ML20064E385

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Monthly Oper Rept for Oct 1978
ML20064E385
Person / Time
Site: North Anna Dominion icon.png
Issue date: 10/31/1978
From: Woods D
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML20064E384 List:
References
NUDOCS 7811170109
Download: ML20064E385 (5)


Text

l VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION MONTHLY OPERATING REPORT MONTH October YEAR 1978 I

SUBMITTED:

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.. SUPERINTENDENT -()TATION OPERATIONS i

APPROVED-i l

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OPERATLNG DATA REPORT DOCKET NO. 50-338 DATE 11-7-78 COMPLETED BY fi f'

Wnds TELEPHONE 703-894-5151 x 360 OPERATING STATUS North Anna Not'5

1. Unit Name:

October 1978

2. Reporting Period:

2,775 i

3. Licensed Thermal Power (MWt):
4. Nameplate Rating (Gross MWe):

94[

90'

5. Design Electrical Rating (Net MWe):

928

6. Maximum Dependable Capacity (Gross MWe):

898

7. Madmum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report.Give Reasons:

N/A

9. Power Level To Which Restricted.lf Any (Net MWe):

N/A

10. Reasons For Restrictions,if Any:

N/A p.

.p This Month Yr. to Date cumulative 745 3,553 3,553

11. Hours in Reporting Period 679.4 3,242.1 3,242.1
12. Number Of Hours Reactor Was Critical k
13. Reactor Reserve Shutdown Hours 0

0 0

657.2 3,211.4 3,211.4

14. Hours Generator On-Line 0

0 0

15. Unit Reserve Shutdown Hours l
16. Gross Therma! Energy Genersted (MWH) 1.750.627 8.379.826 R.379.R76
17. Gross Electrical Energy Generated (MWH) 560.197 2.684.107 2.684.107
18. Net Electrical Energy Generated (MWH) 528,766 2.517.863 2.517.863 88.2%

90.4%

90.4%

19. Unit Service Factor 88.2%

90.4%

90.4%

20. Unit Availability Facroe 79.1%

78.9%

78.9%

21. Unit Capacity Factor (Using MDC Net) 76.5%

76.4%

76.4%

22. Unit Capacity Factor (Using DER Net) 5.3%

1.4%

1.4%

i

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Eacht:

Snubber Inspection. April 1979. I week

25. If Shut Down At End Of Repor' ' riod. Estimated Date of Startup:
26. Units in Test Status (Prior to Coe mercial Operation);

Forecast Achieved INITIAL CRITICALITY INITIAL El.ECTRICITY COMMERCIAL OPERATION (o/77) 1 l

m,._

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-338 UNIT # North Anna #1 1 /7/78 om D. C. Woods COMPLE1ID BY 703-894 5151 x 360 TELEPHONE I

MONTH October DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL i

I (MWe Net)

(MWe Net) 0 844 i

,7

.0 840 2

1s 481 834 3

19 73 836 4

20 481 832 i

5 21 750 833 3

834 836 3

s 844 24 634 l

837 407 25 t

785 820 3,

26 839 823 33 3

12 847 28 R25 13 845

9 831 840 828 34 3a 044 830 15 31 1

845 16 e

INSTRUCTIONS On this format, list the average dady unit power tevelin MWe-Net for each day in the reporting month. Compute to the nearest whole megnvatt.

l f

i (9/77) 2

'W 9'

o UNIT SilUTDOWNS AND POWER REDUCTIONS g,

io Anna 1 DATE Nov. 1_ 197R COMPLETED BY

_A. C Plcufer_.

REPORT MONTil 0ctober TEt>ErilONE 703-894-5151 -x 229 c

jg "g

}[3a:

Cause & Corretlive

}

Licensee g"3 Action to Event g?

gu i

No.

Date g

3g f,

Prevent Recurrence fI 5

j p, Report #

'n U H

g 6

78-28 781003 F

12.3 B

4*

Manual Shutdown to repair blown plug on high pressure turbine cross under pipe rewelded returned to power.

78-29 781004 F

9.0 A*

's High flux rate 2/4 channels caused reactor trip due to fault in a gain pot.

78-30 781024 F

15.7 A*

1 Manual reactor / turbine / generator trip due to a loss of cooling water to "A" reactor coolant pump. Repaired faulty cooling water valve.

4 1

2 3

4 F: Forced Reason:

Method:

Exhibit G. instructions S: Scheduled A Equipment Failure (Expl In) 1-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.

Entry Sheets for Licensee C. Refueling

3. Automatic Scram.

Event Repost (LER) FileINUREG-D Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Training & License Examination -

F-Administrative 5

G Operational Error (Explain)

Exhibit I. Same Sourge 07/77)

II Other (Explain),

  • See attached sheet.

t Paga 1 of 1 UNIT SHUTOOWN AND POWER REDUCTIONS i

EXPLANATION SPEET DOCKET NO. 50-338 REPORT tiONTH UNIT NAME North Anna YEAR 1978 DATE Nov. 1, 1978 COMPLETED BY A. G. Neufer -

NOTE: Shutdcwn 78-27 was concluded 10-3-78 at 0023.

48.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />.

78-28 (4)

Reactor was not shutdown.

78-29 (A)

While power range nuclear instrumentation channel N-44 was in the trip mode due to maintenance, operator attempted to adjust remaining 3 NIS channels in accordance with calorometric data when adjust knob locking device was released. A voltage spike occurred causing a high flux rate trip in channel N-41.

This made up the 2/4 consequence for autor.atic reactor trip.

78-30 (A)

The reactor was manually tripped by the operator from 100%

power due to a loss of cooling water to "A" reactor coolant pump. After the Rx was tripped, the reactor coolant pump was shutdown to preclude pump damage. Subsequent to the occurrence, a section of charging and volume control piping was being returned to service. A drain valva was left open while the piping was pressured. The drain valve allowed water to spray in the vicinity of the containment valve penetration area. 1-TV-CC-102E "A" reactor coolant pump component cooling outlet valve was in the area. 1-TV-CC-102-E went closed at about the same time causing low CC flow alarm alerting the operator. Upon inspection of 1-TV-CC102-E, electricians found a broken mi.cro switch as well as moisture.

I Either problem could have caused the valve to short out and close.

I I

4

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