ML20066D264

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Monthly Operating Rept for Mar 1981
ML20066D264
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/02/1981
From: Gillett W
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20066D250 List:
References
NUDOCS 8211110256
Download: ML20066D264 (6)


Text

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CPERAT:NC DATI RI? ORT

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50'-316 ccC:s*.IT No.

DATI d '2 Al CO.Nt?! ETED IY WT M1latt

- r::e.c.e:_

616-465-590I i

cPEn -'NGSTATUS N* *:5 Donald C. Cook 2

2, ee;; y m e.

Ma rch 1981 R._,.or %.3 a.,.

3391

3. U~._. sed -I ?:wer C.tW:):

1133

4. N::=:ph: Rad =;(Csess ?.IWe):

1100

5. Desi;= II===i=1 R :ing (Ne: 51We):

III8

6. 312::!=== Dqe::d: bis C2psci:7 (Cress SIWE):

1082

7. *.fr.xi=== Dc:: d:5!:C:p::i:7 (Ne: 31We):

S. !f Ch:::;-s Ce=rin Qpaci:7 P'*: gs (1::=s Nu=?m 3 Th:: ugh ~) SI :: I.::: R:pe::. Give Reasons:

7.. :n>c:!.:ve! To W?d=h Res=d:::d If Any (Ne: SIWE):
10. Res:ss For R..:
it=s.If Asy:

'Cds5tonth Yr.<o-Dass C===?::ive.

7a4 2.160

?8.464

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15. Uni: R:ee Ih::down Ecm.

1.053,877

  • 5,833,391
  • 59,453,025
16. Cross Th::. :1 In: *' C4 :=: d CitWii) 343,400._.

1,897,710 18,989,540 1,. Cress.:

-a g Cc.

s. G.tW.u.)

331,911 1,833,6/1 18,29._1,036

13. sre' ;,
. ;y Ce===:.,, L,.A..d) 41.9 80.0-72.3
19. U::i: Servi== 7::: r 41.9 80.0 72.3

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I. Uni: C:ps=!:., 5::::r (Usis: MDC Nec) 90.6 77.2 66.8 l
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-:.. Sh::dow.s scheduled over Nec s.sto :hs< Type. 0:te. : d ce=:fon of I: chi:

l Refuelino Outaae started 3-14-81 will end 5-8-81

5. !! Sh:: cowr At Inc or Repor: P -iod. Estir==:ed D:re ci ses:::=:

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25. Units :: Tes: 2::s (P:for to C: :=er:imi 0 :=:icar:

Tore==st Achieved I

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  • + 2,457 MWT error in Feb. Report mm 8211110256 810410 PDR ADOCK 05000316 R

PDR

l AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-316 UNIT 2

DATE 4-2-81 COMPLETED BY W. T. Gillett TELEPHONE 616-465-5901 MONTH March 1981 OAY AVEFAGE CAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL

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(MWE-Net)

(MWe-Net) 1 1060 17 2

1069 18 3

1069 19 4

1069 20 5

1069 21 6

1063 22 7

1061 23 8

1068 24 I

9 1070 25 10 1067 26 11 1067 27 12 1067 28 13 1031 29 14 30

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15 31

'l 16 INSTRUCTIONS On this fomat list the average daily unit power level in MWe-Net for each day in the reporting month. Comcute to the nearest whole megawatt.

DOCKET No. 50-316 UNITSiluTDOWNS ANI) POWER REDUCTIONS UNIT NAhlE D.C. Cook - Unit 2 DATE 4-9-81 March, 1981 COhlPLETED DY B.A. Svensson ItEPORT AIONTil TELEPilONE (616) 465-5901 3g 3

j' l.icensee

,Ev, Cause & Convective Eg 5

,csd Event Q?

g3 Action to No.

Date Q

y5 5

j if, lleport #

mO U

l-Prevent itecussence g

6 93 810314 S

431.9 B&C 1

N.A.

ZZ ZZZZZZ The unit was removed from service at -

0006 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> on 800314 for scheduled Cycle II - III refueling outage. The estimated outage time is 55 days.

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3 4

F: Fo.ud Iteason:

Method:

lixhibit G -Instructions 5: Scheilulcil A liquipment Failme(Explain) 141anual for Preparation or Data ll4taintenance or Test 2 Manual Scram.

linley Sheets fm 1.icensee C Ilefueling 3-Automalie Scram.

Event Repost (l. lilt) File INUlti:G-D Itegulalany llestiiction 1 Other (Explain) 0161)

I! Operator l' raining & License lixamination F Atiministsative 5

G. Operational linor Ilixplain) lixhibit ! Same Somce Pl/7/)

11 Olher (Explain)

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Docket No.:

50-316 Unit Name:

D. C. Cook Unit 2 Completed By:

C. E. Murphy Telephone:

(616) 465-5901 Date:

April 10,1981 Page:

1 of 1 i

MONTHLY OPERATING EXPERIENCES -- MARCH, 1981 HIGHLIGHTS:

The Unit operated at 100% power until 2200 on March 13, 1981 when power reduction was started to go to Cold Shutdown for Refueling, Maintenance, and Modifications.

The Unit had been on line for 88 days, 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> and 35 minutes.

The Unit Outage is scheduled for a duration of 55 days.

Total electrical generation for the month was 343,400 mwh.

SUMMARY

03/01/81 The East ESW Pump was inoperable for a 0.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period due to a Strain-er Gate not being aligned to the same strainer basket. This occurred during the Automatic Cleaning Sequence.

03/04/81 The High Demand Fire Pump was inoperable for a 7.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for lubrication.

03/11/81 Radiation Monitor (Air Ejectors) was inoperable for a 7.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for Calibration.

03/13/81 At 2200, the Unit was released for shutdown.

03/14/81 At 0510, the Unit entered Mode 4 (Hot Shutdown).

03/15/81 At 1240, the Unit entered Mode 5 (Cold Shutdown). At 2227, the "CD" Diesel became inoperable due to a broken line on the starting Air Check Valve on the rear bank #4 cylinder. This diesel returned to operable at 1245 on 04/07/81 after extensive repairs by the Maintenance Depart-ment.

03/25/81 At 0100, the Unit entered Mode 6 (Refueling).

03/31/81 At 1643, a Safety Injection Actuation occurred on this Unit. The cause of the Actuation was determined to be caused by a Surveillance Test which was being performed on the Pressurizer Pressure Channels. AB Die'sel started satisfactorily and there was no injection to the R.C.

System due to Clearance on the pumps. The Test procedure has been corrected to prevent future reoccurrences.

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DOCKET NO.

50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 4-10-81 COMPLETED BY

3. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 2 MAJOR SAFETY-RELATED MAINTENANCE MARCH, 1981 M-1 The south safety injection pump discharge drain valve, SI-109S, was found leaking by during inspection.

The 3/4" valve had a cracked seat.

The valve was removed and a new valve was welded in. All NDE requirements were met.

M-2 The suction valve for the north safety injection pump, SI-103N, had a body to bonnet leak.

Replaced the bonnet gasket.

M-3 Steam generator power operated relief valve, MRV-243, had a body to bonnet leak.

Replaced the bonnet and cage gaskets.

Had the valve tested.

M-4 Suction valve for CD diesel auxiliary jac'ket water pump, DG-150C, had a damaged stem.

The valve was replaced.

M-5 Non-essential service water containment isolation valves; WCR-909, WCR-929, WCR-931, WCR-948, WCR-951, WCR-952 and WCR-958 failed to pass the type C leak rate test.

Cleaned the valve internals, lapped the seat and replaced gaskets. Valves retested satisfactorily.

M-6 A crack was discovered in a 2 inch safety valve inlet line on the outlet of the west RHR heat exchanger. The crack was in a socket welded connection. The line was removed and a new nipple and flange for the safety valve were welded in. All necessary NDE was performed and.the welds were hydrostatic tested.

M-7 Component cooling water containment isolation check valves, CCW-243-25 and CCW-244-25, failed to pass the type C leak rate test.

Replaced the valve seats and had valves retested.

M-8 Refueling cavity drain line containment isolation valve, SF-159, failed to pass the type C leak rate test.

Replaced the valve diaphragm and had the valve retested. -

M-9 Component cooling water containment isolation valves, CCM-431 and 432, failed to pass the type C leak rate test.

Disassembled the valves, cleaned the internals and lapped the seat.

Reassembled the valves and had them retested.

l M-10 Non-essential service water containment isolation valve, NSW-419-1, failed to pass the type C leak rate test.

Disassembled valve, cleaned the internals, reassembled, and had it retested.

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.s DOCKET N0.

50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 4-10-81 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 2 of 2 MAJOR SAFETY-RELATED MAINTENANCE MARCH, 1981 M-ll The root valve for No. 4 main steam line pressure instrument, MPP-241, had seized in the open position.

Replaced the valve bonnet.

M-12 Non-essential service water containment isolation check valves failed to pass the type C leak rate test.

Disassembled and cleaned valve internals, lapped seats. reassembled with new gaskets and had valves retested.

?1-13 Non-essential service water containment isolation check valve, NSW-415-1, failed to pass the type C leak rate test.

Disassembled and cleaned valve internals.

Replaced the disc, reassembled with new gaskets and had the valve retested.

C&I-l Control Rod Position Indication for Rods H6 and C7 indicated greater than demand. The voltages associated with the two RPI channels were measured and verified the rods' position. The signal conditioning modules were adjusted to provide proper indication.

C&I-2 The two east essential service water pump strainer gates had aligned to different baskets while the pump was not in service.

Agastat time relay, 62X SEST, did not operate with a time delay which resulted in

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the strainer switching over only part of the time.

The time delay relay was replaced.

The 24-hour timer was jumpered to simulate a changeover and verify correct operation.

C&I-3 The auxiliary feedwater flow retention for motor operated auxiliary feedwater regulating valve, FM0-242, did not function.

Flow switch, FFS-245, was tested and found to be out of calibration.

FFS-245 was recalibrated and returned to service. A functional test was performed and verified correct operation.

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