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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20236K7731987-10-31031 October 1987 Monthly Operating Rept for Oct 1987 ML20235W3781987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20238E2741987-08-31031 August 1987 Monthly Operating Rept for Aug 1987 ML20235H3151987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML20214W3241987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20214R5101987-04-30030 April 1987 Rev 1 to Monthly Operating Rept for Apr 1987,correcting Operation Statistics & Shutdown Experience Due to Mathematical Errors ML20215L4941987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20210B4141987-03-31031 March 1987 Revised Monthly Operating Rept for Mar 1987 ML20206F3561987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20212P3101987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20210R6341987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20207M2451986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 ML20215C7911986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20213F3121986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20215G1081986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20212F5321986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20202G3371986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20211B5601986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20197D2651986-04-30030 April 1986 Monthly Operating Rept for Apr 1986 ML20155C6461986-03-31031 March 1986 Monthly Operating Rept for Mar 1986 ML20137Y2631986-02-28028 February 1986 Monthly Operating Rept for Feb 1986 ML20214B9131986-01-31031 January 1986 Monthly Operating Rept for Jan 1986 ML20137B3711985-12-31031 December 1985 Monthly Operating Rept for Dec 1985 ML20137Z0901985-11-30030 November 1985 Monthly Operating Rept for Nov 1985 ML20136A7121985-10-31031 October 1985 Monthly Operating Rept for Oct 1985 ML20133J0521985-09-30030 September 1985 Monthly Operating Rept for Sept 1985 ML20133J0651985-08-31031 August 1985 Revised Monthly Operating Rept for Aug 1985 ML20135F9861985-08-31031 August 1985 Monthly Operating Rept for Aug 1985 ML20134D9611985-07-31031 July 1985 Monthly Operating Rept for Jul 1985 ML20132F6251985-06-30030 June 1985 Monthly Operating Rept for June 1985 ML20135G0641985-06-30030 June 1985 Revised Monthly Operating Rept for June 1985 ML20126L7141985-05-31031 May 1985 Monthly Operating Rept for May 1985 ML20135F9921985-04-30030 April 1985 Revised Monthly Operating Rept for Apr 1985 ML20127G2481985-04-30030 April 1985 Monthly Operating Rept for Apr 1985 ML20115C9401985-03-31031 March 1985 Monthly Operating Rept for Mar 1985 ML20112D9131985-02-28028 February 1985 Monthly Operating Rept for Feb 1985 ML20106J3801985-01-31031 January 1985 Monthly Operating Rept for Jan 1985 ML20112H8071984-12-31031 December 1984 Monthly Operating Rept for Dec 1984 ML20101B1871984-11-30030 November 1984 Monthly Operating Rept for Nov 1984 ML20099C6941984-10-31031 October 1984 Monthly Operating Rept for Oct 1984 ML20093E3861984-09-30030 September 1984 Monthly Operating Rept for Sept 1984 ML20097C7951984-08-31031 August 1984 Monthly Operating Rept for Aug 1984 ML20094N2661984-07-31031 July 1984 Monthly Operating Rept for Jul 1984 ML20090B8591984-06-30030 June 1984 Monthly Operating Rept for June 1984 ML20091M8741984-05-31031 May 1984 Monthly Operating Rept for May 1984 ML20084H8601984-04-30030 April 1984 Monthly Operating Rept for Apr 1984 ML20088A1681984-03-31031 March 1984 Monthly Operating Rept for Mar 1984 ML20087A9181984-02-29029 February 1984 Monthly Operating Rept for Feb 1984 ML20087A5401984-01-31031 January 1984 Monthly Operating Rept for Jan 1984 ML20086N0061984-01-31031 January 1984 Monthly Operating Rept for Jan 1984 1987-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers RA-97-0258, LER 97-S12-00:on 971119,discovered Uncompensated Security Zone.Caused by Inattention to Detail by Members of Security Force.Provided Event Info to Security Shift Personnel & Changed Practice Re Zone Review1997-12-19019 December 1997 LER 97-S12-00:on 971119,discovered Uncompensated Security Zone.Caused by Inattention to Detail by Members of Security Force.Provided Event Info to Security Shift Personnel & Changed Practice Re Zone Review ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20217Q2751997-06-30030 June 1997 CP&L Fitness for Duty Program Performance Data for Period 970101-0630 ML14183A6951995-09-18018 September 1995 Safety Evaluation Approving Relocation of Technical Support Ctr ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML17352A8691993-05-31031 May 1993 Technical Rept, Assessment of Aging Degradation of Civil/ Structural Features at Selected Operating Nuclear Power Plants. ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20079H1571991-09-30030 September 1991 Nonproprietary Evaluation of Revised Transfer to Cold Leg Recirculation Procedure,Hb Robinson Unit 2 ML20086T2951991-06-14014 June 1991 Rev 1 to EQ Documentation Package Eqdp 36.0, Boston Insulated Wire Cable ML20086T2861991-03-0808 March 1991 Rev 1 to EQ Documentation Package Eqdp 11.1, Dekoron Instrumentation Cables ML20086T2561991-03-0808 March 1991 Rev 1 to EQ Documentation Package 10.0, Continental Shielded Instrument Cable ML20065K6961990-10-31031 October 1990 Mechanical Licensing Rept for Hb Robinson High Thermal Performance Fuel Assemblies ML20065K6971990-10-31031 October 1990 Thermal Hydraulic Compatibility Analysis of Anf High Thermal Performance Fuel for Hb Robinson,Unit 2 ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20247E0701989-07-20020 July 1989 Info Rept:On 890717-0804,fire Penetration Seals Will Be Removed from Svc to Allow Access for Ventilation Sys Mod. Addl Fire Barrier Penetrations Will Be Made in Wall Between RHR Pump Pit & Fuel Handling Bldg,Per Tech Spec 3.14.7.2 ML20246E9111989-03-31031 March 1989 PDC-3:Advanced Nuclear Fuels Corp Power Distribution Control for PWRs & Application of PDC-3 to Hb Robinson Unit 2 ML20245H0821989-01-25025 January 1989 Criticality Safety Analysis of Hb Robinson Spent Fuel Pool W/4.2% Nominal Enrichment Fuel Assemblies ML20205T0551988-10-31031 October 1988 Responses to NRC Questions on RTD Bypass Elimination Licensing Rept ML20147E2371988-02-29029 February 1988 1987 Annual Rept - Primary Coolant Iodine Spikes ML20147B1971987-12-31031 December 1987 1987 Annual Rept - Primary Safety & Relief Valve Challenges ML20236K7731987-10-31031 October 1987 Monthly Operating Rept for Oct 1987 ML20235W3781987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20238E2741987-08-31031 August 1987 Monthly Operating Rept for Aug 1987 ML20235H3151987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML17261A5301987-06-18018 June 1987 Part 21 Rept Re Potential Util Failure to Comply W/Component Containment Isolation Licensing Commitment If Proposed Mods to Component Cooling Water Sys Instituted.Utils Advised to Evaluate Containment Isolation Sys ML20214W3241987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20214R5101987-04-30030 April 1987 Rev 1 to Monthly Operating Rept for Apr 1987,correcting Operation Statistics & Shutdown Experience Due to Mathematical Errors ML20215L4941987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20206F3561987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20210B4141987-03-31031 March 1987 Revised Monthly Operating Rept for Mar 1987 ML20205F6021987-03-23023 March 1987 Special Rept:On 870302,noble Gas Effluent Monitor for Main Steam Line B Declared Inoperable & Svc Not Returned Until 870312.Caused by Defective Detector.Detector Replaced.High Voltage for Detector Adjusted & Sys Operation Checked ML20212P3101987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20214Q7891987-01-31031 January 1987 Cycle 12,SAR ML20210R6341987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20207M2451986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 L-18-120, Rev 0 to Supplemental Info in Support of Conservatisms in Criticality Analysis Performed for Hb Robinson Isfsi1986-12-18018 December 1986 Rev 0 to Supplemental Info in Support of Conservatisms in Criticality Analysis Performed for Hb Robinson Isfsi ML20215C7911986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20213F3121986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20215G1081986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20215F0361986-09-29029 September 1986 Special Rept:On 860902,during Cold Shutdown,Pressurizer PORV Lifted Twice to Prevent Overpressurization.Caused by Inadvertent Action by Unit Operators.Operations Personnel Counseled Re Importance of Breaker Position Indicators ML20211C0641986-09-0909 September 1986 Rev 0 to Final Rept Criticality Safety Analysis Hb Robinson Spent Fuel Storage Racks (Unpoisoned,Low Density) W/4.2% Enriched 15x15 Fuel Assemblies ML20211C0491986-09-0202 September 1986 Rev 0 to Final Rept Criticality Safety Analysis Hb Robinson New Fuel Storage Vault W/4.2% Enriched 15x15 Fuel Assemblies ML20212F5321986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20203D0221986-07-14014 July 1986 Part 21 Rept Re Air Monitoring Sys Probes Exhibiting Blue Tip Rather than Normal White Tip & Insensitive to Chlorine. Caused by Improper Handling/Storage.Advisory Bulletin Encl. Item Not Reportable Per Part 21 ML20202G3371986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20211B5601986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20197D2651986-04-30030 April 1986 Monthly Operating Rept for Apr 1986 1999-09-22
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.J ,o Enclorura to Serial: .RSEP/82-1702 Pcgm 1 of 1 OPERATING DATA REPORT DOCKET NO: 50-261 DATE: 821005 tr COMPLETED BY: H. Ray Norris TELEP110NE: (803) 383-4524 OPERATING STATUS '
Notes:
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- 1. Unit-Name: H. B. Robinson Unit No. 2
^2. Reporting Period: 820901,0000/820930,2400 There are presently 157 spent fuel assemblies in the spent fuel pool.
- 3. Licensed Thermal Power (MWt): 2300
- 4. Nameplate Rating (Gross Mle): 739
- 5. Design Electrical Rating (Net MWe): 700
. 700
- 6. MaxiinumDependable
- 7. Maximum Dependable Capacity Capacity (Net(Gross MWe): MWe):_665
- 8. If Changes Occur in Capacity Ratings (ltem Number 3 through 7) Since Last Report, Give Reasons: No change
- 9. Power Level to Which Restricted, If Any (Net MWe): 1955 MWT Reactor Power
- 10. Reasons For Restrictions, If Any: Although the Unit ~is not restricted by any outside agency, the power level is presently reduced due to steam generator considerations.
This Month Yr.-to-Date Cumulative
- 11. Ilours in Reporting Period 720 6551 101477
- 12. Number of Ilours Reactor Was Critical 707.80 2379.63 74725.05
- 13. Reactor Reserve Shutdown llours 0 0 1085.30
- 14. IIours Cencrator On-Line 591.57 2173.77 72729.08~
- 15. Unit Reserve Shutdown llours 0 0 23.20~
- 16. Gross Thermal Energy Generated (MWil) 1029160 3818890 146914264
- 17. Gross Electrical Energy Generated (MWil) 318393 118967_5 47267645 ~
- 18. Net Electrical Energy Generated (MWII) 295731 1084431 44704682
- 19. Unit Service Factor 82.16 33.18 71.67
- 20. Unit Availability Factor 82.16 33.18 71.69
- 21. Unit Capacity Factor (Using MDC Net) 61.76 24.89 66.2 I
- 22. Unit Capacity Factor (Using DER Net) 58.67 23.64 62.93 -
- 23. Unit Forced Outage Rate 17.83 12.35 14.52 -
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Type-2 2/26/83, Four week steam generator inspection outage.
- 25. If Shut Down At End of Report Period, Estimated Date of Stattu,): On line
- 26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY --- ---
INITIAL ELECTRICITY -- --
ComIERCIAL OPERAT10N --- ---
S -
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((Wif0130244 PDR d _.. ADOCK 05000261 821006' !
PDR
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Englosuri to S2ri:13: RSEP/82-17'02
__ Pip 1 of 1 AVERAGE DAILY UNIT POWER LEVEL .
DOCKET NO. 50-261 UNIT TWO 821005 DATE H. Ray Norris
, CO51PLETED BY TELEPHONE (803) 383-4524 September MONT11 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (5tWe Net) (5twe Net) 1 543 17 533 2 542 18 536 3' 232 3 19 4 539 20 467-5 330 21 345 6 466 22 536 540 7 - 23 508 541 g
276 483 9 25 369 10 26 0 544
!! 27 0 544 12 _ - 28
. 213 542 13 29
-535 545 14 30 15 33 536 16 INSTRUCTIONS On this format, list the avmge daily unit power levelin StWe&t fcr each d:y in the reporting month. Compute to the nearest whole rnegawsti.
- (9/77) 44 4 ,
- Enclo ure to S2 rial: RSEP/82-1702 - ,T Paga 1 of 1 .
' %. . i DOCKET NO. 50-261 UNIT S!!UTDOWNS AND POWER REDUCTIONS UNIT N A\tE H. B. ROBINSON f
DATE 821005 ,
COMPLETED BY H. Rav Norris REPORT MONTil Sentember TELEPl!ONE (803) 383-4524 r.
E 5 Cause & Cortcetive
- , .! ? 3 $..Y 5
,8 s s Licensec [ r, .
a? Action to No. Date y, ? $ Even 3P mO 50 Prevent Recurrence
~5= Report a H 35 c2 a
y < v -
6 .
Solenoid for "C',' WRV failed, causing HH INSTRU common fuse for all 3 WRVS to blow,
~
F 9.59 A 3 WRVS closed causing RX trip from low -
09-01 820906
' S/G water level solenoid for "C" WRV was replaced along with all.3 fuses.
82.12 PC VALVEX Relief valve failure caused by operat or 09-02 820907 F 18.72 G 1 error, repaired valve and counseled operator. ,
[lH INSTRU Fatrity hotwell level switch, causing 09-03 820913 F 92.66 A 3 ,
- . "B" cond. and W Pumps to trip re-sulting in low level in "C" S/G. Hot .
- well level switch replaced.
~
-- Rh INSTRU Personnel error while performing a-7.46 3 09-04 820921 F G periodic _ test. Technicians were ,
counseled on importance of following procedures, 3 4
Exhibit G - Instructions
- F: Forced Reawn: fin Preparation of Data 1 Manual S: Scheduled A l'ituipment Failure (Explain) Entrs Sheets for Licensee 2-Manual Scram. -
11 minter.ance of Test Even't Repost (LER) File (NUREC-C Refueling 3 Automatic Scram. I ' '
4 Other (Explain) 01611 D Reputatmy Restriction E Operator Training & Liecuse Examination 5 F-Administrative
G-Operational Error (Ex' plain) '
(9/77) Il Other (Explain) .
9