ML20058J470
| ML20058J470 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 11/30/1993 |
| From: | Merschoff E NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Dennis Morey SOUTHERN NUCLEAR OPERATING CO. |
| References | |
| NUDOCS 9312140123 | |
| Download: ML20058J470 (21) | |
See also: IR 05000348/1993026
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i40V 3 0 !993
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Docket Nos.:
50-348, 50-364
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Southern Nuclear Operating Company, Inc.
ATTN: Mr. D. N. Morey
Vice President
P. O. Box 1295
Birmingham, AL 35201
Gentlemen:
SUBJECT:
ENFORCEMENT CONFERENCE SUMMARY
(NRC INSPECTION REPORT NOS. 50-348/93-26 AND 50-364/93-26)
This letter refers to the Open Enforcement Conference held at our request on
November 17, 1993. The issues discussed at this conference related to
personnel errors resulting in losses of configuration control during perfor-
mance of maintenance and testing activities. A list of attendees and a copy
of your handout are enclosed. We are continuing our review of these issues to
determine the appropriate enforcement action.
In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2,
Title 10, Code of Federal Regulations, a copy of this letter and its
enclosures will be placed in the NRC Public Document Room.
Should you have any questions regarding these arrangements, we will be pleased
to discuss them.
Sincerely,
n) [
A
13n103
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mm
Eilis W. Herschoff, Director
Division of Reactor Projects
Enclosures:
1.
List of Attendees
2.
Presentation Summary
cc w/encls:
B. L. Moore
Licensing Manager
Southern Nuclear Operating
Company, Inc.
P. O. Box 1295
Birmingham, AL 35201-1295
(cc w/encls cont'd - See page 2)
9312140123 931130
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ADOCK 05000348
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Southern Nuclear Operating
2
Company, Inc.
(cc w/encls cont'd)
R. D. Hill, Jr.
General Manager, Farley Plant
Southern Nuclear Operating
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Company, Inc.
P. O. Box 470
Ashford, AL 36312
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W. R. Bayne, Supervisor
Safety Audit and Engineering Review
Farley Nuclear Plant
P. O. Box 470
Ashford, AL 36312
State Health Officer
Alabama Department of Public Health
434 Monroe Street
Montgomery, AL 36130-1701
James H. Miller, III, Esq.
Balch and Bingham
P. O. Box 306
j
1710 Sixth Avenue North
Birmingham, AL 35201
Chairman
Houston County Commission
P. O. Box 6406
Dothan, AL 36302
bcc w/encls:
B. Siegel, NRR
F. Cantrell, RII
Document Control Desk
NRC Resident Inspector
U.S. Nuclear Regulatory Commission
Route 2, Box 24
i
Columbia, AL 36319
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ENCLOSURE 1
List of Attendees
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NRC Attendees:
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S. D. Ebneter, Regional Administrator, Region II (RII)
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A. F. Gibson, Director, Division of Reactor Safety (DRS), RII
J. E. Beall, Enforcement Specialist, Office of Enforcement
,
G. R. Jenkins, Director, Enforcement and Investigation Coordination Staff
l
(EICS),RII
B. Uryc, Senior Enforcement Specialist, EICS, RII
,
C. F. Evans, Regional Counsel, RII
'
J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP), RII
D. M. Verrelli, Chief, Reactor Projects Branch I, DRP, RII
F. S. Cantrell, Chief, Reactor Projects Section 18, DRP, RII
R. W. Wright, Project Engineer, Section IB, DRP, RII
S. J. Cahill, Reactor Engineer, Operator Licensing Section, DRS, RII
T. M. Ross, Senior Resident Inspector - Faricy, DRP, RII
)
M. J. Morgan, Resident Inspector - Farley, DRP, RII
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B. L. Siegel, Project Manager, Project Directorate II-1, Office of Nuclear
Reactor Regulation
Licensee Attendees:
J. D. Woodard, Executive Vice President, Souther Nuclear Company (SNC)
D. N. Morey, Vice President, Nuclear Generation, SNC
R. D. Hill, General Plant Manager, Farley, SNC
B. L. Moore, Manager, Licensing, SNC
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J. W. McGowan, Manager, Safety Audit & Engineering Review, SNC
J. E. Garlington, General Manager, Nuclear Support, SNC
E. F. Bates, Senior Engineer, Farley Support, SNC
G. S. Waymire, Senior Engineer, Farley Operations, SNC
A. R. Deweese, Systems Operator, Operations, SNC
G. P. Crone, Superintendent, Operations Support, SNC
B. J. Bell, Superintendent, Electrical Maintenance, SNC
A. G. James, President, IBEW Local 796, SNC
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ET4 CLOSURE 2
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ENFORCEMENT CONFERENCE
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FARLEY NUCLEAR PLANT
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AGENDA
NOVEMBER 17,1993
I.
INTRODUCTION AND OPENING RE31 ARKS
S. Ebneter
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II.
DISCUSSION OF TIIE ENFORCEMENT POLICY
G. Jenkins
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III.
OVERVIEW
S. Ebneter
,
IV.
APPARENT EXAMPLES OF VIOLATION
AND NRC CONCERNS
J. Johnson
V.
OPENING REMARKS
D. Morey
VI.
DISCUSSION OF APPARENT VIOLATION
R. Ilill
VII.
SAFETY SIGNIFICANCE
B. Moore
Ylli.
CONCLUSION
R. Ilill
IX.
CLOSING REMARKS
D. Morey
X.
BREAK
,
XI.
NRC FOLLOWUP QUESTIONS
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CLOSING
S. Ebneter
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PERSONNEL VERSUS TOTAL
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1991
1992
1993(YTD)
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E TOTAL REACTOR TRIPS
R REACTOR TRIPS DUE TO PERSONNEL ERROR
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LER CAUSE TYPES
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1991
- 1992
1993(YTD)
YEARS
TOTAL LER'S Ll PERSONNEL
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REPORT 93-26 - THREE EVENTS
CONTROL ROOM PRESSURIZATION CAPABILITY
.
SERVICE WATER TO 2A CCW ISOLATION VALVE (MOV 3130A)
.
SPENT FUEL POOL COOLING
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CONTROL ROOM PRESSURIZATION BOUNDARY
CONDENSER END BELL REMOVAL REQUIRED TO REPAIR REFRIGERANT LEAK
.
PLANNER DID NOT LIST REMOVAL OF IIVAC PANELS IN WORK SEQUENCE
.
SilIFT FOREMAN IDENTIFIED PROBLEM AND PANELS RE-INSTALLED
.
CAUSE
INADEQUATE PLANNING
CORRECTIVE ACTION
CORRECTED COMPONENT DATA BASE
LABELED TIIE A/C UNIT
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- - - - - -
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SW TO 2A CCW ISOLATION VALVE - MOV 3130A
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TESTING PLANNED FOR MOV 3130B
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TEST ENGINEER INCORRECTLY TRANSCRIBED DATA
.
OPERATION OF MOV 3130A NOTED BY TEST ENGINEER
.
CONTROL ROOM NOTIFIED AND MOV 3130A RE-OPENED
.
CAUSE
INCORRECTLY TRANSCRIBED DATA
CORRECTIVE
ADDED DATA SIIEET VERIFICATION
ACTION
COACIIED PERSONNEL
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CCW ISOLATED TO SFP HF,AT EXCHANGER
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TAG ORDER PREPARED TO ISOLATE MOV 3047
.
PERSONNEL DID NOT CONFIRM ON-SERVICE CCW IIEAT EXCIIANGER
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CONTROL ROOM ALARM FOR SFP llIGli TEMPERATURE
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COOLING RESTORED
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CAUSE
INADEQUATE COMMUNICATIONS
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IMPROPER TAG ORDER
CORRECTIVE ACTION
RETRAINED PERSONNEL
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SAFETY SIGNIFICANCE
CONTROL ROOM HVAC
ONLY LEAKAGE PATII WAS TO Tile IIVAC ROOM
.
B-TRAIN CR IIVAC STILL CAPABLE OF MAINTAINING IIABITABLE ENVIRONMENT
.
CIILORINE IS NOT A CREDIBLE IIAZARD
.
CR OPERATORS WOULD NOT IIAVE EXCEEDED REGULATORY LIMITS
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SAFETY SIGNIFICANCE
INADVERTENT OPERATION OF MOV3130A
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OCCURRED ON AN OFF-SERVICE CCW llEAT EXCIIANGER
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NO IMPACT ON PLANT EQUIPMENT OR OPERATIONS
.
ONLY A 3 MINUTE DURATION EVENT
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NOT. A REPORTABLE EVENT
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SAFETY SIGNIFICANCE
LOSS OF COOLING TO SFP COOLING
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CR ANNUNCIATOR FOR IllGII SFP TEMPERATURE
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ADEQUATE MAKEUP WATER SOURCES EXIST FOR SFP
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(RWST, DEMIN, RMWST)
NOT A REPORTABLE EVENT
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PERSONNEL ERROR ANALYSIS
A.
REDUCTION IN:
LEVEL OF SIGNIFICANCE
.
ERRORS CAUSED BY WORK CONTROL
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IMPROPER USE OF PROCEDURES
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ERRORS ON BACKSillFT
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B.
INCREASE IN ERRORS CAUSED BY WORK ACTIVITY PREPARATION
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COMPARATIVE ANALYSIS
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CURRENT EVENTS - IMPROPERLY PREPARED DOCUMENTS
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PAST SIMILAR EVENTS -INADEQUATE WORK IMPLEMENTATION
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CORRECTIVE ACTION RESULTS
SIGNIFICANT PERSONNEL ERRORS REDUCED IN 1993
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PAST CORRECTIVE ACTIONS / STAR PROGRAM llAVE BEEN SUCCESSFUL
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6-
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TEMPORARY OPERATIONS SHIFT MANAGER
RE-ENFORCE MANAGEMENT EXPECTATIONS TO SIIIFT SUPERVISORS
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IDENTIFY AREAS TIIAT CAN BE CIIANGED TO REDUCE ERRORS
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ASSIGNED SENIOR PLANT MANAGEMENT
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OBSERVATIONS
STAR PROGRAM - IMPLEMENTATION VERSUS PLANNING
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FORMALITY- ROUTINE VERSUS NON-ROUTINE ACTIVITIES
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ESTABLISIIED BARRIERS- NOT ALWAYS UNDERSTOOD
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INSUFFICIENT FEEDBACK BETWEEN PLANNERS AND IMPLEMENT'NG INDIVIDUALS
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CORRECTIVE ACTIONS
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BROADEN FOCUS OF STAR PROGRAM
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RE-ENFORCE MANAGEMENT EXPECTATIONS TO EMPLOYEES
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EVALUATE ESTABLISIIED BARRIERS
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IMPROVE FEEDBACK BETWEEN PLANNERS AND IMPLEMENTING INDIVIDUALS
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SUMMARY
SAFETY SIGNIFICANCE OF EVENTS WAS LOW
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IDENTIFIED BY FARLEY NUCLEAR PLANT PERSONNEL
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PROMPT CORRECTIVE ACTION TAKEN
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OUR PROGRAM FOR REDUCING PERSONNEL ERRORS IS WORKING
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STAR PROGRAM FOCUS NEEDS TO BE BROADENED
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SOME MANAGEMENT EXPECTATIONS NEED TO BE REINFORCED
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BARRIERS / CAUTIONS NEED TO BE REEVALUATED
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WE ARE IMPROVING
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