ML20067E576

From kanterella
Jump to navigation Jump to search
Forwards 17th Quarterly Update to Startup Rept for Cycle 1
ML20067E576
Person / Time
Site: Catawba Duke Energy icon.png
Issue date: 02/07/1991
From: Tuckman M
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9102150154
Download: ML20067E576 (2)


Text

.

.~~-- ~........, - - ~. __~ -..

~..

s x

.m Duke her Cornpany.

- (70.g)37340l1

- i Nuclear Pnxtuction Departrnent, L

PO Bar 1007

- Charlotte, NC20011007

^

,. y -;r

" e, DUKE POWER Tebruary' 7,- 1991 U. S. Nuclear. Regulatory Conunission ATTN: Document Control: Desk Washington, D.LC. L20555

Subject:

Catawba Nuclear Station, Unit 2 i

LDocket No.1S0-414-f Seventeenth Qu'arterly Update to Startup Report iln-accordance with Section 6.9.l.3'of the Catawba-Nuclear Station

~

Technical Specifications, find attached the seventeenth quarterly update u,

to1the Unit 2 Startup Report.

Asi. indicated in my November 15, 1990 letter, one test is.not complete.. Additional. quarterly updates to the

~

Startup Report will be submitted as required by the. Technical

- Specifications.

.Very trulylyours,

f h.

MkSMTuckman.

CRLY

~ Attachment a

xc: ~ Mr.: S.iD., Ebneter.

LRegionaljAdministrato Q Region'11:

UE S.; Nuclear-Regulatory Cornission (1017Marietta: Street, NW, Suit'e 2900=

Atlantag! Georgia L30301
Mr.! WET.. Orders NRC:ResidentLIrspector,
  • l' Catawba Nuclear Station-_

m 7'

cMr.

R'. E. Martin-g

' Office:of-Nuclear 1 Reactor Regulations:

UF S. Nuclear Regulatory Commission J 0ne ' White' Flint N. orth,-. Mail Stop 9H3:

' Washington,=0.1C. 120555

?

g i

L

, A~ ~

-9102150154'910207.-

1l -l i

.i J

PDR.,ADOCK 05000414 E

'tP-POR-4 w

y.m

-e w

wy e

e y

.,4e+

y 4

n.-

' /

STARIUP REIGT QUARTERLY UP! ATE CATAWBA UNIT 2 CYCLE 1

-February 5, 1991 l

Testnn ctF4FTTED TRDG CUARTER None.

STAWS OF TmrDC WJr 034PIETE STEADY STATE PIPDC SYSTDG OPERATIMAL VIBRATIM MEASURDOTP - TP/2/A/1200/21 his test was described in Sections 10.5 and 11.5 in the Startup Report.

It

- is couplete s W for retesting of piping an w Mted with the Diesel Generator FLcl Oil and Inbe Oil systems. Additional restraints were installed during the B.C-1 refueling cutage. However, further modifications are found to be mry.- Those nodifications involved the replawmust of rigid piping

-with flexible piping. Vibration testing following empletion of the modification indicated that overall vibration levels had been r d W.

However, vibration levels in isolated portions of the piping still W_

allowable criteria. These levels wre evaluated and found to not constitute an inninent danger of failure. To resolve these isolated problems, modifications are planned which will result in a piping configuration similar

. to Unit 1.

The noilfications include replaw-uit of non-standard fittings wjth standard fittings, deletion of umry flanges, and valve relocation.

-Due to the extent of these modifications, they are schMiled 'for tha Unit 2

~BDC 4 refueling outageL(fourth quarter 1991).

P

-N 'l,

i<

1

:f 1

I t

L