 1140 hours0.0132 days <br />0.317 hours <br />0.00188 weeks <br />4.3377e-4 months <br />.

NARPATIVE

SUMMARY

OF M0lTIHLY OPERATDJG EXPERIDJCE UNIT 1 MAY 1994 (continued)

May 23 The Unit operated at a nominal value of 100% output.

May 24 At 1331 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.064455e-4 months <br /> the Unit experienced a load rejection to approximately 48% output.

This was caused by a loose card in the Turbine Electrohydraulic Control (Dic) circuitry. Power was subsequently stabili2.ed at approximately 70% output. The card connections were repaired and the Unit was returned to approximately 100% output at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br />.

May 25 The Unit operated at a nominal value of 100% output.

through May 29 May 30 The Unit continued to operate at a nominal value of 100%

output.

At 1714 hours0.0198 days <br />0.476 hours <br />0.00283 weeks <br />6.52177e-4 months <br />, the "B" Cooling Tower Pump was shutdown due to high motor bearing temperatures. With one Cooling 7bwer Pump out of service and unusually wam atmospheric conditions present, a load reduction to approximately 98.5% output was commenced to stabilize cordenser hotwell conditions. Once the outside air cooled down and conditions in the condenser hotwell improved, the Unit returned to full power at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />.

May 31 The Unit continued to operate at a naminal value of 100%

output.

With one Cooling Tower Pump out of service and continuiry wam

weather, periodic load reductions were commenced at 0818 hours0.00947 days <br />0.227 hours <br />0.00135 weeks <br />3.11249e-4 months <br /> to stabilize condenser hotwell coryditions.

A minimum load reduction to approximately 98.3%

output was achieved at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.

Once conditions in the condenser hotwell had improved, the Unit returned to full power at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br /> and operated at a nominal value of 100% output for the remainder of the report period.

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-334 UNIT BVPS Unit 1 DATE June 3, 1994 COMPLEIID BY David T. Jones TELEPHONE (412) 393-7553 MOf71H May 1994 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(!&e-Net) 1 821 17 0

2 825 18 0

3 829 19 0

4 821 20 69 5

829 21 425 6

817 22 800 7

95 23 813 8

0 24 750 5

0 25 817 10 0

26 817 11 0

27 813 12 0

28 825 13 0

29 321 14 0

30 817 15 0

31 804 16 0

INSTRUCTIONS On this form, list the average daily unit power level MWe-Net for each day in

'he reportiry month. Ccrpute to the nearest stiole megawatt.

OPERATING DATA REPORT DOCRET NO..

50-334 REPORT DATE:

06/03/94 COMPLETED BY: DAVID T. JONES TELEPHONE:

(412) 393-7553 OPERATING STATUS

1. UNIT NAME:

BEAVER VALLEY POWER STATION, UNIT 1

2. REPORTING PERIOD:

Notes MAY 1994 3.

LICENSED THERMAL POWER (MWt) :

2652

4. NAMEPLATE RATING (Gross MWe):

923

5. DESIGN ELECTRICAL RATING (Net MWe):

835

6. MAX. DEPENDABLE CAPACITY (Gross MWe):

860

7. MAX. DEPENDABLE CAPACITY (Net MWe): 810 8.

IF CHANGES OCCUR IN CAPACITY RATINGS SINCE IAST REPORT, GIVE REASONS:

9 POWER LEVEL TO WHICH RESTRICTED, IF ANY (Net MWe):

None 10 REASONS FOR RESTRICTIONS, IF ANY:

N/A THIS MONTH YEAR TO DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD:

744.0 3623.0 158519.0

12. No. OF HRS. REACTOR WAS CRITICAL:

434.8 3078.2 102609.1

' 3. REACTOR RESERVE SHUTDOWN 110URS:

14. HOURS GENERATOR WAS ON LINE:

G0 0.0 4482.8

15. UNIT RESERVE SilUTDOWN HOURS:

425.6 3064.3 100607.5

16. CROSS THERMAL ENERGY GEN. (MWH):

1064786.0 7953520.0 241358996.5 0.0 0.0 0.0

17. GROSS ELECT. ENERGY GEN. (MWH):

348020.0 2593560.0 77751083.0

18. NET ELECTRICAL ENERGY GEN. (MWH).:

318410.0 2433830.0 72653350.0 19 UNIT SERVICE FACTOR: (PERCENT) 57.2 84.6 65.4

20. UNIT AVAILABILITY FACTOR:(PERCENT) 57.2 04.6 65.4
21. UNIT CAPACITY FACTOR (MDC): PCT
22. UNIT CAPACITY FACTOR (DER): PCT 52.8 82.9 59.1
23. UNIT FORCED OUTAGE RATE: (PERCENT)42.8 15.4 15.8 51.3 80.5 57.3 24 THE UNIT IS SCHEDULED TO SHUTDOWN FOR ITS TENTH OCTOBER 7.

1994 THE REFUELING OUTAGE IS SCHEDULED TO LAST FOR 70 DAY

25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

INITIAL CRITICALITY FORECAST ACHIEVED N/A N/A INITIAL EI.ECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A

UNIT SHUTDOWNS AND POWER REDUCTIONS (1201)

Docket No.

50-334 Unit Name BVPS Unit #1 Date June 3.

1994 Completed By David T.

Jones REPORT MONTH MAY 1994 Telephone (412) 393-7553 Method of Licensee Cause & Corrective Duration Shutting Event System Component Action to No.

Date Typet (Hours)

Reason 2 Down Reactor 3 Report #

Code 4 Code 5 Prevent Recurrence 5

940506 F

318.4 A

1 1-94-004 WA PIPEXX The Unit was shutdown due to the ongoing status of repair efforts to a small pipe leak on the "A" Train Reactor Plant River Water supply line to the Diesel Generator.

6 940524 F

0 H

5 N/A NA ELECON The Unit experienced a load rejection to approximately 48%

output caused by a loose card in the Turbine Electrohydraulic Control (EHC) circuitry.

1 2

3 4

F-Forced Reason:

Method:

Exhibit F*lnstructions for S-Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data Entry Sheets B-Maintenance or Test 2-Manual Scram for Licensee Event Report (LER) File C-Refueling 3-Automatic Scram (NUREG0161).

'D-Regulatory Restriction 4-Cont'd. from Previous Month E-Operator Training & License Exam 5-Reduction 5

F-Administrative 9-Other Exhibit H-Same Source.

G-Operational Error (Explain)

H-Other (Explain)

NARRATIVE SLMRRY OF MotTHILY OPERATIIKI EXPERIDiCE UtrIT 2 MAY 1994 May 1

'Ihe Unit operated at a nominal value of 100% output during through the entire report period.

May 31

}

i 1

l

AVERAGE DAILY UNIT POWER LEVEL DOCKET 10.

50-412 UNIT BVPS Unit 2 DATE June 3, 1994 COMPLETED BY __ David T. Jones TELEPHONE (412) 393-7553 MotTIH May 1994 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 844 17 844 2

845 18 843 3

843 19 842 4

842 20 838 5

841 21 833 6

842 22 832 7

844 23 832 8

842 24 834 9

837 25 834 i

10 841 26 836

{

11 837 27 843 12 841 28 839

{

13 840 29 835 14 837 30 830 15 830 31 825 16 841 INSTRUCTIONS on this fonn, list the average daily unit pcuer level MWe-Net for each day in the reporting month.

Campute to the nearest whole megawatt.

OPERATING DATA REPORT DOCRET NO.:

50-412 REPORT DATE:

06/03/94 COMPLETED BY: DAVID T. JONES TELEPHONE:

(412) 393-7553 OPERATING STATUS

1. UNIT NAME:
2. REPORTING PERIOD: BEAVER VALLEY POWER STATION, UNIT 2 MAY 1994 Notes
3. LICENSED THERMAL POWER (MWt):

2652 4

NAMEPLATE RATING (Gross MWe):

5. DESIGN ELECTRICAL RATING (Net MWe):

923 836

6. MAX. DEPENDABLE CAPACITY (Gross MWe):
7. MAX. DEPENDABLE CAPACITY (Net MWe):

870 820 8.

IF CHANGES OCCUR IN CAPACITY RATINGS SINCE LAST REPORT

, GIVE REASONS:

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (Net MWe): _

None

10. REASONS FOR RESTRICTIONS, IF ANY:

N/A THIS MONTH YEAR TO DATE CUMUIATIVE

11. HOURS IN REPORTING PERIOD:
12. NO. OF HRS REACTOR WAS CRITICAL:

744.0 3623.0 57302.0

13. REACTOR RESERVE SHUTDOWN HOURS:

744.0 3623.0 48953.3

14. HOURS GENERATOR WAS ON LINE:

0.0 0.0 0.0

15. UNIT RESERVE SHUTDOWN HOURS:

744.0 3623.0 48619.6

16. CROSS THERMAL ENERGY GEN.

0.0 0.0

0.0 (MWH)

1960148.0 9537469.0 119769354.4

17. CROSS ELECT. ENERGY GEN.(MWH):

656107.0 3199861.0 38851866.0

18. NET ELECTRICAL ENERGY GEN.

(MWH):

623620.0 3043555.0 36693834.0

19. UNIT SERVICE FACTOR: (PERCENT) 100.0 100.0 84.8
20. UNIT AVAILABILITY FACTOR:(PERCENT)
21. UNIT CAPACITY FACTOR (MDC): PCT 100.0 100.0 84.8
22. UNIT CAPACITY FACTOR (DER): PCT 102.2 102.4 77.6
23. UNIT FORCED OUTAGE RATE:

100.3 100.5 76.6 (PERCENT) 0.0 0.0 2.8 24 SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE,DATE AN 25.

IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION INITIAL CRITICALITY FORECAST ACHIEVED INITIAL ELECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A N/A N/A

UNIT SMU1 DOWNS AND POWER REDUCTIONS (120%)

k Docket No.

_50-412 Unit Name

_.BVPS Unit #2 Date June 3.

1994 REPORT MONTH MAY 1994 Completed By _ David T.

Jones Telephone (412) 393-7553 Method of Licensee Duration Shutting Event System Component No.

Date Typel (Mours)

Reason 2 Down Reactor 3 Report #

Code 4 Code 5 Cause & Corrective Action to Prevent Recurrence NONE 1

2 F-Forced Reason:

3 4

S-Scheduled A-Equipment Failure (Explain)

Method:

B-Maintenance or Test 1-Manual Exhibit F-Instructions for C-Refueling 2 Manual Scram Preparation of Data Entry Sheets D-Regulatory Restriction 3-Automatic Scram for Licensee Event Report (LER) File (NUREG0161).

4-Cont'd. from Previous Month E-Operator Training & License Exam F-Administrative 5 Reduction 5

9 Other G-Operational Error (Explain)

Exhibit N-Same Source, H-Other (Explain)

_ _ _ - - _ - - - -