ML20065T125
| ML20065T125 | |
| Person / Time | |
|---|---|
| Site: | Cooper |
| Issue date: | 09/08/1982 |
| From: | Ballinger P NEBRASKA PUBLIC POWER DISTRICT |
| To: | |
| Shared Package | |
| ML20065T116 | List: |
| References | |
| NUDOCS 8211020223 | |
| Download: ML20065T125 (4) | |
Text
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OPERATING DATA REPORT DOCKET NO.
050-298 DATE 9-8-82 COMPLETED BY P.
L. Ballinger TELEPHONE 402-825-3811 OPERATING STATUS Notes Cooper Nuclear Station
- 1. Unit Name:
August 1982
- 2. Reporting Period:
2381
- 3. Licensed Thermal Power (MWt):
836
- 4. Nameplate Rating (Gross MWe):
778
- 5. Design Electrical Rating (Net MWe):
787
- 6. Maximum Dependable Capacity (Gross MWe):
764
- 7. Maximum Deperviable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
- 9. Power Level To Which Restricted. If Any (Net MWe):
- 10. Reasons For Restrictions. If Any:
This Month Yr..to.Date Cumulative 744.0 5,831.0 71,616.0 i1. Hours in Reporting Period 716.5 4,600.6 58,487.0
- 12. Number Of Hours Reactor Was Critical 0.0 0.0 -
' O.0
- 13. Reactor Reserve Shutdown Hours 700.9 4,550.2 57,507.7
- 14. Hours Generator On-Line 0.0 0.0 0.0
- 15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (MWH) 1,503,024.0 9,868,200.0 113,556,678.0
- 17. Gross Electrical Energy Generated (MWH) 491,847.0,_,
3,269,131.0 35,749,918.0
- 18. Net Electrical Energy Generated (MWH) 475,188.0 3,164,680.0 34,462,058.0 94.2 78.0 80.3
- 19. Unit Service Factor 94.2 78.0 80.3
- 20. Unit Availability Factor 83.6 71.0 63.0
- 21. Unit Capacity Factor (Using MDC Net!
82.1 69.8 61.9 I
- 22. Unit Capacity Factor (Using DER Net) 5.8 3.0 3.9 I
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type.Date.and Duration of EachI:
f
- 25. If Shut Down At End Of Repost Pen;od. Estimated Date oiStartup:
l
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 82 1
("/ W D
0 R
v AVERAGE DAILY UNIT POWER LEVEL DOCKET No.
050-298 UNIT Cooper Nuclear Stat.
DATE 9-8-82 t
COMPLETED BY P. L. Ballinger TELEPHONE 402-825-3811 MONTH August DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 515 17 483 2
562 gg 0
3 669 19 29 4
752 20 279 5
748 21 607- -
6 750 22 605
_7 752 23 753 8
751 24 745 9
735 25 703 10 700 26 711 698 754 g3 27 705 727 12
- g 721 725 13 29 14 723 30 740 15 701 33 752 16 726 INSTRUCTIONS On this format. list the average daily unit power levelin MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77) ll 4
050-298
~C DOCKET NO.
UNIT SIIUlDOWNS AND POWER REDUCTIONS C Per Nuclear Statios UNIT N AME DATE September 8, 1982 COMPLETED BY P.
I,.
Ballinger REPORT MONTil August TELEPHONE, 402-825-3811
~.
E c
5 ?
'h
$Y3 Licensee gg yn, Cause & Corrective No.
Date g
5g 4
2s5 Event p
pu Action to jE 5
Ji di c Report e mO Prevent Recurrence H
o g
U Q
82-7 820817 F
43.1 A
3 N/A N/A N/a A failure in the turbine control sys-tem caused the main steam control val-ves to close. The pressure transient caused by the control valve closure resulted in a neutron flux spike and a reactor scram. A bad circuit card was replaced in the turbine control system and plant returned to operation.
I 2
3 4
F: Forced Reason:
Method:
Exhibit G - Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data Il-Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C-Refueling 3-Automatic Scram.
Event Report (LER) Fde (NURI G-D Regulatory Restriction 4 01her (Explain) 0161)
E-Operator Training & License Examination F Administrative 5
Exhibit I - Same Source G Operational Error (Explain)
(?/77)
Il-Other (Explain)
,. ~
OPERATIONS NARRATIVE Cooper Nuclear Station August 1982 The plant operated the month of August with only one unscheduled shut-down. On August 17, a failure in the turbine control system electronic circuitry caused the main steam control valves to close. This closure caused a pressure transient in the reactor vessel and resulted in high neutron flux and a reactor scram. A circuit card in the turbine control system was found def ective and was replaced. The plant returned to operation after satisfactorily testing of the' turbine control system.