ML20065L801
| ML20065L801 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 10/04/1982 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20065L799 | List: |
| References | |
| NUDOCS 8210190723 | |
| Download: ML20065L801 (8) | |
Text
.
- L JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE
SUMMARY
OF OPERATIONS SEPTEMBER, 1982
~
In the month of September there was one (1) unit shutdown.
The.following safety-related maintenance was performed in the month of September:
1
- 1. Performed miscellaneous maintenance on diesel generators.
- 2. Rewired starter box and replaced contactor to accommodate 15KW-lube oil heater on~ diesel ge. aerators IC and 2C.
- 3. Disassembled Waste Evaporator Feed Pump and installed new bearings', oil seals, seal housing "0" ring and i'npeller "0" ring.
- 4. Installed stops for Spent Fuel Pool Heat Exchanger IB Maint-enance Monorail.
- 5. Repacked #9 River Water Pump.
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OPERATING DATA REPORT I
DOCKET NO. 50-348 8 j' DATE 10/04/82 COMPLETED BY W.G.Hairston II8 TELEPilONE (205)899-5155 OPERATING STATUS
- 1. Unit Name:
Joseph M.
Farlev-Unit 1
. Notes
- 2. Reporting Period:
September, 1982 1)-Cumulative data
- 3. Licensed Thermal Power (MWt):
2652 since 12/01/77, date
- 4. Nameplate Rating (Gross MWe):
860 Of commercial oper-
- 5. Design Electrical Rating (Net MWe):
829 ation.
- 6. Maximum Dependable Capacity (Gross MWe):
844.6
~
- 7. idaxinnm Dependable Capacity (Net MWe):
803.6
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
- 9. Power Level To Which Restricted,if Any (Net MWe):
N/A
- 10. Reasons For Restrictions,if Any:
N/A This Month Yr. to-Date Ctimulative
- 11. Hours In Reporting Period 720 6551 42,359
- 12. Number Of Hours Reactor Was Critical 709.9 4982.2 25,964
- 13. Reactor Reserve Shutdown flours
- 10. 1 104.5 3,596.5
- 14. Ilours Generator on-Line 707.3 4779.1 25,108.8
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWil) 1,812,488
_12,068,904 63,013,815
- 17. Gross Electrical Energy Generated (MWH) 572 2]6_
3,794,606 20,031,558 t
- 18. Net Electrical Energy Generated (MWH) 542.016 3.566.112 18.789.836
- 19. Unit Service Factor 98.2 73.0 59.3
- 20. Unit Availabilitv Factor 98.2 73.0 59.3
- 21. Unit Capacity Factor (Using MDC Net) 93.7 67.7 55.2
- 22. Unit Capacity Factor (Using DER Net) 90.8 65.7 53.5
- 23. Unit Forced Outage Rate
- 1. 8 26.8 19.4
- 24. Shutdowns Scheduled Oser Next 6 Months (Type. Date,and Duration of Each1:
Re fuel i n g Ont age,
,T an n a rv 1-1983? Approximately 10 weeks l
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed i
INITIA L CRIIICALITY 8/06/77 8/09/77 INillA L ELECTRICITY 8/20/77 8/18/77 i
COMMERCIAL OPER ATION 12/01/77 12/01/77 t
(9/77 )
~ 1
3 50-348 DOCKLI tiO.
J.
M.
Ferley-Unitl
' UNIT DAlt 10/04'/82 C05fPLETED DY W.
G.
Hairston,III i
7ELEPl!ONE (205)899-5156
. ggg, September
- DAY AVERAGE D.\\lLY l'OhER LEVEL DAY AVERAGE D AIL POWER L EVEL
. (Sitie. Net).
(5tWe-Net) y-568~
791
,7 791 782 g3 2;
791 791 3
39 N
790
-793 4
20 795 798
- ~
^
15..
21 794 805 6
n 808 796 23 7
804 797 2,g g;
9 790 25 803 to 788 26 804
- 3 n
447 790 j
232 789 e
12' 700 13:
788
,9 799
-789 30
- 3.g.
787 3
.ts 116 :
790' I
INSTRtici!ONS On this formir. list the. svenge daily umt power le elin htwe. Net for each d:y in the reponing inienth. Compute to
, the nesseu whole nw ;mait.
,i (9/77)
.h 4
+
t I
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4 UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
UNIT NAME J.M. Farley-Unit 1 -*
DATE 10/04/82 REPORT MONTil Septaber, 1982 COMPLETED gy W.G. Hairston III TELEPlf0NE (205)899-5156 ~
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.! E
}
} Ej Licensee Eg Cause & Curreceive No.
Date
{
3g
,, g x Event uv
$E 5
ji5g Report #
fO" Acilon so 50 Prevent Recurrence i-5 008 820927 F
12.7 A
3 NA EB REIAYX A printed circuit card for a protective relay for a load center input breaker failed, hence de-energizing the load center. 'Ihis resulted in an open in-dication on Reactor Coolant PLmp #1 breaker, thus causing a Unit trip.
Following the replac ment of the printed circuit card, the Unit ws returned to service.
l l
t 1
2 3
4 l
F: Forced Reason:
Method:
Exhibit G. Instructions S: Sclieduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.
Entry Sheels for Licensec C Refueling 3 Automatic Scra.n.
Event Report (LER) File (NOREG-D Regulatosy Resti.ction 4-Other (Explain) 0161)
E Opesator Tsaining & IJcense Examination F Administaasive 5
G.Opesational Ee ms (Explain)
Exinbis 1 - Same Source (9/77) ll Othes (E xplain)
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)
JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1
-NARRATIVE
SUMMARY
OF OPERATIONS SEPTEMBER, 1982 In the month of September there was one (1) unit shutdown.
The following safety-related maintenance was performed in the month of September:
- 1. Performed miscellaneous maintenance on diesel generators.
- 2. Rewired starter box and replaced contactor to accommodate 15KW lube oil heater on diesel generators IC and 2C.
- 3. Disassembled Waste Evaporator Feed Pump and installed new bearings, oil seals, seal housing "0" ring and impelbr "0"
ring.
- 4. Installed stops for Spent Fuel Pool Heat Exchanger IB Maint-enance Monorail.
- 5. Repacked #9 River Water Pump.
+
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OPER ATING DATA REPORT DOCKET NO. 50-348 8l DATE 10/Q1/12
_W.G.Hai 1205) 89.rston II2
~ - t,OMPLETED BY 9-5155 TELEPilONE 6
!I*
OPERATING STATUS Notes
- i. Unit Name:
Joseph'M.' Farley-Unit 1
- 2. Reporting Period:
September, 1982
'1) Cumulative data
~
2652 since 12/01/77, date
- 3. Licensed Thermal Power (MWt):
- 4. Nameplate Rating (Gross MWe):
860 of commercial oper-
- 5. Design Electrical Rating (Net MWel:
829 ation.
844.6
- 6. Maximum Dependable Capacity (Gross MWe):
803.6 I
7, Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Smce Last Report. Give Reasons:
N/A
- 9. Power Lesel To Which Restricted,if Any (Net MWe):
N/A-10 Reasons Fst Restrictions.If Ar.y:
N/A This Month Yr.-ta.Date Cumulative
- 11. Hours in Reporting Period 720 6551 42,359
- 12. Number Of flours Reactor Was Critical 709.9 4982.2 25,964
- 13. Reactor Resene Shutdown Hours 10.1
'104.5 3,596.5
- 14. Hours Generator On.Line 707.3 4779.1 25,108.8
- 15. Unit Resene Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1,812,488 12,068,904 63,013,815
- 17. Gross Electrical Energy Generated (MWil) 572,236, 3,794,606 20,031,558 i
'l8. Net Electrical Energy Generated (MWH) 542 016
't _. 5 6 6.112 18.789.836
- 19. Unit Senice Factor 98.2 73.0 59.3
- 20. Unit Asailability Factor 98.2 73.0 59.3
- 21. Unit Capacity Factor (Using MDC Net)
-93.7 67.7 55,2
- 22. Unit Capacity Factor (Using DER Net) 90.8 65.7 53.5
- 23. Unit Forced Outage Rate
- 1. 8 26.8 19,4
- 24. Shutdowns Scheduled Over Next 6 Mont'hs (Type. Date.and Duration of Eacht
+
Re runl i ng Ontage -.Tannary 1.
1983-Approximately 10 weeks
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
N/A
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed INITIAL CRiflCALITY '
8/06/77 8/09/77 INITI AL ELECTRICITY 8/20/77 8/18/77 i
COMMERCIAL OPER ATION 12/01/77 12/01/77 (9/77) g
w.
c-___._.
50-348 DOCELI 140.
- nw
. UNIT J. M. ' Farley-Unit]
.m
.N x
O dan 10/04'/82 rT;' U ? ig'
~
C05fPLETED Dy W.
G. Hairston,III I
- y -
+:
- is 1ELEPl!ONE (205)899-5156
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.. September
. 3!ONTil
=w-4-
4 l '
. DAY AVElt.tGE D.\\lLY l'OWEit LEVEL DAY AVEllAGE D All POWEli L EVEL (MWe Net)
-(MWcNc0 568 791 37 791 782 g3 2
~
791 19 3
793 790 20 4
795 21 '
798
' j' 805
^
,794
~
6 808 796 23 x,
7 804
- g' 797
- 4 803
- 25
,'r',, ; <> -
790
~ '
+
s 804
,: Jjo 788 26 f.
c-447 790 n
gg.
789 3
232 12 788
~
700
- 9 13 799 789 1.g 30 787 31 gg 790 16
-p s ;-
INgRbCllONS -
1 m
On th0 formir. list th,: svenge daily umt puweric=ct in MWe Net for each d:y in the reporimg month. Compiite to
'.; the neare:t v.hule negr.ust.
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(9(77)
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4 UNIT 58tUTDOWNS AND POWER REDUCHONS DOCKET NO.
UNIT NAME J.M. Farley-Wat 1 -
DATE 10/04/82 REPORT MONTIf Septaber, 1982 COMPLETED sY W.G. Hairston, III TELEPlGONE (205)899-5156
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j175g Reinw #
E0 Psevais Recus,ence d
008 820927 F
12.7 A
3 NA EB REIAYX
'A printed circuit card for a protective relay for a load center input breaker failed, hence de-energizing the load center. 'Ihis resulted in an open in-c dication c-Beactor Coolant Ptrp il breaker, trm causing a Unit trip.
Following the replacenent of the
' printed circuit card, the Unit was i
returned to service.
d 1
i F: Forced
' 2 3
4 Reason:
Method:
Exhibit G. insitucti.ms j
S: Scheduled A. Equipment Failure (Explain)
I-Manual for Preparati m of Data li-Maintenance of Test 2 Manual Scram.
Entry Sheets for l_icensee C. Refueling 3 Automatic Sceaan.
Event Rep wi (1.ER) File (NOREG-D-Regulatosy Resisicti m 4 0. lier (Explain) 01611 E-Ope ator Tsaining & license Examinati m I Administsasive l
G.Opciatiemal Esror (Explain) 5 Exlubia I - Same Sour. e (9/77) ll Othes (Explain)
-.