ML20067E576
| ML20067E576 | |
| Person / Time | |
|---|---|
| Site: | Catawba |
| Issue date: | 02/07/1991 |
| From: | Tuckman M DUKE POWER CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9102150154 | |
| Download: ML20067E576 (2) | |
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.m Duke her Cornpany.
- (70.g)37340l1
- i Nuclear Pnxtuction Departrnent, L
PO Bar 1007
- Charlotte, NC20011007
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" e, DUKE POWER Tebruary' 7,- 1991 U. S. Nuclear. Regulatory Conunission ATTN: Document Control: Desk Washington, D.LC. L20555
Subject:
Catawba Nuclear Station, Unit 2 i
LDocket No.1S0-414-f Seventeenth Qu'arterly Update to Startup Report iln-accordance with Section 6.9.l.3'of the Catawba-Nuclear Station
~
- Technical Specifications, find attached the seventeenth quarterly update u,
to1the Unit 2 Startup Report.
Asi. indicated in my November 15, 1990 letter, one test is.not complete.. Additional. quarterly updates to the
~
Startup Report will be submitted as required by the. Technical
- Specifications.
.Very trulylyours,
- f h.
MkSMTuckman.
- CRLY
~ Attachment a
- xc: ~ Mr.: S.iD., Ebneter.
LRegionaljAdministrato Q Region'11:
UE S.; Nuclear-Regulatory Cornission (1017Marietta: Street, NW, Suit'e 2900=
- Atlantag! Georgia L30301
- Mr.! WET.. Orders NRC:ResidentLIrspector,
- l' Catawba Nuclear Station-_
m 7'
cMr.
R'. E. Martin-g
' Office:of-Nuclear 1 Reactor Regulations:
UF S. Nuclear Regulatory Commission J 0ne ' White' Flint N. orth,-. Mail Stop 9H3:
' Washington,=0.1C. 120555
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STARIUP REIGT QUARTERLY UP! ATE CATAWBA UNIT 2 CYCLE 1
-February 5, 1991 l
Testnn ctF4FTTED TRDG CUARTER None.
STAWS OF TmrDC WJr 034PIETE STEADY STATE PIPDC SYSTDG OPERATIMAL VIBRATIM MEASURDOTP - TP/2/A/1200/21 his test was described in Sections 10.5 and 11.5 in the Startup Report.
It
- is couplete s W for retesting of piping an w Mted with the Diesel Generator FLcl Oil and Inbe Oil systems. Additional restraints were installed during the B.C-1 refueling cutage. However, further modifications are found to be mry.- Those nodifications involved the replawmust of rigid piping
-with flexible piping. Vibration testing following empletion of the modification indicated that overall vibration levels had been r d W.
However, vibration levels in isolated portions of the piping still W_
allowable criteria. These levels wre evaluated and found to not constitute an inninent danger of failure. To resolve these isolated problems, modifications are planned which will result in a piping configuration similar
. to Unit 1.
The noilfications include replaw-uit of non-standard fittings wjth standard fittings, deletion of umry flanges, and valve relocation.
-Due to the extent of these modifications, they are schMiled 'for tha Unit 2
~BDC 4 refueling outageL(fourth quarter 1991).
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