ML20062H029
| ML20062H029 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 08/03/1982 |
| From: | Peterson D CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML20062H023 | List: |
| References | |
| NUDOCS 8208130273 | |
| Download: ML20062H029 (4) | |
Text
- s OPERATING DATA REPORT DOCKET NO.
50-255 2,
DATE 8/3/82 C051PLETED BY DAPeterson TELEPHONE 616 76h_8913
- OPERATING STATUS
- 1. Unit Name:
Palisades Notes
- 2. Reporting Period:
820701 - 820731
.g
- 3. Licensed Thermal Power (51Wt):
2510
- 4. Nameplate Rating (Gross 51We):
811 7
- 5. Design Electrical Rating (Net 31We): 805
- 6. Stasimum Dependable Capacity (Gross SIWE):
- 675
- 635
- 7. 51admum Dependable Capacity (Net 51We):
S. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
1 6
- 9. Power Lesel To Which Restricted.lf Any(Net 51We):
- 10. Reasons For Restrictions.If Any:
i j
fi
,k This 51onth Yr.-to Date Cumulatise
- 11. Hours In Reporting Period Thh 5087 03.062 9'
- 12. Number Of Hours Reactor Was Critical 257 7 2359 3 51_,_082.5 if
- 13. Reactor Resene Shutdown Hours
- 14. Hours Generator On-Line 257.7 1971.3 h8.17s.7
~
,15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (31WH) 581.Shh h,356,7hh 95,764,008
- 17. Gross Electrical Energy Generated (51WH) 179,370
___1,360,730
_ 29.,188.680
- 18. Net Electrical Energy Generated (51WH) 169,215 1.278.710 97.701.6ha 34.6 98.8 51.8 j
' 19. Unit Senice Factor 34.6 38.8 si.8
[
- 20. Unit Availability Factor t
- 21. Unit Capacity Factor (Using 31DC Net) '
95.8 39.6 h7.0
- j. -
- 22. Unit Capacity Factor (Using DER Net) 28.2 31.2 37.1
- 23. Unit Forced Outage Rate 65.h 61.2 35.1
~
- 24. Shutdowns Scheduled Oser Next 6 Slonths (ifpe.Date,and Duration of Each1:
a
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
8/12/82
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIA L CRITICA LITY INITI A L ELECTRICITY Coil %1ERCIAL OPERATION 1-
- u ~ aa nn c'onAanner Backpressure (9/77) 8208130273 820809 PDR ADDCK 05000255 g.
.R PDR
~*
AVERAGE DAILY UNIT POWER LEVEL DOCKETNO.
50-255 UNIT Palise. des 0/b/02 DATE COMPLETED BY DAPetierson TELEPHONE 616 764 8913 MONTil Julv DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe-Net) 1 758 17 749 2
.18 3~
747 19 745 4
20 5
739 21 695 6
22 1
7 712 23 730 3
24 7142 9
25 2II 10 26 11 157 27 12 28 13 29 14 30 15 31 16 i
INSTRUCTIONS On this format. fist the aserage dail "i' P ### l#*#II" MWe-Net for each day in tiic reporting month. Compute to the nearest whole mecawatt-(9/77)
.=
UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-255
= UNIT NAME _
Palisades DATE 6-5-62 REPORT MONTil July 1982 COMPLETED By DVanDenBerg TELEPilONE 616 764-8013 r.
E E
.!E 2 2"d
~ Licensee
,E +
{"3 3
Cause A Corrective No.
Date g
3g i
jg5 Event u7 e-Action to
$E 3g=
Report sr r$ u gu Prevent Recurrence H
g o
e O
12 820710 F.
h86.3 A
2 Cooling Tower Pump Bearing Failure v
1 2
3 4
F: Forced Reason:
Method:
Exhibit G Instructions S: Scheduled A lk:nipment Failure (Explain) 1 Manual for Preparation of Data 11 Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C. Refueling 3-Automatic Scram.
Event Report (LERI File INUlti.G-D-Regulatory Restriction 4-Other (Explain) 01611 li Operaior Training & l.icense Examination F-Administrative 5
G-Operational Errier (Explain)
Esinbit I Same Source 01/77)
Il Other (Explain)
2LMfARY OF OPERATING EXPERIENCE FOR THE MONTH OF JULY 1982 The Plant operated at essentially 100% power until July 10 when power was reduced to repair P-39A Cooling Tower Pump. The unit was manually tripped off line on July 11 at 1720 hours0.0199 days <br />0.478 hours <br />0.00284 weeks <br />6.5446e-4 months <br /> from h3% power when P-39B Cooling Tower Pump displayed signs of distress. Repairs to the pumps continued through the end of the month.
,