ML20066D454
| ML20066D454 | |
| Person / Time | |
|---|---|
| Site: | Cooper |
| Issue date: | 10/06/1982 |
| From: | Ballinger P NEBRASKA PUBLIC POWER DISTRICT |
| To: | |
| Shared Package | |
| ML20066D448 | List: |
| References | |
| NUDOCS 8211110346 | |
| Download: ML20066D454 (4) | |
Text
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6 OPERATING DATA REPORT DOCKET NO. 050-298 DATE 10-6-82 COMPLETED BY P.
L.
Ballinger TELEPHONE 40Z-625-3311 OPERATING STATUS Notes
- 1. Unit Name:
Cooper Nuclear Station
- 2. Reporting Period:
September 1982
- 3. Licensed Thennal Power (MWt):
2381 836
- 4. Nameplate Rating (Gross MWe):
- 5. Design Electrical Rating (Net MWe):
778 787
- 6. Maximum Dependable Capacity (Gross MWe):
754
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report.Give Reasons:
- 9. Power Level To Which Restricted.lf Any (Net MWe):
- 10. Reasons For Restrictions.If Any:
This Month Yr to.Date Cumulative 720.0 6.551.0 72,336.0
- 11. Hours in Reporting Period 705.4 5,306.0 59,192.4
- 12. Number Of Hours Resetor Was Critical 0.0 0.0 0.0
- 13. Reactor Reserve Shutdown Hours 696.5 5,246.7 58,204.2
- 14. Hours Generator On.Line
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1,511,832.0 11,380,032.0 115,068,510.0
- 17. Gross Electrical Energy Generated (MWH) 503,570.0 _,
3,772,701.0 36,253,488.0
- 18. Net Electrical Energy Generated (MWH) 486,715.0 3,651,395.0 34,948,773.0
- 19. Unit Seavice Factor 96.7 80.1 80.5 96.7 80.1 80.5
- 20. Unit Availability Factor 88.5 73.0 63.2
- 21. Unit Capacity Factor (Using MDC Net) 86.9 71.6 62.1 l
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate 3.3 3.1 3.9
- 24. Shutdowns Schedul-d Over Next 6 Months (Type. Date,and Duration of Each1:
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY l
INITIAL ELECTRICITY c
COMMERCIAL OPERATION C'211110346 821006 PDR ADOCK 05000298 toc 7, R
FDR
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 050-298 Cooper Nuclear Station UNIT DATE October 6, 1982 t
COMPLETED BY P. L. Ballinger TELEPHONE 402-825-3811 MONTH September
~
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 764 37 728 729 2
758 13 3
759 714 39 728 4
304 20 3
130 728 21 493 728 6
22 534 729 7
,3 8
639 730 24 9
731 743 25 720 700 10 26 1I 717 27 731 12 698
- g 751 773 13 713 29 14 705 729 30 694 15 3,
16 725 INSTRUCTIONS On this format. list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
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t DOCKET NO. 050-298 UNIT SIIUIDOWNS AND POWER REDUCTIONS UNIT N AME Cooper Nuclear Station DATE october 6 1982 COMPLETED BY P. L. Ballinger REPORT MONTil s a m-amk a r TELEPHONE 402-825-3811 "E
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Cause & Corrective
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$Y5 Licensee
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No.
Date i
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Event p
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Prevent Recurrence 5
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82-8 820904 F
23.5 A
3 NA NA NA An electronic component in the "A" feedwater pump controller shorted out causing the "A" W loop flow to reduce to nearly zero flow. The reactor water level decreased to the trip leve L and the reactor scrammed. The failed component in the W pump controller was replaced and the plant was re-turned to operation.
1 I
1 2
3 4
F: Forced Reason:
Methtxt:
Exhibit G -Instructions S: Scheduled A. Equipment Failure (Explain) 1-Manual for Preparation of Data n-Meintenance or Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling 3 Automatic Scram.
Event Report ILER) Fde t N1IRIT;-
D Regulatory Restriction 4-Other (Explain) 0161) l E-Operator Training & License Examination F Administrative 5
Exhibit I - Same Source G-Operational Error (Explain) l')/77 )
Il-Other (Explaini l
g*
e -
Attachment B OPERATIONS NARRATIVE Cooper Nuclear Station September 1982 The plant operated the month of September with only one unscheduled shutdown. On September 4, 1982, an electronic component in the "A" feedwater pump control system failed causing the "A" FW loop flow to drop to nearly zero flow. Reactor water level decreased to the trip level and the reactor scrammed. Although the "B" FW automatically increased its flow to compensate for the loss of the "A" FW loop flow, it was insufficient to prevent the reactor scram. The failed component in the FW control system was replaced and the plant was returned to operation.
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4
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