ML20064B200

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Forwards Special Rept Spr 90-12 Re Fifth Inservice Insp of Steam Generator Tubes,Per Tech Specs 4.4.5.2 & 4.4.5.3
ML20064B200
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 09/21/1990
From: Skolds J
SOUTH CAROLINA ELECTRIC & GAS CO.
To: Ebneter S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
NUDOCS 9010150210
Download: ML20064B200 (33)


Text

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South Carolipe Decific & Gas Company John L. Siolds P O. Don BB V6c3 Prisio;nt j

Jonxinsvita. SC MD65

%cett Operitons j

(833) 3454040 i

SCEAG i

,,en.,

l September 21,1990 90 SEPi5 A10: 50 j

)

l Mr. S. D. Ebneter Regional Administrator U. S. Nuclear Regulatory Commission Region 11 Suite 2900 101 Harietta Street. H. W.

Atlanta, Georgia 30323 J

SUBJECT:

Virgil C. Summer Nuclear Station Docket No. 50/395 Operating License No. NPF-12 Special Report (SPR 90-12)

Steam Generator Tube Eddy Current Examination

Dear Mr. Ebneter:

This report is being submitted in accordance with Technical Specification 4.4.5.5(b).

This inspection constitutes the "Fifth Inservice Inspection" of Steam Generator tubes as required by Technical Specifications 4.4.5.2 and 4.4.5.3.

This report includes the following:

1.

Introduction; 2.

The number and extent of tubes inspected; 3.

Location and percent of wall thickness penetration for each indication of an imperfection; and 4.

Identification of tubes plugged or repaired.

Should there be any questions, please call us at your convenience.

Very truly yours, John L. Skolds ARR/JLS: led Attachments i

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D'. Ebneter I

E iL September 21, 1990 l'

Page 2 of 2

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0. W. Dixon. Jr./T. C. Nichols. Jr.

w/o Attachment 2 l

E.'C.. Roberts w/o Attachment-2 R. V.LTanner w/o Attachment 2 General Managers w/o Attachment 2 l

J. J. Hayes, Jr.

'C. A. Price (w/oAttachment2)

.l R. E. Kelso NCR Resident-Inspector J.lB. Knotts, Jr.

(w/oAttachment2)

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6 Marsh & McLennan Document' Control Desk INPO Records Center ANI Library--

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.. to SPR 90-12 Septsmber 21, 1990 Page 1 of 2 SOUTH CAROLINA ELECTRIC & GAS COMPANY VIRGIL C. SlM4ER NUCLEAR STATION, UNIT 1 JENKINSVILLE, SOUTH CAROLINA 29065 l

STIAM GENERATORS A, 8, & C APRIL 1990 iNTRODUCT10N STEAM GENERATOR TVBE E00Y CURRENT EXAMINATION The fifth inservice eddy current examination of Virgil C. Summer Nuclear Station steam generator tubing was performed during April, 1990.

This I

examination was performed in accordance with the ASME " Boiler and Pressure Vessel Code"Section XI, 1977 edition, through Summer 1978 addenda, and as specified by the Nuclear Regulatory Commission in Regulatory Guide 1.83 Revision 1, dated July 1975.

An examination was performed on all unplugged tubes.

100% of the hot leg l

tubesheet was inspected. Table 1 lists-the number of tubes inspected in each steam generator and the length of tube inspected. The inspection was i

conducted using " state of the art" digital multifrequency bobbin techniques.

1 TABLE 1 l

\\

l -~

S/G S/G S/G A

B C

TEH to 02H 3041 2728 3021 TEH to 14C(Over U Bend) 636 620 638 I

TEH to TEC (Full Length) 717 819 711 Totalinspected RFO 5 4394 4167 4370 l

Previously Plugged 280 507 304 Total Tube Population 4674 4674 4674

-i

.. to SPR 90-12

.Septe:ber 21, 1990 Page 2 of 2 Table 2 summarizes total tubes in each category:

TABLE 2 I

5/G S/G S/G A

B C

mmmmmmme Total number of tubes plugged previously 280 507 304 Number of plugs installed for new indications

  • 88 110 81 Number of F* tubes 132 230 115 Number of tubes repaired (i.e., sleeved) 76 49 0

Total number of tubes now plugged 368 617 385 Percent of total bundle now plugged 7.9 %

13.2 %

8.2 %

i

  • Note: Seven of the tubes (1 A,1 B,5 C)had cabledampersinstalled.

The attached list identifies, by row and column, each tube for which an indication of an imperfection was reported. Recorded next to the row and column number is the resulting disposition for each tube.

For clarification the location codes used are defined as follows:

TEH

=. Tube End Hot Leg TSH Tube Sheet Hot leg

=

-TEC Tube End Cold Leg TSC Tube Sheet Cold leg

=

=

AV#

Anti-Vibration Bar Number

=

(# represents the location on the tube)

Support plate locations are noted by number and the side of the u-tube which contains the indication (e. g., 02H = second support plate on the hot leg side).

Codes used for disposition are as follows:

PLG Plugged

=

F*

F* Applied

=

l AAl Accepted As is

=

l TCD Tube Plugged with Cable Damper Installed

=

NDD No Detectable Discontinuities

=

SLV Sleeved

=

l Note: The list provides the location for the highest degradation found in the tube.

l 1

.s:

' At'tihm'e;t 2 t3 SPR 90-12 V C Summer Station steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location A

9 16 SLV TEH

+ 20.28 40 A

9 19 SLV TEH

+ 17.81 40 A

2 37 SLV TEH

+ 7.95 40 A

8 21 SLV TEH

+ 18.92 40' A

8 23 SLV TEH

+-18.04 40 A

9 21 SLV TEH

+ 19.94 40 A

9 22 SLV TEH

+ 18.94 40 A

23 22 SLV TEH

+ 18.95 40 A

24 21 SLV TEH

+ 17.96 97 A

25 19 SLV TEH

+ 16.97 40 A

7 33 SLV TEH

+ 19.87 40 A

18 66 SLV TEH

+ 18.62 40 A

19 43 SLV TEH

+ 17.85 40 A

19 62 SLV TEH

+ 18.86 67 A

19 66 SLV TEH

+ 18.73 40 A

20 43 SLV TEH

+ 18.78 40 A

24 35 SLV TEH

+ 3.26 40 A

25 55 SLV TEH

+ 17.93 40 A

27 31 SLV TEH

+ 17.90 40 A

28 35 SLV TEH

+ 17.77 40 A

28 39 SLV TEH

+ 17.96 40 A

28 52 SLV TEH

+ 16.98 88 A

28 56 SLV TEH

+ 16.01 40 A

29 64 SLV TEH

+ 15.76 40 A

30 33 SLV' TEH

+ 18.86 40-A 31 31 SLV TEH

+ 17.89 40 A

31 32 SLV TEH

+ 10.10 40 A

33 41 SLV TEH

+ 18.96 40 A

35 31 SLV TEH

+ 16.72 40 A

36 31 SLV TEH

+ 18.77 40 A-36 48 SLV TEH

+ 18.76 92 A

39 42 SLV TSH

+ 0.00 40 A

39 76 SLV TEH

+ 19.95 40 I

A 41 35 SLV TEH

+ 11.10 40 l

.A 41 44 SLV TEH

+ 5.73 50 J

A 41 68 SLV TEH

+ 17.56 43 A

42 33 SLV TEH

+ 18.86.

40 A

43 44 SLV TEH

+ 17.88 57 i

A 44.

37 SLV TSH

+ 0.00 63 A

44 40 SLV TEH

+ 19.83 40 A

44 44 SLV TEH

+ 17.91 70 A-45 47 SLV TEH

+ 18.82 40 A

45 48 SLV TEH

+ 15.88 40 A

48 37 SLV TEH

+ 17.98 40 m

A 9

26 SLV TEH

+ 19.90 40

r i

1 P

Attd;he'nt 2 t2 SPR 90-12 e

V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.-

2 Highest 09/14/90 Reported Percent 8/G Row Column Disposition Degradation Thru-Wall Location A

15 92 SLV TEH

+ 20.09 74 A

18 92 SLV TEH

+ 13.04 40 A

23 89 SLV TEH

+ 19.91 40 A

23 93 SLV TEH

+ 18.87 40 i)

A 34 25 SLV TEH

+ 19.83 40 A

7 29 SLV TEH

+ 18.02 40 A

7 77 SLV TEH

+ 19.08 40 A

18 71 SLV TEH

+ 13.14-40 A

27 73 SLV TEH

+ 19.85 40 A

28 70 SLV TEH

+ 19.78 40 A

28 73 SLV TEH

+ 17.58 82 A-28 74 SLV TEH

+ 19.64 40 A

31 70 SLV TEH

+ 16.82 40 A

33 77 SLV TEH

+ 18.98 40 A

38 71 SLV TEH

-+ 19.91 40 A

43 74 SLV TEH

+ 18.83 40 A

49 73 SLV TEH

+ 18.85 40 A

7 42 SLV TEH

+ 17.06 40 A

9 107 SLV TEH

+ 17.90 40 A

10 42 SLV TEH

+ 5.44 40 A

10 45 SLV TEH

+ 16.98 40 A

10 51 SLV TEH

+ 17.52 87 A

10 52 SLV TEH

+ 19.04 40 A

13 80 SLV TEH

+ 19.74 40 A

17 76 SLV TEH

+ 19.70 40

. A 18 84 SLV TEH

+ 21.12 40 A

30 81 SLV TEH

+ 20.11 47 A

36 79 SLV TEH

+ 11.16 40 A

38 81 SLV TEH

+ 12.97 40 A

43 86 SLV TEH

+ 17.14 44 0 A

7 48 SLV TEH

+ 19.86

-40 I

i i

l

4L*+

Att2hdent 2 t3 SPR 90-12 V C Summer Station an Steam Generator Tube Disposition i

Fifth Refueling Outage j

Page No.

I Highest 09/14/90 Reported Percent i

S/G.

Row Column Disposition Degradation Thru-Wall l

Location i

B 1

68 SLV TEH

+ 16.58 96 B

2 6

SLV TSH

+ 0.03 40 8

2 12' SLV TSH

+ 0.00 40 B

2 62 SLV TSH

+ 0.00 40 t r B-3 68, SLV TEH

+ 19.44 40 p

B 5

63 SLV TEH

+ 17.23 40 B

5 71 SLV TEH

+ 18.29 54 J

B 6

74 SLV TEH

+ 17.03 40 l

B

-7 13 SLV TEH

+ 19.75 40 B-8 68 SLV TEH

+ 18.77 40 8

10 17 SLV TSH

+ 0.00 40

.B 10 18 SLV TEH

+ 18.84 40 B

12 17 SLV TEH

+ 17.92 40 8

12 67 SLV TEH

+ 18.71 40 8

19 21 SLV TEH

+ 17.79 40 l

B

'28 13 SLV TSH

+ 0.00 40 r

B 3

25 SLV TEH

+ 18.83 40 B

3 26 SLV TEH

+ 20.78 40 B

4 22 SLV TEH

+ 19.85 40 B-6 27 SLV TEH

+ 19.74 40 B

9 22 SLV TEH

+ 18.89 40 B

32 22 SLV TEH

+ 18.71 40 B

7 31 SLV TEH

+ 18.91 40 B

10 41 SLV TSH

+

0.00-40 B

12 42 SLV TEH

+ 18.88 74 1

B 15 39 SLV TEH

+ 19.06 40 B

9 77 SLV TEH

+ 19.84 40 B

31 76 SLV TEH

+ 19.83 40 I

B 32 75 SLV TEH

+ 18.88 40 B

6 93 SLV TEH

+ 20.56 40 B

1 87 SLV TEH

+ 19.10 40 B

2 39 SLV TEH

+ 18.57.

'40

'B-3 35' SLV TEH

+ 19.87 40 B'

3 38-SLV TEH

+ 19.93 40-

.B 5

39 SLV TSH

+ 0.00 40 B

5-84 SLV TEH

+ 19.83 40 B

7 83 SLV TEH

+ 17.79 40 B

8 35 SLV TEH

+ 17.22 40 B

10 37 SLV TEH

+ 19.20 40 B-11 38 SLV TSH

+ 0.00 64

'B 13~

34 SLV TEH

+ 16.25 96

-B 13 37 SLV TEH

+ 18.71 40

[

B 15 36 SLV TEH

+ 18.72 40 B

15 41 SLV TEH

+ 19.79 40 8

17 30 SLV TSH

+ 0.00 40 1

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't Att !hniert 2 t3 SPR 90-12 j

.jiYlf.

V C Summer Station l

_1 N.,

Steam' Generator Tube Disposition l

2 ;, "

Fifth Refueling Outage g

t

.s i

^

Page No.

'2 Highest 09/14/90 Reported Percent-S/G Row Column Disposition Degradation

. Thru-Wall i

Location B

28 55 SLV TEH

+ 17.03 40 gh'-

B 29 51 SLV TEH

+ 19.79-40 i

ft B

46 35 SLV TEH

+ 16.56 40 B

49

-39 SLV TEH

+ 18.71 40

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  • e Attdrhment 2 to sPR 90-12 V C Summer Station steam Generator Tube Disposition Fifth Refueling Outage-Page No.

-1 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location A

5 15 PLG TSH

+ 0.00 40 A

6 4

PLO TEH

+ 19.15 40 l

A 6

18 PLG TEH

+ 5.37 79 i

A 6

58 PLO TEH

+ 19.42 40 A

7 14 PLG TEH

+ 18.88 96 A

10 6

PLG TEH

+ 19.80 40 A

13 9

PLO TEH

+ 17.82 40 A

13 12 PLG TEH

+ 19.90 40 A

13 59 PLO TEH

+ 14.85 40 A

22 11 PLO TEH

+ 10.60 88 F

A 24 7

PLG TEH

+ 17.94 76 A

24 8

PLG TEH

+ 18.91 40 A

25 15 PLO TEH

+ 18.90 40 A

27 13 PLC TEH

+ 18.90 40 A

29 11 PLG TEH

+ 19.81 40 A-35 14 PLO TSH

+ 0.00 40 A

3 15 PLO TEH

+ 19.10 53 A

4 20 PLG TSH

+ 0.00 40 A

6 61 PLG TEH

+ 19.83 40 A

6 62 PLG TEH

+ 19.85 40 A

6 65 PLG 02H

+ 0.00 76 A

6 6f PLG TEH

+ 18.76 40 A

6 f7 PLG TEH

+ 19.75 40 A

6 68 PLG TEH

+ 19.74 40 A

6 70 PLO TEH

+ 19.71 40 7

A 7

24 PLG TEH

+ 18.00 40 A

7 62 PLG TEH

+ 19.89 40 A

7 71 PLC TEH

+ 18.81 40 A

8 68 PLG TEH

+ 18.80 40 A

8 73 PLG TEH

+ 19.79 40 A

9 63 PLG TEH

+ 19.49 40 A

11 72 PLC TEH

+ 17.71 40

-A 13 61-PLC TEH

+ 18.73 40 A-13 73 PLG TEH

+ 19.68 40 A

17 69 PLG TEH

+ 19.73 40 A

22

-19 PLC TEH

+ 18.97 40 A

25 23 PLG TEH

+ 15.06 40 A

26 22 PLG TEH

+ 7.63 76 A

30 19 PLG TEH

+ 18.85 40 A

31 22 PLG TEH

+

5.40 40 A

33 20 PLG TEH

+ 19.86 40 A

36 23 PLG TEH

+ 19.89 40 A

38 22 PLG TEH

+ 19.87 40 l

A 40 22 PLG TEH

+ 20.01 40 A-41 21 PLG TEH

+ 18.89 40

e, E

Att$ hment 2 to SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

2

+

Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location A-43 22 PLG TEH

+ 19.86 40 A

7 35 PLG TEH

+ 16.88 40 A

16 41 PLG TEH

+ 15.80 40 A

18 46 PLG TEH

+ 19.96 40 A

19 36 PLO TEH

+ 18.82 40 A

20 62 PLG TEC

+ 18.01 40 A

21 35 PLG TEH

+ 8.34 40 A

21 50 PLG TEH

+ 19.67 40 A

22 31 PLG TEH

+ 17.77 40 A

22 49 PLG TEH

+ 19.79 40 A

29 40 PLG TEH

+ 16.80 40 A

38 33 PLG TEH

+ 18.87 40 A

44 35 PLG TEH

+ 17.11 40 A

47 33 PLG TEH

+ 19.86 40 A

48 75 PLO 06C

+ 0.00 42 A

49 33 PLG TEH

+ 18.93 40 l

A 49 34 PLG 06C

+ 0.00 40 A

49 37 PLO 06C

+ 0.00 40 A

49 39 PLG 06C

+ 0.00 51 A

6 29 PLG TEH

+ 15.37 72 A

13 26 PLG TEH

+ 16.97 55 A

16 95 PLG TEH

+ 19.30 40 l

A 17 92 PLG TEH

+ 19.09 40 A

36 29 PLG TEH

+ 19.93 40 A

39 26 PLC TEH

+ 19.92 40

.l A

41-28 PLC TEH

+ 16.04 40 A

42 28 PLG TSH

+ 0.00 50 j

.A 19 76 PLG TEH

+ 19.83 40 A

2 55 PLG TEH

+ 19.61 40 A

4 42 PLG TSH

+ 0.00 40 i

A 5

56 PLG TEH

+ 18.85 40

'l A

6 55 PLG TEH

+ 19.84 40 A

8 52 PLG TEH

+ 18.96 40 l

A 9

52 PLC TEH

+ 19.86 40 A

13 54 PLG TEH

+ 18.01 65 l

A 14 42 PLG TSH

+ 0.00 40 A

15 49 PLC TEH

+ 19.79 40 A

17 108 PL3 TEH

+ 13.01 82 A

18 88 PLG TEH

+ 19.90 40 i

A 35 100 PLC TEH

+ 19.20 57 A

20 44 PLG TEH

+ 18.69 40 A

47 37 PLG TEH

+ 20.60 26 3

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'+

i Atti;hment 2 tS SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location B

2 3

PLG TSH

+ 0.00 40 B

2 64 PLG TEH

+ 15.59 40 B

3 4

PLO TSH

+ 0.00 40 B

3 64 PLC TEH

+ 12.19 40 8

4 73 PLG TEH

+ 18.95 98 B

5 4

PLG TSH

+ 0.00 40 B

5 7

PLC TSH

+ 0.00 40 B

5 60 PLG TSH

+ 0.00 40 B

5 64 PLO TEH

+ 4.74 69 B

10 64 PLG 02H

+ 0.00 73 B

11 6

PLG TSH

+ 0.00 40 B

11 60 PLG TEH

+ 18.82 40 B

12 2

PLC TSH

+ 0.00 40 B

16 5

PLG TEH

+ 20.07 41 B

18 6

PLC TSH

+ 0.00 50 B

19 18 PLG TEH

+ 21.20 40 B

20 9

PLC TSH

+ 0.00 40 B

21 5

PLC TSH

+ 0.00 40 B

21 8

PLG TSH

+ 0.00 40 B

26 15 PLG TSH

+ 0.00 40 B

30 15 PLO TEH

+ 19.98 40 B

32 21 PLG TEH

+ 18.82 40 B

35 19 PLG TSH

+ 0.00 40 B

38 21 PLC TEH

+ 17.84 40 B

9 27 PLC TEH

+ 19.84 40 B

22 24 PLG TEH

+ 14.70 40 B

27 22 PLC TSH

+ 0.00 40 B

30 23 PLO TEH

+ 17.96 40 B

33 23 PLG TEH

+ 18.00 40 B

44 24 PLG TSH

+ 0.00 40 B

44 25 PLC TEH

+ 20.91 40 B

20 43 PLC TEH

+ 18.85 40 B

29 44 PLC TSH

+ 0.00 40 B

40 43 PLO TSH

+ 0.00 40 B

44 44 PLG TEH

+ 19.85 40 B

26 58 PLC TEH

+ 16.16 40 B

27 57 PLG TEH

+ 15.30 40 B

28 57 PLG TEH

+ 18.11 40 B

31 56 PLG TEH

+ 16.02 40 B

31 57 PLG TEH

+ 18.96 40 B

33 57 PLG TEH

+ 19.91 40 B

47 57 PLG TEH

+ 15.20 40 B

12 77 PLG TEH

+ 19.90 40 B

22 79 PLG TEH

+ 14.86 40 B

24 77 PLC TEH

+ 18.84 40 1

'o Atti:hment 2 t9 SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage l

Page No.

2 Highest 09/14/90 Reported Percent

$/G Row Column Disposition Degradation Thru-Wall Location

-2 26 77 PLG TEH

+ 18.83 40 B

27 79 PLG TEH

+ 12.27 79 B

6 92 PLG TEH

+ 18.88 40 8

35 98 PLO TEH

+ 19.04 53 B

36 89.

PLO TEH

+ 20.27 46 B

2 44 PLG TSH

+ 0.00 40 B

2 45 PLC TSH

+ 0.00 40 B

2 46 PLC TSH

+ 0.00 40 i

B 2

50 PLG TSH

+ 0.00 40 B

3 51 PLG TSH

+ 0.00 40 B

4 100 PLG TEH

+ 20.89 50 B

6 49 PLG TEH

+ 19.92 40 B

6 100 PLC TEH

+ 19.77 40 0

6 104 PLG TEH

+ 15.92 40 8

9 49 PLG TEH

+ 18.80 40 B

10 55 PLG TEH

+ 17.72 40 B

12 50 PLG TEH

+ 17.73 40 B

23 109 PLG TEH

+ 16.37 45 B

25 108 PLC TEH

+ 18.03 40 B

26 100 PLG TEH

+ 15.75 40 B

6 83 PLC TEH

+ 15.75 75 B

10 31 PLG 02H

+ 0.00 69 B

17 28 PLG TEH

+ 20.40 40 B

19 61 PLG TEH

+ 17.80 40 B

19 67 PLO TEH

+ 18.76 40 B

22 31 PLG TSH

+ 0.00 40 B

23 84 PLG TEH

+ 19.77 40 B

24 51 PLG TEH

+ 18.87 40 B

25 35 PLG TEH

+ 19.75 40 B

28 70 PLG TEH

+ 17.10 40 B

28 86 PLG TEH

+ 18.83 40 B

29 48 PLO TEH

+ 14.89 40 B

30 39 PLG TSH

+ 0.00 40 L

B 32 29 PLG TEH

+ 19.49 61 B

33 35 PLG TEH

+ 16.85 40 B

33 70 PLG TEH

+ 13.83 40 B

34 51 PLG TEH

+ 21.05 40 B

35 35 PLG TEH

+ 17.77 40 B

36 53 PLG TSH

+ 0.10 40 B

36 79 PLG TEC

+ 18.07 40 B

38 45 PLC TEH

+ 17.91 40 L

B 39 48 PLG TEH

+ 19.84 40 l

B 40 66 PLG TEH

+ 19.30 40 1

B 40 68 PLG TEH

+ 20.00 40 B

40 69 PLG TEH

+ 16.73 40

q -+

q l

)

' s 1

Attdthment 2 to SPR 90-32 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage t

Page No.

3 Highest 09/14/90 Reported Percent j

S/G Row Column Disposition Degradation Thru-Wall Location B

42 33 PLG TEH

+ 20.21 53 B

43 40 PLG 02H

+ 0.00

'60 B

43 55 PLG TEH

+ 20.13 93 I

B 44 30 PLG TEH

+ 19.80 40 B

45 29-PLG TEH

+ 16.91 40 B:

46 33 PLC TEH

+ 16.80 40 B

47 56 PLG TEH

+ 18.10 40 B

48 48 PLG-TEH

+ 15.52 40.

[

- B 48 52 PLC TEH

+ 16.80 40 B-48 53 PLG TEH

+ 18.25 65 B

49 38 PLG TEH-

+ 12.17 40

. B:

49 79 PLG OBC

+ 0.00 47 B

31 60 PLG TEH

+ 19.30' 39 B

37 59 PLC TEH

+ 20.80 22 B

25 55 PLG TSH

+ 0.95 15

- B 5

106 PLG 02H

+ 0.00 37 B

32 79 PLG OSH

+ 30.82 19 B~

49 80 PLG 08C

+ 0.00 36 B

7-9 PLG TEH

+ 16.01 66 s

I

(

I i

1 ts I

Attfchmant 2 ts SPR 90-12 p

V ~ C Summer Statio:4 Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 l

' Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location C

3 5

PLG TEH

+ 19.95 40 C

3 6

PLG TEH

+ 19.84 40 C

3 11 PLG TSH

+ 0.00 40 C

3

'71 PLG TEH

+ 19.83 40 C

4 7-PLO TEH

+ 19.86 40 C

4 37 PLG TEH

+ 18.84 40 C-5 6

PLO TEH

+ 20.05 40 C

6 89 PLG TEH

+ 19.17 40 C

8 7

PLG TEH

+ 19.95 40 C

-9 2

PLG TEH

+ 18.00 40 C

9 4

~ PLG TEH

+ 19.89 40

-C 9

13 PLG TEH

+ 17.92 40

_ {

ic 9

7 PLG TEH

+ 16.06 40 C

11-9 PLG TEH

+ 16.99 40 C

11 70 PLG TEH

+ 19.83 40 C

12 13 PLG TEH

+ 19.20 40 I

C-13 11 PLG TEH

+ 18.80 40 C

14 94 PLG TEH

+ 15.93 40

[

C 28 15 PLG TEH

+ 18.87 84 j

C 18 37 PLG TEH

+ 12.97 40 C

3 27 PLG TSH

+ 0.00 40 C

5 22 PLG TEH

+ 19.99 40

~!

I C

5

'31 PLG TEH

+ 20.23 40 C

6 24 PLG TEH

+ 19.95 40 i

C 7.

20 PLG TEC

+ 17.93 40 C

11 16 PLG TEH

+ 18.02 40 C-

'12 31 PLG TEH

+'18.88 40 C

13 21 PLG TEH

+ 19.83 40

~{

C 13' 36 PLG TEH

+ 18.77 40 C

21 20 PLG TEH

+ 19.97 40 C

24' 19 PLG TIH

+ 18.99 40 C

29 25 PLC TEH

+ 21.10

.40 C

30 30 PLG TEH

+ 21.10 40 l

C 34 31 PLG TEH

+ 20.05 4'O C

35 20 PLG TEH

+ 15.28 40 C

37 31 PLG TEH

+ 19.91 40 C

38 19 PLG 02H

+ 0.00 52 C

41

'21 PLO TSH

+ 0.00

'40 DC 24 41 PLG TSH

+ 0.00 40 C'

24

'42 PLG TSH

+ 0.00 40 C

5 82 PLG TSH

+ 0.00 40 1

C 8

81 PLG TEH

+ 19.77 40 C

11 83-PLG TEH

+ 19.24 40 C

16

~83 PLG TEH

+ 16.06 40 C

20 47 PLG TEH

+ 18.82 40 i

o ;.

t t

l l

5, m

I Attdchment'2 to'SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage

'Page No.-

2 Highest 09/14/90-

. Reported-Percent S/G Row Column Disposition Degradation Thru-Wall I

Location C

28 50-PLG TEH

+ 16.71 40 C

34 53 PLO TEH

+ 18.83 40 C

40 57-PLG TEH

+ 18.99 40 C

40' 58 PLG TEH

+ 19.09 83

-C 42 48 PLG TEH

+ 20.16 40 C

43 48 PLG TEH

+ 17.10 40 C

3 43 PLG TEH

+ 19.19 40 C

3 45 PLG TEH

+ 19.98 40 C

6 111 PLG TSH

+ 0.00 40 C

7 45 PLG TEH

+ 21.17 40 C

7 55 PLG TEH

+ 17.89 40 C

9 48 PLG TSH

+ 0.00 40 t

.c 10 43 PLG TSH

+ 0.00 40 C

10 50 PLG TEH

+ 20.05 53 C

12 42 PLG TEH

+ 19.87 40 C

13 46 PLG TEH

+ 18.84 40 C

14 47 PLG TSH

+ 0.00 40 C

14 74 PLC TEH

+ 18.84 40 C

18 71 PLG TEH

+ 19.16 40 i

C 19 69 PLG TEH

+ 20.22 40 C

20 101 PLC TEH

+ 19.83 40 l

C 21 71 PLG TEH

+ 18.70 40 C

23 75 PLG TEH

+ 20.94 40 C

24 71 PLG TEH

+ 18.85 40 C

42 71 PLG TEH

+ 19.06 40

-C 33-100 PLG 02H

+ 0.00 80 JC 1

28 PLG TEH

+ 18.11 40 C

2 54 PLG TEH

+ 19.08 40 C

3 17 PLG

-TSH

+ 0.00 40 C

4 54 PLG TEH

+ 18.91 40 C

22 27 PLG TSH

+ 0.00 45 P

.[

1 a

r

'l

'Attsshment:2 to SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reported Percent S/O.

Row Column Disposition Degradation Thru-Wall Location A

3 10 F*

TEH

+ 17.92 40 A

3 17 F*

TEH

+ 15.01 40 A

5 7

F*

TEH

+ 17.81 40 A

6 8

F*

TEH

+ 16.93 40 A-6-

15 F*

TEH

+ 17.97 40-A 7

60 F*

TEH

+ 5.05 82 A

8 59 F*

TEH

+ 17.85 40

-A 11 60 Fa TEH

+ 15.85 40 A

13 19 F*

TEH

+ 11.40 40 A

13 50 F*

TEH

+ 13.02 40

'I A

13 11 F*

TEH

+ 15.93 40 A

17 58 F*

TEH

+ 17.90 40 A

23 11 F*

TEH

+ 13.44 40 A

28 17 F*

TEH

+ 12.88 40 A

1 6

F*

TEH

+ 6.90 94

[

-A 2

11 F*

TEH

+ 2.11 83 A

- 2 36 F*

TEH-

+ 8.36 40 l

A 3

36 F*

TEH

+ 11.02 40 A

- 9 72 F*

TEH

+ 17.70 40'

-A 10 20 F*

TEH

+ 14.18 40 A

13 69 F*

TEH

+ 10.72 40 A

15 61 F*

TEH

+ 17.77 40 i

A-17 23 F*

TEH

+ 4,40 40 A

17 64-i*

TEH

+ 18.82 40 A

20 20 F*

TEH

+.14.05 40 i

'A' 27 21 F*

TEH

+ 12.13 40 A

31 19 F*

TEH

+ 5.45 96

-A 33-21 F* -

TEH

+ 17.85 40 A

34 19 F*

TEH

+ 16.05 94 A

- 36 22 F*

TEH

+ 16.97 40 A

39-24 F*

TEH

+

2.47' 40 A

41 24 F*

TEH

+ 15.03 40

.A 6

38 F*

TEH

+ 10.06 40 A.

7 30 Fa

~TEH

+ 17.02 40

-f A

8 38 F*

TEH

+ 18.39 40

?

F A

' 9 36' F*

TEH

-+

1.94 40

' ll 75 F*

TEH

+ 16.92

-41 JL Al

- 12 32 F*

TEH

+ 18.87 40

~

A 12 35 F*

TEH

+ 15.96 40 py

-- A 19 61 F*

TEH

+ 14.81' 40 3

A 20 31 F*

TEH

+ 17.83 40

.A-20 39 F*

TEH

+ 12.97 40 A

20 51-F*

TEH

+ 17.82 40 A

20 64 F*

TEH

+

5.00 72 1

A 23 49 F*

TEH

+ 18.77 40 e

c iI t

V

[

~ Attdchment'2 to SPR 90-12 V C Summer Station.

Steam Generator Tube Disposition Fifth Refueling Outage l-1 Page No..

2 Highest 09/14/90 Reported Percent S/G Row -Column Disposition Degradation Thru-Wall Location A

23 59 F*

TEH

+ 17.63 40 A

24 52 F*

TEH

+ 17.84 72 A

24 64 F*

TEH

+

6.02 53 A

25 46 F*

TEH

+ 15.83 78 A

26 30 F*

TEH

+ 17.10 40 A

26 31 F*

TEH

+ 11.82 40 A'

26 42 F*

TEH

+ 4.09 40 A

27 30 F*

TEH

+ 16.20 40 i=

A.

27 32 F*

TEH

+ 12.99 40 A

27 52 Fa TEH

+ 16.04 66

.A 27 53 F*

TEH

+ 15.10 57 A

28 49 F*

TEH

+113.89 40 i

A 28 58 Fa TEH

+ 18.70 40 A

29 31~

F*

TEH

+ 16.80 93 A

29 43 F*

TEH

+ 14.86 40 A-29 65 F*

TEH

+

6.01 75 A

30-35-F*

TEH

+ 12.19 40 A

30 46 F*

TEH

+

5.29 52 A

31 52 F*

.TEH

+ 14.06 40 A

31 56 F*

TEH

+ 4.72 50 A

32 34 F*

TEH

+ 13.89 40 A

32 38 F*

TEH

+ 13.61 40 A

32 47 F*

TEH

+ 17.79 70 A

32 48 F*

TEH

+ 16.75 40 A

'32 52 RF

  • TEH

+ 17.99 77 A

132 64 F*

TEH

+ 17.60 89-

A 33 30 F*

TEH;

.4.15.80-40 A

'33 40 F*

TEH

+ ' 6.99 40 i

'A.

34-

-48 F*

TEH

+ 15.71 40 A

35 48 F*

TEH

+ 17.83 40-

'A 37-57 F*

TEH

+ 17.74 40 A

38 41 F*

TEH

+ 15.92 82 A

39 33 F*

TEH

+ 15.89 40 A

'39 49 F*

TEH

+

8.90' 40 A

39<

53 F*

T'EH

+ 17.95 40 A

40 42 F*

TEH

+ 15.03 40 A

46

.65' F*

TEH

+

8.42 93 i

A' 47 87 F*

TEH

+ 16.03 40

~A 13 27-F*

TEH

+ 12.78 75 f

A 24 18 2 F*

TEH

+ 17.69 40

-5 26 F*

TEH

+ -7.34' 40 A

A-

'15 98 Fa TEH

+ 17.16 91 L

A

' 19 -

-29 F*

TEH

+

8.59 85 A

21 28 F*

TEH

+ 12.10 40 l

L' A

41 25 F*

TEH

+ 11.92 94 L

.x y

~N

= Alt $chment 2 to SPR-90-12 V C Summer Station steam cenerator Tube Disposition Fifth Refueling Outage Page No.

3 Highest 09/14/90 Reported Percent s/G Row Column Disposition Degradation Thru-Wall Location A

41 93 F*

TEH

+ 6.52 40 A

41 95 F*

TEH

+ 14.08 75 A

43 25 F*

TEH

+ 16.03 40 A

44 26 F*

TEH

+ 14.01 40 A

3-26 F*

TEH

+ 8.37 40.

A' 5

77 Fa TEH

+ 16.52 40.

A 23 76 F*

TEH

+ 17.79

.40 A

24 69 F*

TEH

+ 9.15 58 A

27 70 F*

TEH

+ 15.77 40 A

29 68 F*

TEH

+ 15.70 95 A

39 71 F*

TEH

+ 16.92 40 A

39 77 F*

TEH

+ 17.86 94 A.

40 69 F*

TEH.

+ 11.65 86 A

40 72-F*

TEH

+ 16.03 40 A

41 71 F*

TEH

+ 18.92 90

. A 43 73 F*

TEH

+ 12.34 86 i

A 43 77 F*

TEH

+ 13.13 40 I

A 45 78 F*

TEF

+ 14.08 40

. A 47 72 F*

TEV1

+ 9.17 40 A

48 74 F*

TEH

+ 16.86 82 A'-

6 47 F*

TEH

+ 9.47 53

-l A

6

'79 F*

TEH

+ 11.36 61.

A 7-51 F*

TEH

+ 17.12 40 A

9 48 F*

TEH

+ 1.85 62 A

- 12 51 F*

TEH

+ 17.83 40 i

A 12 52.

F*

TEH

+ 16'.76 40 L

A

. 13 46 F*

TEH

+ 3.40 99 A

19 84 F*

TEH

.+. 7.18 40 A

~3 5 84 F*

TEH

+ 12.32 40 A.

' 35-86 F*

TEH

+ 12.09 97.

A-35 101 F*

TEH

+ 18.07 98 A

42 83.

F*

TEH

+ 16.85-69 4.5 A

43 82 F*

TEH

+ 14.92 63 K

A 14 7 83 F*J TEH

+ 16.20 68 AL 49 82 F*

TEH

+ 13.28 64 A

. 5-23 F*

TEH

+ 6.20 42

- A 8

58 F*

TEH

+ 15.55 85 U

A' 24 44 F*

TEH

+ 18.71 40

- A

- 26 38 F*-

TEH

+-18.79 90 l

A 27 44 F*

TEH'

+ 14.88 40 A'

29-38 F*.

TEH

+ 16.85 85 A

45 37 F*

TEH

+ 4.34 40 L'

e I

i

i Attdchment'2'to'SPR190-12 V C Summer Station.

Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reported Percent-S/G Row Column Disposition Degradation Thru-Wall Location B.

2 60 F*

TEH

+-16.81 71 B

2 75 F*

TEH

+ 17.97 40

'B 3

69 F*

TEH

+

3.17 94 B

3 70 F*-

TEH

+ 5.28 85 B

3 71 F*

TEH

+ 6.13 75 I

B 72 F*

TEH

+ 3.20 60 B-4 63 F*

TEH

+ 16.49 40 B

4 65 F*

TEH

+

6.07 40 B

4 67 F*

TEH

+ 15.88 90 B

4 74 F*

TEH

+ 5.75 60 B

5 62 F*

TEH

+ 11.89 82 B

5 65 F*

TEH

+ 18.89 84 B

5 75=

F*

TEH

+ 12.70 40 i

B 6

64 F*

TEH

+

6.43 60

'B 6

66 F*

TEH

+

4.89 66

'B 6

67 F*

TEH

+ 3.51 45 B

6 72 F*

TEH

+

6.88 67 B

7 5

F*

TEH

+ 18.80 40 B

8 69 F*

TEH

+ 17.93 40 B

9_

21 Fa TEH

+ 11.50 40 B

11' 21 F*

TEH

+ 14.82 40 B

12 20 F*

TEH

+ 13.89 40 B-15 17 F*

TEH

+ 17.92 40 B

15.

.19 F*

TEH

+ 17.85 40 B

15 64 F*

TEti

+ 12.19 40 B

16 16 F*-

TEH

+ 17.10

'40 B

17 10 F*

TEH

+ 15.85 40 B

17 12 F*

TEH

+ 14.87 40 B.

17 14 F*

TEH

+ 15.86 40 B

17 16 F*

TEH

+ 12.07 40 B

18 8

F*

TEH

+ 16.91 40 B-

. 18.

9 F*-

TEH

+ 15.75 40=

q B

18 11 F*

TEH

+ 14.83 40 F

B 19 10 F*

TEH

+ 16.82 40 B'

- 19 19 F*

TEH

+ 16.80 49 B

20 20 F*

TEH

+ 13.93 40' l

B-21 17 F*

TEH

+ 16.91 40 Bs 21 18 F*

TEH

+ 16.76 40 B

21 20 F*

TEH

+ 18.80' 40

.B 24 8

F*

TEH

+ 2.33 72 B

. 24 9

F*

TEH

+ 1.39 97 B

24 15 F*

TEH

+ 15.31 40 B

24

.2-0 F*

TEH 1.44 63 D

25 8

F*

TEH 13.73 40 B'

25 19 F*

TEH

+ 14.86 40 t

4 h

9 f '

E.

"4;.

Attdshment 2 to SPR ^0-12

- + -

V C Summer Station steam Generator Tube Disposition Fifth Refueling Outage.

Page No.

2 Highest 09/14/90 Reportedu Percent S/O Row Column Disposition Degradation Thru-Wall Location B

26 14 F*

TEH

+

2.22, 16 4 B

26 16 F*

TEH

+ 2.26 91

-l B

27 1M)

F*

TEH

' + 1.44 75 l

B 27 21 F*

TEH

+ 14.19 40

- B 30 20 F*

TEH

+ 17.84 40 B

31 15 F*'

TEH

+ 15.02 40

. B 31 17 F*

TEH

+ 16.86 40 k

'B 34 17 F*-

TEH

+ 2.24 72 B

35 21 F*

TEH

+ 15.95 40 B

36 21 F*

TEH

+'16.93 40 B

3 24 F*

TEH

+ 16.11 40

.i B

10 24 F*

TEH

+ 16.97 40 B

10 27 F*

TEH

+ 15.87 40 B

11 25 F*

TEH

+ 13.26 78 B

12 25.

F*

TEH

+ 5.35 89 B

13 25 F*

TEH

+ 18.24 40 k

B 15 24 F*.

TEH

+ 14.06 40 B'

15 26 F*

TEH

+ 15.84 40 i

B 15 27 F*

TEH

+ 12.19 61

.i B

21 24 F*

TEH

+ 14.13 40

.B 24'

.2 6 '

F*

TEH

+ 16.85 40 B

25 24 F*

TEH

+ 14.77 95 LB 27 26 F*

TEH

+ 11.90 40 B

~30 25 F*

TEH

+ 16.88' 40.

B-30 26 F*

TEH

+ 18.81 40 B.

31 23 F*'

TEH.

+ 17.95 40 B

31 24

-F*

TEH

' + 16.68 40 B

31 27 F*

TEH

+ 14.09

-40 a

+

B-32' 25 F*

TEH

+=16.26 53-B 32 26 F*

TEH

+ 13.69 40 B

33-26

.F*

TEH

+ 14.05 40 B.

37

26 F*

TEH

+ 15.15 46 B.

38 26 F*

TEH

+ 14.94 40 B.

6 30 F*

TEH

+ 16.74 40 N

til B-6 40 F*

TEH

+ 14.49 40 B-

.7 41 F*

TEH

+ 18.91 40 LB B

31-F*

TEH

+ 18.76 40 B-11 40 F*

TEH

+ 18.80 65 L

i B --

20 39 F*

TEH

+ 11.05 40 B-20 41 F*

TEH

+ 17.85 65 B

21' 42 F*

TEH~

+ 17.70 40 B

.B 29 40 Fa TEH

+ 15.14 40 B

30 41 F*

TEH

+ 8.22 81 B.

33 40 F*

TEH-

+ 17.84 80 B

33 41 F*

TEH

+ 16.72 40

-\\

.3 -

R

1 P

e.,

Attdchment 2 to'SPR'90-32 n

V C Summer Station:

Stene. Generator Tube Disposition

)

Fifth Refueling Outage Page No.

3 Highest 09/14/90 Reported Percent S/G-Row Column Disposition Degradation Thru-Wall I

Location B

33 43 F*

TEH

+ 12.23 40 B

34 40 F*

TEH

+ 2.94 60 B

34 43-F*

TEH

+

1.70 60 B

35 44 F*

TEH

+

1.23 66 8

36 44 F*

TEH

+

1.10 87

~B 37 42 F*

TEH

+ 11.54 48 B

40 44 F*

TEH

+

7.96 79 B

42 43 F*

TEH

+ 14.33 52 B

42 44 F*

TEH

+ 16.84 87 B

49 43 F*

TEH

+ 16.10 40-B 23 62 F*

TEH

+ e5.10 40 B

27 58 F*

TEH'

+ S.42 40 B

28 58 F*

TEH

+ 16.11 40

[

B 32 57.

F*

TEH-

+ 12.25 40 B

32 62 F*

TEH

+

7.80 63 Ji B

33 61-F*

TIM

+ 16.;J 61 B

.34 58 F*

TEH

+ 18.28-40 B-37-60 F*

TEH

+.4.99 53 B

40 62 F*

TEH

+ 16.13 40 i

B 4

79 F*

TEH

+ 9.28 40 B

17 79 F*

TEH

+ 11.06 40 8

23 79 F*

TEH

+ 4.21 78 B

39 78 F*

TEH

+ 1.82 95 B

10 99 F*

TEH

+

4.43 82 B

27' 89 F*

TEH

+ 13.07 98, B

2 30 F*

TEH

+

8.99 40 B-2 35 F*

TEH

+ 16.69 40-B 4

76 F*

TEH

+

8.01-87 B

2

-57 F*

TEH

+ 18.92 40-B 2

58 F*

TEH

+ 18.94.

75

[

B 7-44 F*

TEH-

+

7.53 59

'i B

7 53 F*

TEH

+ 18.71 40 i

B 7

56 F*

TEH

+ 14.81 40 B'

8 59 F*

TEH

+ 16.66 40 B^

10 57 F*

TEH

+ 18.76 40

[

B 10 103 F*

TEH

+

5.97 93-B 11-19 F*

TEH

+ 16.64~

40 B-11-30 F*

TEH

+ 17.65 40 l

B 11 54 F*

TEH

+ 15.65~

40 L

B 11L 55 F*

TEH.

+ 16.04 59 B'

11-56 F*

TEH

+ 10.16 56 B

11 57-F*

TEH

+ 14'.93 40.

_l B'

11 59 F*

TEH

+ 17.66 40 B

'11 104 F*

TEH

+ 10.14 93 B'

12 49 F*

TEH

+ 17.88 60 ll 4

4

1 i

,q.'*

e Attdchment-2 to OPR 90-12 L

V C Summer Station

,j Steam'Genecator. Tube Disposition l

Fifth Refueling Outage Page No.

4 Highest 09/14/90-Reported Percent s/G Row Column Disposition Degradation Thru-Wall Location

B 12 52 F*

TEH

+ 13.65 40 B

12 53 F*

TEH

+ 13.74 40 B

14 55 F*

TEH

+ 14.16 88 B

14 56 F*

TEH

+ 14.76 45 B

15 48 F*

TEH

+ 15.68-40 B

'15 49 F*

TEH

+ 17.67 88 B

15 52 F*

TEH

+ 15.45 40 B

15 53 F*

TEH

+ 17.79 40 B

'16 44 F*

TEH

+ 16.93 40 B

-16 52 F*

TEH

+ 14.90 46

~B 16 53 F*

TEH

+ 17.68 40

-B 16 58 F*

TEH

+

2.75-89

-4

-B

~2 2 100 F*

TEH

+

5.71 82 B

27-107 F*

TEH

+ 2.56 60 B-7 35 F*

TEH

+ 13.61 93 D

7 37

'F*'

TEH

+ 17.70 61 B

8 33 F*

TEH

+ 4.32 40 t

B-9 32 F*

TEH

+

8.07 40 B

11 37 F*

TEH

+ 18.81 40 B

12 32 F*

TEH

+ 7.56 81 B-13 28 F*

TEH

+ 7.47 44

.B-13 30 F*

TEH

+ 17.92 40

~B 19-75 F*

TEH

+ 19.36 40 B

20 45-F*

TEH

+ 12.91 40 B

20' 51 F*

-TEH

+ 16.00 40 B

20 65 F*

TEH

+ 18.68 40-B 21 31-F*

TEH

+'15.85 40.

B 21 36 F*

TEH

+ 17.69 40 B

21-39 F*

TEH

+ 11.99 40

-B 21 51 F*

TEH

+ 17.91 40 B'

22 33 F=

TEH

+ 17.95 40 B

23 28-F*

TEH

+ 17.80-40

'B' 23 50 F*

TEH

+ 16.03 40 B'

.24 30 F*

TEH

+ 15.79 40 B-24 34 F*

TEH

+ 11.92 40

B!

24-37 F*

TEH

+ 18.84 40 i

~

27 74 F*

TEH

+ 17.04 40 B

B' 28 28 F*-

.TEH

+ 12.11 95 0:0 B

28 47 F*

TEH

+ 10.99 40 B

28 69 F*

TEH

+ 16.63 40 B

29 28 F*

TEH

+ 11.22-66 B

=29 33 F*

TEH

+ 16.91 40 B

30 37 F*

TEH

+

7.65 76 B

31 31 F*

TEH

+ 13.12 98 L

B 31 37 F*

TEH

+ 10.74 76 l-l-

i p

l'

_ _l

=,

'AttCchment 2 to'SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

5 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location B

31 46-F*

TEH

+ 14.77 61 B

31 55 F*

TEH

+ 12.22 78 8

31 63 F*

TEH

+ 15.30 71 9

31 65 F*

TEH

+ 11.98 84 8

32 27 F*

TEH

+ 16.80 40 B

32 31 F*-

TEH

+ 2.04 96 B

32 33 F*

TEH

+ 11.26 65 B

13 2 63 F*

TEH

+ 13.06 70 B

33 29 F*

TEH

+ 3.25 98 8

33 30 F*

TEH

+ 14.04 40 B-33 31 F*

TEH

+ 17.90 40 B

33 32 Fa TEH

+ 17.98 40-B 33 34 F*

TEH

+ 15.95 40 B

33 50 F*

TEH

+ 8.34 40 B

33 52 Fa TEH

+ 12.33 43 B

34 30 F*

TEH

+ 18.88 50 B

34 33 F*

TEH

+ 18.96 40 B

34 34 F*

TEH

+ 18.09 40 B

34 36 F*

TEH

+ '2.30 53 B

34 38 F*

TEH

+ 1.27 70 B-34 64 F*

TEH

+ 18.79 40 B

34' 72 F*

TEH

+ 13.13 62 B-35-30 F*

TEH

+ 1.30 52 B

35

'38 F*

TEH

+ 3.32 79 B

36 32 F*

TEH

+

8.12 a64 B

36 37 F*

TEH

+ 1.22 76 B

36 47

'F*

TEH

+ 13.10 40 8

36 48 F*

TEH

+ 14.89 40 D

37 49 F*

TEH

+ 3.40 66 B

37 56 F*

TEH

+ 12.23 40 B

'37 71 F*

TEH

+

9.'26 86 B

37 72 F*

TEH

+ 12.80 40 B~

38 46 F*

TEH-

+ 16.96 40 r

B 40 46 F*

TEH

+ 1.60 75 B

40 67 F*

TEH

+ 17.00 100 B

<4 'O 71 F*

TEH

+ 16.72 70 B

42 39 F*

TEH

+118.66 40 8-42 41 F*

TEH

+ 14.87 40 B

44.

35 F*

TEH

+ 11.17 40 B

44 42 Fa TEH

+ 18.83 94 B

46:

80 F*

TEH

+ 4.22 40 B

-47 33 Fa TEH

+ 2.67 40 B

47 49 F*

TEH

+ 15.51 41 B

48 34 F*

TEH

+ 18.10 50 B

48 42 F*

TEH-

+ 7.26 40

," g.'e-Attdchment 2 to SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

6 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall Location B

49 37 F*

TEH

+ 6.19 40

-B 49 47 F*

TEH

+ 11.00-40 B

49 51 F*

TEH

+ 8.10 40 B.

25 56 F*

TEH

+ 9.86 40 B

32 59 F*

TEH

+ 15.80 40 i

1 s

f i

\\

- n f

f

)

ap

- ; ;,, - n; I

Atidchment 2 ta'SPR 90-12 V C Summer Station Steam Generator Tube Disposition Fifth' Refueling Outage-Page~No.

1 Highest 09/14/90 Reported Fercent S/G Row Column Disposition Degradation Thru-Wall Location C

1 17 F*

TEH

+ 14.86 89 C

1 64 F*

TEH

+ 4.88 81 C

1 68 F* -

TEH

+ 6.68 40 C

3 73 F*

TEH

+ 18.94 40 C'

3 93 F*

TEH

+ 15.45 97 C

4 5

F*

TEH

+ 18.03 40 C-4 15' F*

TEH

+ 13.09 40 C

4 94 F*

TEH

+ 2.09 86 C

5 13 F*

TEH

+ 18.85 40 C

.6 14 F*

TEH

+ 11.94 67

. c 6

15 F*

TEH

+ 14.01 74 C

-8 67

.F*

TEH

+ 18.26 53 C

11 5

F*

TEH

+ 16.93 40 C

11-10 F*

TEH

+ 15.95 40 r

C.

12 10 F*

TEH

+ 16.02 40 C

13 3

F*

TEH

+ 18.86 40 C

11 3 7

F* '

TEH

+ 13.11 40 C

13 88 F*

TEH

+ 16.91 40 C

16 9

F*

TEH

+ 9.35 40 C

E16 38 F*

TEH

+ 14.50 40 C

17 7

F*

TEH

+ 16.03 40

.i

' C 17 13

F*

TEH

+ 18.87 40 i

C 17 37 F*

TEH

+ 13.97 40 C

.18 12

'F*

TEH

+ 16.88 40 C

19 9

F*

TEH

+ 17.90 40 C

21 5

F*

TEH

+ 17.92 40 C.

31 37 F*

TEH

+ 14.50 40 C

32 14 F*

TEH

+ 15.86 40

' C-47 87 F*

TEC

+ 3.94 93 l

. c

-5 19 F*

TEH

+ 18.99 40' l'

C 6

19 F*

TEH

+ 18.94 40 C

7 35 F*

TEH

+ 11.30 40 C

8 20 F*

TEH

+ 18.97-40 C

8 25 F*

TEH

+ 17.98-4l0 L

C 9.

22 F*

TEH

+.17.74 40 C

9 36 F*

TEH

+ 14.97 40

. c 11 17 F*

TEH

+ 15.82 40 l

C 11-F*

TEH

+ 18.19 40 1

C-13 17 F*

TEH

~ + 14.98-40 C-13 25 F*

TEH-

+ 15.13 40 sm ;

C 14 26 F*

TEH

+ 17.09 40 C

15 20-F*

TEH

+ *6.86 40

' C; 18:

18 F*

TEH

+ 13.20 40 j,

C 19-18 F*

TEH-

+ 19.30 40

. C

19 f20 F*

TEH

+ 13.16 40 U

{

i 4

8 g

+

4

1

]

,1 o

'Att$chmont 2 to SPR'90-12 4

V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.;

2 R

Highest 09/14/90 Reported Percent S/G.

Row Column Disposition Degradation Thru-Wall Location C

20 29 F*

TEH

+ 17.98 40 C

20

-30 F*

TEH

+ 14.11=

40 C-20 31 F*

TEH

+ 2.27 40-C.

22 25 F*

TEH

+ 14.30 40 C

25 30 F*

TEH

+.15.82 40 C

26 25 F*

TEH

+ 18.18 40 C~

32

,22 F*

TEH

+ 17.95 40 C

32 25 F*

TEH

+ 14.60

-40 C

32 30 F*

TEH

+ 15.03 40 C

32 34-F*

TEH

+ 12.10 40 C

32 35 F*

TEH

+

7.55 40 C

35 18 F*

TEH

+ 16.00 40 C

35 31 F*

TEH

+ 18.03 40 1

C 35 35 F*

TEH

+ 18.04 40 C.

42 33:

F*

TEH

-+ 15.35 40 f

C 48 35 F*

TEH

+ 3.39 78 21--

+1 8

C 23 59 F*

TEH

+ 17.99 52 C

27 59 F*

TEH

+ 9.40 40 C

32 62 F*

TEH

+ 10.25 50 C

9 83 F*

TEH

+ 12.96 40 C

23-83 F*

TEH

+ 17.93

-40 C'

-44 63 F*

TEH

+ 11.27 40 C

22 52 F*

TEH

+ 5.20 40 C

22 58 F*

TEH

+ 13.94-40 C

25 46 F*

TEH

+ 13.89 40 C

26 44 F*

TEH

+ 15.78 93 i

C 26 55' F*

TEH

+ 15.90 40 l.

C, 27 45 F*

TEH

+ 14.82 40 C

27

'47 F*

TEH

,+ 15.13 40 C

27.

58 F*

TEH

+ 8.23 40 3

C 28-

-48 F*

TEH-

+ 14.85 40

[

C

'28 56-F*

TEH

+ 13.99 40

'C 31 47 F*

TEH-

+ 16.94-40:

C 32 57 F*

TEH

+ 13.98 91 C

39 48 F*

TEH

+

7.36-40 C-6

'112 F*

TEH'

+

2.14 40 C

8

'44 F*

TEH

+ 18.86 40 C

9 42 F*

TEH

+ 12.98 40 C

9 43 F*

TEH

+ 13.13 40 C

-9 47 F*

TEH

+

5.99 40 i

C 9

53 F*

TEH

+ 18.88 85 C

12 43 F*

TEH

+ 16.79 40 C

12 46 F*

TEH

+ 15.83 40

4-1,,.

i s

'Attdchment'2 to SPR 90-12:

V C Summer. Station Steam Generator Tube Disposition 2=

Fifth Refueling Outage Page No.

3 Highest 09/14/90 Reported.

Percent' S/C Row Column Disposition Degradation Thru-Wall.

Location C

13 45 F*

TEH

+ 14.88 40 C

15 46 F*

TEH

+ 16.89 55 C

16 45 F*

TEH

+ 15.83 40 C

17 47 F*

TEH

+ 6.31 40 C-4 27 F*

TEH c 17.96 40 C

5 74 F*

TEH

+ 2.22 50 C

11 74 F*

TEH

+ 16.78 40 C

19 71 F*

TEH

+ 9.33 40 C

20 69 F*

TEH

+ 16.21 40 C

20 78 F*

TEH

+ 17.62' 40 C

21 62 F*

TEH

+ 16.21 80 C

23 76 F*

TEH

+ 14.84 40 C

27 70 F*

TEH

+ 8.16 40 C

27 71 F*

TEH-

+ 8.32

'40 C

31 75 F*

TEH

+ 18.11 40 l

C 45 75 F*

TEH

+ 16.03 93 C

6 102-F*

TEH

+ 16.50 72 C

13 104 F*

TEH

+ 18.85 94 C

-22 102 F*

TEH

+ 18.84 80

{

C 24 85 F*

TEH

+ 16.82 40

-C 24 100 F*

TEH

+ 17.76 66-C 32 86 F*

TEH

+ 11.97 40 C

41 85 F*

TEH-

+ 5.29 40 C-1=

35 F*

TEH-

+ 1.27 94.

C 1

55 F*

TEH

+ 1.28 89 i

l 4

g f

e P

.j t

7 N-

L i,,

g-Attdch$snt2to'SPR90-12' V C Summer Station

. Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1, Highest.

09/14/90 Reported Percent S/G Row. Column Disposition Degradation Thru-Wall Location A

9' 83 TCD NDD

.i i

i

.l.

I i'

\\

l s

',1:

.1

p s

.i-

.,l'

%3 4

s

)

p '

S+g

e i :,, ;' *

~-Atttchment 2 to SPR 90212 V C Summer Station Steam Generator Tube Disposition Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reporteed Percent S/O' Row Column Disposition Degradation Thru-Wall Location B

9 56 TCD TEH

+ 19.60 40 i

b o

0 o

r-

.;,, Att$0hment2.toSPR90-12 V C Summer Station i

Steam Generator Tube Disposition

-)

Fifth Refueling Outage Page No.

1 Highest 09/14/90 J

Reported Percent S/G Row Column Disposition Degradation Thru-Wall t

Location C

13 5

TCD TEH

+ 15.95 40 C

12 5

TCD NDD C

10 23 TCD NDD C

9 29 TCD NDD C

9 106 TCD NDD i

i n

i f

i r

v I-.

Af,tdb ent2 t0'SPR 90-12 LC i

l' V C Stamer Station Generator Tube Disposition

<t*

Fifth Refueling Outage.

Page No.'

l' Highest 09/14/90 Reported Percent S/0 Row Column Disposition -

Degradation

-Thru-Wall Location

?

A 42 66 AAI.

AV3

+ 00.00 22 A-47 75 AAI 06c-

+ 00.00 20

.A 48 41 AAI.

09c

+ 00.00 23 A

48 53 AAI 06c

+ 00.00 20 A

48 59 AAI 06c

+ 00.00 21 A

49 34 AAI 06c

+ 00.00 23

-A-49 37 AAI 06c

+ 00.00 23 A

49 40 1AI 06c

+ 00.00 23 A

49 52 AAI

'06c

+ 00.00 23 A

49 53 AAI 06c

+ 00.00 21 A

-49 55 AAI 06c

+ 00.00 27 A

49 57 AAI 06c

+E00.00 20 A-49 62 AAI 06c

+ 00.00 22

~A.

8' 80 AAI 12H

+ 24.59 4

A 28 104 AAI AV3

+ 00.00 12 A

40 63 AAI AV1

+ 00.00 7

A 41 50 AAI AV1

+ 00.00 9

A 42 62 AAI AV1

+ 00.00 12 A

42 65 AAI AV1

+ 00.00' 7

A-47 55 AAI 08C

+ 00.00-17 A

47 59 AAI-06c

+ 00.00 15 i

A 48 52 AAI-08C

+ 00.00

17 A

48 53 AAI" 08C:

+ 00.00-14

.A-48' 60 AAI 06c

+ 00.00 18-i A

49 52 AAI 08c.

+L00.00 10

,A 49

-57 AAI 05c

-+ 00.00 14 A

49 59; AAI 06c

+ 00.00 18 A

49 75 ~

AAI 06c

+ 00.00 16 l

l_

A

-49 76 AAI 06c

+ 00.00 14 i

lU

.c i

1

'1 I

I L b t.

lj

(.....

Alt $chment2'to'SPR90-12 7

V c Summer Station Steam Generator Tube Disposition t

Fifth Refueling Outage Page No.

1 Highest 09/14/90 Reported Percent

.S/G-Row Column Disposition Degradation Thru-Wall Location B

34 100 AAI AV2

+ 00.00 23 B

43 04 AAI AV3

+ 00.00 31 8

47 52-AAI 06c

+ 00.00 22 7

B 47 71 AAI 06c

+ 00.00 20-B 47 72 AAI OBC

+ 00.00 23 JB 47 76 AAI 06c

+ 00.00 24 B

48 54 AAI 06c

+ 00.00-20 B

48 55 AAI 06c

+ 00.00 24 B

48 69 AAI 06c

+ 00.00 21 B

48 76 AAI 08C

+ 00.00 32 B

48 79 AAI 08C

+ 00.00-27 B

48 80 AAI-08C

+ 00.00 25 B

49 51 AAI 06c

+ 00.00 24 B.

14 9 54 AAI 06c

+ 00.00 21 B

49 56 AAI 06c

+ 00.00 22 B

49 64 AAI 06c

+ 00.00 22 B

49 76 AAI 06c

+ 00.00 29

'B 49 78 AAI 06c

+ 00.00 28 B

49 81 AAI

-08C

+ 00.00 28 B

3 60 AAI 13H

+ 18.30 1

B 26 8'

AAI AV2

+ 00.00 7

B 26 101 AAI AV2

+ 00.00 14 B

26 106:

AAI AV3

+ 00.00 12 B

39 93 AAI AV3

+ 00.00.

15 B

45 89 AAI AV2

+ 00.00

.11

- B 46 52 AAI 06C

+ 00.00 17

. B 48-38 AAI 06c

+ 00.00 18

. B 48 67 AAI 07c

+ 00.00 9

B 48 72 AAI 06c

+ 00.00 17 di B

49 55 AAI 06c

+ 00.00 18 L

B 49' 69 AAI 06c

+ 00.00 14 B

49 70 74I 06C

+ 00.00 19 B

49 77 AAI

'08C

+ 00.00 19 Y

6 o

l I

l J

os

o ;,/ $ -

Attcchment'2 to'SPR'90-12 V C Summer Station

-Steam Oenerator Tube Disposition j

Fifth Refueling Dutage

-Page No.

1 Highest 09/14/90 Reported Percent S/G Row Column Disposition Degradation Thru-Wall' Location C

40 84 AAI AV2

+ 00.00 22 C.

46 44 AAI 06C

+ 00.00 21 C

47 42 AAI 06C

+ 00.00 21 C

47

.44 AAI OSC

+ 00.00 23 C

48 39 AAI 06C

+ 00.00 20 i

C 48 43 AAI 04C

+ 00.00 20 C

48 56 AAI' 06C

+ 00.00 24 C

48 58 AAI 08C

+ 00.00 20-C 48 61 AAI 06C

+ 00.00 20 i

C 49 54 AAI 06C

+ 00.00 30 C

49' 58 AAI 06C

+ 00.00 22 C

49 63 AAI 06C

+ 00.00 23

-C 49 74 AAI 06C

+ 00.00 27

-C 28 104 AAI AV2

+ 00.00 11 C

40 83 AAI AV3

+ 00.00 16 C

46 44 AAI 04C

+ 00.00 15 C

46 47

.AAI 06C

+ 00.00 12 4

C 47 54 AAI 06C

+ 00.00 19 f

C' 48 38 AAI OSC

+ 00.00

'19 C

48 42 AAI 06C

+ 00.00 18

.I C

48 44 AAI' 06C

+ 00.00 16 i

j C

48 51 AAI 06C

+ 00.00 7

C 48 63 AAI 06C

+ 00.00 16

.l C

48 64

_AAI 06C

+ 00.00 17

]

-C 48 67 AAI 06C

+-00.00 19

.l C

48

'74 AAI 06C

+ 00.00 11 C

49 61 AAI 06C

+ 00.00 18 C

49

.62 '

AAI 08C'

+ 00.00 19 q

t a

'l l

1 w :+

'j i

m c

4 a

.)

n-

/

", 3 c g-

..o

(