ML20065L801

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Monthly Operating Rept for Sept 1982
ML20065L801
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 10/04/1982
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML20065L799 List:
References
NUDOCS 8210190723
Download: ML20065L801 (8)


Text

.

L JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE

SUMMARY

OF OPERATIONS SEPTEMBER, 1982

~

In the month of September there was one (1) unit shutdown.

The.following safety-related maintenance was performed in the month of September:

1

1. Performed miscellaneous maintenance on diesel generators.
2. Rewired starter box and replaced contactor to accommodate 15KW-lube oil heater on~ diesel ge. aerators IC and 2C.
3. Disassembled Waste Evaporator Feed Pump and installed new bearings', oil seals, seal housing "0" ring and i'npeller "0" ring.
4. Installed stops for Spent Fuel Pool Heat Exchanger IB Maint-enance Monorail.
5. Repacked #9 River Water Pump.

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OPERATING DATA REPORT I

DOCKET NO. 50-348 8 j' DATE 10/04/82 COMPLETED BY W.G.Hairston II8 TELEPilONE (205)899-5155 OPERATING STATUS

1. Unit Name:

Joseph M.

Farlev-Unit 1

. Notes

2. Reporting Period:

September, 1982 1)-Cumulative data

3. Licensed Thermal Power (MWt):

2652 since 12/01/77, date

4. Nameplate Rating (Gross MWe):

860 Of commercial oper-

5. Design Electrical Rating (Net MWe):

829 ation.

6. Maximum Dependable Capacity (Gross MWe):

844.6

~

7. idaxinnm Dependable Capacity (Net MWe):

803.6

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

N/A

9. Power Level To Which Restricted,if Any (Net MWe):

N/A

10. Reasons For Restrictions,if Any:

N/A This Month Yr. to-Date Ctimulative

11. Hours In Reporting Period 720 6551 42,359
12. Number Of Hours Reactor Was Critical 709.9 4982.2 25,964
13. Reactor Reserve Shutdown flours
10. 1 104.5 3,596.5
14. Ilours Generator on-Line 707.3 4779.1 25,108.8
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWil) 1,812,488

_12,068,904 63,013,815

17. Gross Electrical Energy Generated (MWH) 572 2]6_

3,794,606 20,031,558 t

18. Net Electrical Energy Generated (MWH) 542.016 3.566.112 18.789.836
19. Unit Service Factor 98.2 73.0 59.3
20. Unit Availabilitv Factor 98.2 73.0 59.3
21. Unit Capacity Factor (Using MDC Net) 93.7 67.7 55.2
22. Unit Capacity Factor (Using DER Net) 90.8 65.7 53.5
23. Unit Forced Outage Rate
1. 8 26.8 19.4
24. Shutdowns Scheduled Oser Next 6 Months (Type. Date,and Duration of Each1:

Re fuel i n g Ont age,

,T an n a rv 1-1983? Approximately 10 weeks l

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiesed i

INITIA L CRIIICALITY 8/06/77 8/09/77 INillA L ELECTRICITY 8/20/77 8/18/77 i

COMMERCIAL OPER ATION 12/01/77 12/01/77 t

(9/77 )

~ 1

3 50-348 DOCKLI tiO.

J.

M.

Ferley-Unitl

' UNIT DAlt 10/04'/82 C05fPLETED DY W.

G.

Hairston,III i

7ELEPl!ONE (205)899-5156

. ggg, September

- DAY AVERAGE D.\\lLY l'OhER LEVEL DAY AVERAGE D AIL POWER L EVEL

. (Sitie. Net).

(5tWe-Net) y-568~

791

,7 791 782 g3 2;

791 791 3

39 N

790

-793 4

20 795 798

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^

15..

21 794 805 6

n 808 796 23 7

804 797 2,g g;

9 790 25 803 to 788 26 804

3 n

447 790 j

232 789 e

12' 700 13:

788

,9 799

-789 30

- 3.g.

787 3

.ts 116 :

790' I

INSTRtici!ONS On this formir. list the. svenge daily umt power le elin htwe. Net for each d:y in the reponing inienth. Compute to

, the nesseu whole nw ;mait.

,i (9/77)

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4 UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO.

UNIT NAME J.M. Farley-Unit 1 -*

DATE 10/04/82 REPORT MONTil Septaber, 1982 COMPLETED gy W.G. Hairston III TELEPlf0NE (205)899-5156 ~

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} Ej Licensee Eg Cause & Curreceive No.

Date

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,, g x Event uv

$E 5

ji5g Report #

fO" Acilon so 50 Prevent Recurrence i-5 008 820927 F

12.7 A

3 NA EB REIAYX A printed circuit card for a protective relay for a load center input breaker failed, hence de-energizing the load center. 'Ihis resulted in an open in-dication on Reactor Coolant PLmp #1 breaker, thus causing a Unit trip.

Following the replac ment of the printed circuit card, the Unit ws returned to service.

l l

t 1

2 3

4 l

F: Forced Reason:

Method:

Exhibit G. Instructions S: Sclieduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.

Entry Sheels for Licensec C Refueling 3 Automatic Scra.n.

Event Report (LER) File (NOREG-D Regulatosy Resti.ction 4-Other (Explain) 0161)

E Opesator Tsaining & IJcense Examination F Administaasive 5

G.Opesational Ee ms (Explain)

Exinbis 1 - Same Source (9/77) ll Othes (E xplain)

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JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1

-NARRATIVE

SUMMARY

OF OPERATIONS SEPTEMBER, 1982 In the month of September there was one (1) unit shutdown.

The following safety-related maintenance was performed in the month of September:

1. Performed miscellaneous maintenance on diesel generators.
2. Rewired starter box and replaced contactor to accommodate 15KW lube oil heater on diesel generators IC and 2C.
3. Disassembled Waste Evaporator Feed Pump and installed new bearings, oil seals, seal housing "0" ring and impelbr "0"

ring.

4. Installed stops for Spent Fuel Pool Heat Exchanger IB Maint-enance Monorail.
5. Repacked #9 River Water Pump.

+

1

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OPER ATING DATA REPORT DOCKET NO. 50-348 8l DATE 10/Q1/12

_W.G.Hai 1205) 89.rston II2

~ - t,OMPLETED BY 9-5155 TELEPilONE 6

!I*

OPERATING STATUS Notes

i. Unit Name:

Joseph'M.' Farley-Unit 1

2. Reporting Period:

September, 1982

'1) Cumulative data

~

2652 since 12/01/77, date

- 3. Licensed Thermal Power (MWt):

4. Nameplate Rating (Gross MWe):

860 of commercial oper-

5. Design Electrical Rating (Net MWel:

829 ation.

844.6

6. Maximum Dependable Capacity (Gross MWe):

803.6 I

7, Maximum Dependable Capacity (Net MWe):

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Smce Last Report. Give Reasons:

N/A

9. Power Lesel To Which Restricted,if Any (Net MWe):

N/A-10 Reasons Fst Restrictions.If Ar.y:

N/A This Month Yr.-ta.Date Cumulative

11. Hours in Reporting Period 720 6551 42,359
12. Number Of flours Reactor Was Critical 709.9 4982.2 25,964
13. Reactor Resene Shutdown Hours 10.1

'104.5 3,596.5

14. Hours Generator On.Line 707.3 4779.1 25,108.8
15. Unit Resene Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1,812,488 12,068,904 63,013,815
17. Gross Electrical Energy Generated (MWil) 572,236, 3,794,606 20,031,558 i

'l8. Net Electrical Energy Generated (MWH) 542 016

't _. 5 6 6.112 18.789.836

19. Unit Senice Factor 98.2 73.0 59.3
20. Unit Asailability Factor 98.2 73.0 59.3
21. Unit Capacity Factor (Using MDC Net)

-93.7 67.7 55,2

22. Unit Capacity Factor (Using DER Net) 90.8 65.7 53.5
23. Unit Forced Outage Rate
1. 8 26.8 19,4
24. Shutdowns Scheduled Over Next 6 Mont'hs (Type. Date.and Duration of Eacht

+

Re runl i ng Ontage -.Tannary 1.

1983-Approximately 10 weeks

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiesed INITIAL CRiflCALITY '

8/06/77 8/09/77 INITI AL ELECTRICITY 8/20/77 8/18/77 i

COMMERCIAL OPER ATION 12/01/77 12/01/77 (9/77) g

w.

c-___._.

50-348 DOCELI 140.

nw

. UNIT J. M. ' Farley-Unit]

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O dan 10/04'/82 rT;' U ? ig'

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C05fPLETED Dy W.

G. Hairston,III I

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is 1ELEPl!ONE (205)899-5156

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.. September

. 3!ONTil

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. DAY AVElt.tGE D.\\lLY l'OWEit LEVEL DAY AVEllAGE D All POWEli L EVEL (MWe Net)

-(MWcNc0 568 791 37 791 782 g3 2

~

791 19 3

793 790 20 4

795 21 '

798

' j' 805

^

,794

~

6 808 796 23 x,

7 804

g' 797
4 803

- 25

,'r',, ; <> -

790

~ '

+

s 804

,: Jjo 788 26 f.

c-447 790 n

gg.

789 3

232 12 788

~

700

9 13 799 789 1.g 30 787 31 gg 790 16

-p s ;-

INgRbCllONS -

1 m

On th0 formir. list th,: svenge daily umt puweric=ct in MWe Net for each d:y in the reporimg month. Compiite to

'.; the neare:t v.hule negr.ust.

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4 UNIT 58tUTDOWNS AND POWER REDUCHONS DOCKET NO.

UNIT NAME J.M. Farley-Wat 1 -

DATE 10/04/82 REPORT MONTIf Septaber, 1982 COMPLETED sY W.G. Hairston, III TELEPlGONE (205)899-5156

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j175g Reinw #

E0 Psevais Recus,ence d

008 820927 F

12.7 A

3 NA EB REIAYX

'A printed circuit card for a protective relay for a load center input breaker failed, hence de-energizing the load center. 'Ihis resulted in an open in-c dication c-Beactor Coolant Ptrp il breaker, trm causing a Unit trip.

Following the replacenent of the

' printed circuit card, the Unit was i

returned to service.

d 1

i F: Forced

' 2 3

4 Reason:

Method:

Exhibit G. insitucti.ms j

S: Scheduled A. Equipment Failure (Explain)

I-Manual for Preparati m of Data li-Maintenance of Test 2 Manual Scram.

Entry Sheets for l_icensee C. Refueling 3 Automatic Sceaan.

Event Rep wi (1.ER) File (NOREG-D-Regulatosy Resisicti m 4 0. lier (Explain) 01611 E-Ope ator Tsaining & license Examinati m I Administsasive l

G.Opciatiemal Esror (Explain) 5 Exlubia I - Same Sour. e (9/77) ll Othes (Explain)

-.