ML20058J470

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Discusses 931117 Open Enforcement Conference Re Insp Repts 50-348/93-26 & 50-364/93-26 & to Discuss Personnel Errors
ML20058J470
Person / Time
Site: Farley  
Issue date: 11/30/1993
From: Merschoff E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Dennis Morey
SOUTHERN NUCLEAR OPERATING CO.
References
NUDOCS 9312140123
Download: ML20058J470 (21)


See also: IR 05000348/1993026

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Docket Nos.:

50-348, 50-364

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License Nos.: NPF-2, NPF-8

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Southern Nuclear Operating Company, Inc.

ATTN: Mr. D. N. Morey

Vice President

P. O. Box 1295

Birmingham, AL 35201

Gentlemen:

SUBJECT:

ENFORCEMENT CONFERENCE SUMMARY

(NRC INSPECTION REPORT NOS. 50-348/93-26 AND 50-364/93-26)

This letter refers to the Open Enforcement Conference held at our request on

November 17, 1993. The issues discussed at this conference related to

personnel errors resulting in losses of configuration control during perfor-

mance of maintenance and testing activities. A list of attendees and a copy

of your handout are enclosed. We are continuing our review of these issues to

determine the appropriate enforcement action.

In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its

enclosures will be placed in the NRC Public Document Room.

Should you have any questions regarding these arrangements, we will be pleased

to discuss them.

Sincerely,

n) [

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13n103

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Eilis W. Herschoff, Director

Division of Reactor Projects

Enclosures:

1.

List of Attendees

2.

Presentation Summary

cc w/encls:

B. L. Moore

Licensing Manager

Southern Nuclear Operating

Company, Inc.

P. O. Box 1295

Birmingham, AL 35201-1295

(cc w/encls cont'd - See page 2)

9312140123 931130

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Southern Nuclear Operating

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Company, Inc.

(cc w/encls cont'd)

R. D. Hill, Jr.

General Manager, Farley Plant

Southern Nuclear Operating

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Company, Inc.

P. O. Box 470

Ashford, AL 36312

-

W. R. Bayne, Supervisor

Safety Audit and Engineering Review

Farley Nuclear Plant

P. O. Box 470

Ashford, AL 36312

State Health Officer

Alabama Department of Public Health

434 Monroe Street

Montgomery, AL 36130-1701

James H. Miller, III, Esq.

Balch and Bingham

P. O. Box 306

j

1710 Sixth Avenue North

Birmingham, AL 35201

Chairman

Houston County Commission

P. O. Box 6406

Dothan, AL 36302

bcc w/encls:

B. Siegel, NRR

F. Cantrell, RII

Document Control Desk

NRC Resident Inspector

U.S. Nuclear Regulatory Commission

Route 2, Box 24

i

Columbia, AL 36319

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ENCLOSURE 1

List of Attendees

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NRC Attendees:

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.

S. D. Ebneter, Regional Administrator, Region II (RII)

'

A. F. Gibson, Director, Division of Reactor Safety (DRS), RII

J. E. Beall, Enforcement Specialist, Office of Enforcement

,

G. R. Jenkins, Director, Enforcement and Investigation Coordination Staff

l

(EICS),RII

B. Uryc, Senior Enforcement Specialist, EICS, RII

,

C. F. Evans, Regional Counsel, RII

'

J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP), RII

D. M. Verrelli, Chief, Reactor Projects Branch I, DRP, RII

F. S. Cantrell, Chief, Reactor Projects Section 18, DRP, RII

R. W. Wright, Project Engineer, Section IB, DRP, RII

S. J. Cahill, Reactor Engineer, Operator Licensing Section, DRS, RII

T. M. Ross, Senior Resident Inspector - Faricy, DRP, RII

)

M. J. Morgan, Resident Inspector - Farley, DRP, RII

'

.

B. L. Siegel, Project Manager, Project Directorate II-1, Office of Nuclear

Reactor Regulation

Licensee Attendees:

J. D. Woodard, Executive Vice President, Souther Nuclear Company (SNC)

D. N. Morey, Vice President, Nuclear Generation, SNC

R. D. Hill, General Plant Manager, Farley, SNC

B. L. Moore, Manager, Licensing, SNC

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J. W. McGowan, Manager, Safety Audit & Engineering Review, SNC

J. E. Garlington, General Manager, Nuclear Support, SNC

E. F. Bates, Senior Engineer, Farley Support, SNC

G. S. Waymire, Senior Engineer, Farley Operations, SNC

A. R. Deweese, Systems Operator, Operations, SNC

G. P. Crone, Superintendent, Operations Support, SNC

B. J. Bell, Superintendent, Electrical Maintenance, SNC

A. G. James, President, IBEW Local 796, SNC

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ET4 CLOSURE 2

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ENFORCEMENT CONFERENCE

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FARLEY NUCLEAR PLANT

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AGENDA

NOVEMBER 17,1993

I.

INTRODUCTION AND OPENING RE31 ARKS

S. Ebneter

'

,

II.

DISCUSSION OF TIIE ENFORCEMENT POLICY

G. Jenkins

,

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'

III.

OVERVIEW

S. Ebneter

,

IV.

APPARENT EXAMPLES OF VIOLATION

AND NRC CONCERNS

J. Johnson

V.

OPENING REMARKS

D. Morey

VI.

DISCUSSION OF APPARENT VIOLATION

R. Ilill

VII.

SAFETY SIGNIFICANCE

B. Moore

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CONCLUSION

R. Ilill

IX.

CLOSING REMARKS

D. Morey

X.

BREAK

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XI.

NRC FOLLOWUP QUESTIONS

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CLOSING

S. Ebneter

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REACTOR TRIPS

PERSONNEL VERSUS TOTAL

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1991

1992

1993(YTD)

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E TOTAL REACTOR TRIPS

R REACTOR TRIPS DUE TO PERSONNEL ERROR

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1991

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YEARS

TOTAL LER'S Ll PERSONNEL

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REPORT 93-26 - THREE EVENTS

CONTROL ROOM PRESSURIZATION CAPABILITY

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SERVICE WATER TO 2A CCW ISOLATION VALVE (MOV 3130A)

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SPENT FUEL POOL COOLING

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CONTROL ROOM PRESSURIZATION BOUNDARY

CONDENSER END BELL REMOVAL REQUIRED TO REPAIR REFRIGERANT LEAK

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PLANNER DID NOT LIST REMOVAL OF IIVAC PANELS IN WORK SEQUENCE

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SilIFT FOREMAN IDENTIFIED PROBLEM AND PANELS RE-INSTALLED

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CAUSE

INADEQUATE PLANNING

CORRECTIVE ACTION

CORRECTED COMPONENT DATA BASE

LABELED TIIE A/C UNIT

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SW TO 2A CCW ISOLATION VALVE - MOV 3130A

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TESTING PLANNED FOR MOV 3130B

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TEST ENGINEER INCORRECTLY TRANSCRIBED DATA

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OPERATION OF MOV 3130A NOTED BY TEST ENGINEER

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CONTROL ROOM NOTIFIED AND MOV 3130A RE-OPENED

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CAUSE

INCORRECTLY TRANSCRIBED DATA

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ADDED DATA SIIEET VERIFICATION

ACTION

COACIIED PERSONNEL

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CCW ISOLATED TO SFP HF,AT EXCHANGER

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TAG ORDER PREPARED TO ISOLATE MOV 3047

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PERSONNEL DID NOT CONFIRM ON-SERVICE CCW IIEAT EXCIIANGER

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CONTROL ROOM ALARM FOR SFP llIGli TEMPERATURE

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COOLING RESTORED

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CAUSE

INADEQUATE COMMUNICATIONS

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IMPROPER TAG ORDER

CORRECTIVE ACTION

RETRAINED PERSONNEL

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SAFETY SIGNIFICANCE

CONTROL ROOM HVAC

ONLY LEAKAGE PATII WAS TO Tile IIVAC ROOM

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B-TRAIN CR IIVAC STILL CAPABLE OF MAINTAINING IIABITABLE ENVIRONMENT

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CIILORINE IS NOT A CREDIBLE IIAZARD

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CR OPERATORS WOULD NOT IIAVE EXCEEDED REGULATORY LIMITS

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SAFETY SIGNIFICANCE

INADVERTENT OPERATION OF MOV3130A

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NO IMPACT ON PLANT EQUIPMENT OR OPERATIONS

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ONLY A 3 MINUTE DURATION EVENT

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NOT. A REPORTABLE EVENT

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SAFETY SIGNIFICANCE

LOSS OF COOLING TO SFP COOLING

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LOW SFP IIEATUP RATE

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CR ANNUNCIATOR FOR IllGII SFP TEMPERATURE

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ADEQUATE MAKEUP WATER SOURCES EXIST FOR SFP

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(RWST, DEMIN, RMWST)

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PERSONNEL ERROR ANALYSIS

A.

REDUCTION IN:

LEVEL OF SIGNIFICANCE

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ERRORS CAUSED BY WORK CONTROL

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IMPROPER USE OF PROCEDURES

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ERRORS ON BACKSillFT

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B.

INCREASE IN ERRORS CAUSED BY WORK ACTIVITY PREPARATION

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COMPARATIVE ANALYSIS

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CURRENT EVENTS - IMPROPERLY PREPARED DOCUMENTS

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PAST SIMILAR EVENTS -INADEQUATE WORK IMPLEMENTATION

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CORRECTIVE ACTION RESULTS

SIGNIFICANT PERSONNEL ERRORS REDUCED IN 1993

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PAST CORRECTIVE ACTIONS / STAR PROGRAM llAVE BEEN SUCCESSFUL

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- , . .-. -.- - ... . . . _ . . . . . . _ .

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.

6-

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TEMPORARY OPERATIONS SHIFT MANAGER

RE-ENFORCE MANAGEMENT EXPECTATIONS TO SIIIFT SUPERVISORS

.

IDENTIFY AREAS TIIAT CAN BE CIIANGED TO REDUCE ERRORS

.

ASSIGNED SENIOR PLANT MANAGEMENT

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OBSERVATIONS

STAR PROGRAM - IMPLEMENTATION VERSUS PLANNING

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FORMALITY- ROUTINE VERSUS NON-ROUTINE ACTIVITIES

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ESTABLISIIED BARRIERS- NOT ALWAYS UNDERSTOOD

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INSUFFICIENT FEEDBACK BETWEEN PLANNERS AND IMPLEMENT'NG INDIVIDUALS

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CORRECTIVE ACTIONS

1

BROADEN FOCUS OF STAR PROGRAM

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RE-ENFORCE MANAGEMENT EXPECTATIONS TO EMPLOYEES

.

EVALUATE ESTABLISIIED BARRIERS

.

IMPROVE FEEDBACK BETWEEN PLANNERS AND IMPLEMENTING INDIVIDUALS

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SUMMARY

SAFETY SIGNIFICANCE OF EVENTS WAS LOW

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n

IDENTIFIED BY FARLEY NUCLEAR PLANT PERSONNEL

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PROMPT CORRECTIVE ACTION TAKEN

.

OUR PROGRAM FOR REDUCING PERSONNEL ERRORS IS WORKING

.

STAR PROGRAM FOCUS NEEDS TO BE BROADENED

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SOME MANAGEMENT EXPECTATIONS NEED TO BE REINFORCED

..

BARRIERS / CAUTIONS NEED TO BE REEVALUATED

.

WE ARE IMPROVING

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