ML20057C322

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Insp Repts 50-327/93-36 & 50-328/93-36 on 930809-20.No Violations or Deviations Noted.Major Areas Inspected:Balance of Plant Activities to Assess License C/A Being Taken in Response to Equipment That Has Been Unreliable
ML20057C322
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 09/14/1993
From: Casto C, Matt Thomas
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20057C319 List:
References
50-327-93-36, 50-328-93-36, NUDOCS 9309280214
Download: ML20057C322 (9)


See also: IR 05000327/1993036

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Report Nos.: 50-327/93-36 and 50-328/93-36

Licensee: Tennessee Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

Docket Nos.:

50-327 and 50-328

License Nos.: DPR-77 and DPR-79

Facility Name: Sequoyah I and 2

Inspection Conducted: , August 9-20, 1993

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Inspector:

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C.'Casto, Chief

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Test Programs Section

Engineering Branch

Division of Reactor Safety

SUMMARY

Scope:

This special, announced inspection was conducted in the areas of balance of

plant (B0P) activities to assess the licensee's corrective actions being taken

in response to B0P equipment that has been unreliable and has contributed to

unplanned challenges to reactor safety systems.

Findings identified during

this inspection will be followed up during subsequent inspections that will be

performed prior to restart of the units.

Results:

In the areas inspected, violations or deviations were not identified. An

inspector followup item (IFI) was identified to review the licensee's

evaluation and resolution of the essential raw cooling water (ERCW) system

containment isolation motor operated valve (MOV) issue.

In general, the

prioritization and scheduling of corrective actions for BOP restart work items

was performed appropriately. However weaknesses were identified by the NRC in

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the backlog review process as described in paragraph 4.

The corrective

actions already completed, plus those planned, adequately address the

significant material problems that were identified as having contributed to

the adverse trends in the reliability and availability of BOP components and

sy:tems. The corrective actions should improve the material condition of the

BOP.

Except for the issue with PVC jacketed cables (discussed in NRC report

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50-327,328/93-35), the material condition of the BOP should be satisfactory

for restart and operation after all planned corrective actions are completed.

The cable issue was still in the early stages of resolution and the potential

impact on restart and operation of the units had not been determined at the

conclusion of inspection 50-327, 328/93-35. The Site Quality department has

been active in assessing B0P activities for restart and aggressive in

identifying areas of weakness to plant management.

The efforts by the Site

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Quality Department were considered to be a strength.

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • M. Anderson, Design Control Manager, Site Engineering
  • J. Bajraszewski, Licensing Engineer
  • J. Baumstark, Operations Manager
  • C. Brimer, Project Engineering and Support Manager
  • L. Bryant, Maintenance Manager
  • M. Burzynski, Site Engineering Manager
  • M. Cooper, Maintenance Program Manager
  • R. Drake, Project Management / Controls Manager
  • R. Driscoll, Site Quality Manager
  • R. Fenech, Sequoyah Site Vice President
  • T. Flippo, Site Support Manager

D. Keuter, Nuclear Readiness Vice President

  • D. Lundy, Technical Support Manager
  • J. Maciejewski, Operations and Maintenance (0&M) Manager

K. Meade, Licensing Engineer

  • M. Needham, Customer Group 0&M Manager
  • S. Poage, Quality Audit and Assessment Manager
  • K. Powers, Plant Manager
  • J. Proffitt, Licensing Engineer

H. Rogers, Technical Support Program Manager

  • R. Shell, Site Licensing Manager
  • M. Skarzinski, Technical Programs and Performance Manager
  • R. Thompson, Compliance Licensing Manager

P. Trudel, Design Engineering Manager

  • J. Ward, Engineering and Modifications Manager

Other licensee employees contacted included engineers, operators, shift

supervisors, QA/QC personnel, craftsmen, and other plant personnel.

NRC Employees

  • C. Casto, Section Chief, Region II
  • W. Holland, Senior Resident Inspector
  • P. Kellogg, Section Chief, Region II
  • A. Long, Resident Inspector
  • S. Shaeffer, Resident Inspector
  • Attended exit meeting

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

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2.

Plant Status

Unit I was in the refueling condition (Mode 6) to support a refueling

outage and Unit 2 was in the cold shutdown condition (Mode 5) for a

forced outage.

3.

Background

During 1992 and early 1993, Sequoyah experienced a significant increase

in the number of transients and reactor trips associated with secondary

or B0P systems and equipment. Sequoyah Units 1 and 2 were shut down on

March 1 and 2,1993, following the rupture of an extraction steam line

(B0P system) in Unit 2.

After the units were shut down, the licensee

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developed a Sequoyah Restart Plan. The overall objectives of the

Restart Plan are to ensure the comprehensiveness of the restart efforts,

to provide an integrated framework for consistent and effective

implementation of those efforts, and to assist in the management and

communication of those efforts.

The purpose of the B0P inspections at Sequoyah is to evaluate the

corrective actions taken by TVA in response to the equipment problems to

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determine if the corrective actions are adequate to ensure that the

material condition of B0P equipment and systems is acceptable prior to

unit restart.

4.

B0P Assessments and Studies

As i result of the adverse trend in the performance of the secondary

plant and the impact on reliability and availability at Sequoyah, site

senior management initiated a Secondary Plant Reliability Study in

January 1993. The objective of the reliability study was to understand

the root cause of the increased contribution of the secondary plant to

unit transients and reactor trips at Sequoyah and, based on this

understanding, provide specific recommendations to site management to

reduce the occurrence of secondary plant induced events. The licensee

also contracted Stone and Webster Engineering Corporation (SWEC) to

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perform an independent design review of selected B0P systems in order to

identify additional problems or vulnerabilities in the B0P which could

jeopardize plant reliability.

The reliability study identified several areas of weakness, with

inadequate resource management and control of work being the most

significant contributors to the adverse trend in secondary plant

performance. The study also identified numerous secondary plant

material condition deficiencies which could potentially affect secondary

plant reliability and availability.

Recommended corrective actions were

provided for the areas of weakness and the material condition

deficiencies.

NRC inspectors have performed several inspections in the 80P area during

the period June-August 1993. The inspectors reviewed the results and

the recommended corrective actions from the backlog review process, the

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TVA reliability study, and the SWEC independent design review. The NRC

inspection efforts are documented in inspection reports (IR) 50-327,

328/93-22, 93-26, 93-27, 93-31, 93-32, 93-35, and 93-36.

B0P Material Condition

The licensee identified the backlogged work that existed as of

May 1, 1993 for the focus systems identified in the Restart Plan.

The backlogged work was prioritized for completion before or after

restart, based on the restart criteria specified in the Restart

Plan.

Improvements were made that were identified in the TVA

reliability study and the SWEC design study. The licensee

performed material condition walkdowns to determine if all

hardware problems had been identified. The walkdowns resulted in

a significant number of work requests (WR) being written (over

3000) for material condition deficiencies. The inspectors noted

from earlier discussions with licensee personnel that the

walkdowns were initially planned to be performed after corrective

actions had been implemented in order to verify the readiness of

the applicable systems.

It was only after NRC inspectors

identified material condition deficiencies during their walkdowns

(IR 50-327,328/93-22 and 93-26) that the licensee decided to

perform material condition walkdowns of the focus systems.

Modification and maintenance work activities are currently on-

going to correct material deficiencies.

NRC inspectors selected 13 of the focus systems and reviewed the

applicable system notebooks of backlegged work, performed material

condition walkdowns, and reviewed the licensee's prioritization

and scheduling of backlogged items for work off. The inspectors

also reviewed the TVA reliability study and the SWEC BOP design

study. System walkdowns performed by NRC identified material

condition deficiencies that TVA had not identified. After the NRC

walkdowns, TVA's threshold and criteria for material condition

walkdowns were changed to identify more deficient conditions. As

stated above, the TVA walkdowns have resulted in over 3000 WRs

(B0P and safety related) being written for deficient material

conditions.

The inspectors concluded that, in general, the prioritization and

scheduling of work items for restart was performed appropriately

and conservatively. However, there were weaknesses identified in

the backlog review process and during the implementation of one

design change notice (DCN). These weaknesses included:

1) some

backlogged items were either not reviewed for restart or were

inadequately reviewed by the Backlog Review Committee (BRC);

2)

some restart items were deleted from the outage schedule without

the knowledge of the applicable system engineer or the BRC (this

weakness was identified by the licensee); 3) the licensee's

scheduling of material condition walkdowns were not timely;

and

4) field installation of a DCN was not in accordance with the DCN

requirements.

Except for the issue concerning PVC jacketed cables

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(discussed in IR 50-327,328/93-35), the material condition of the

B0P should be satisfactory for operation after all planned

corrective actions are completed.

B0P Reliability

As discussed previously in this report, TVA performed a Secondary

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Plant Reliability Study which identified a number of BOP high

priority modifications and maintenance activities that needed to

be corrected before restart to improve the reliability of the B0P.

The SWEC B0P design study also recommended items that should be

addressed prior to restart. TVA took actions to address the

findings and recommendations from the reliability study and the

SWEC study.

The inspectors reviewed the TVA reliability study and the SWEC

design study, the prioritization and scheduling of the items from

the studies, the licensee's justification for items determined to

be non-restart, and performed field inspections to verify that

corrective actions were being adequately implemented.

The studies were determined to be thorough and comprehensive.

Appropriate corrective actions were planned and scheduled.

Adequate justifications were provided for the items that were

considered to be non-restart. The studies provided TVA management

with a better understanding of the condition of the B0P. The

corrective actions performed to date and those scheduled for

completion prior to restart should improve the reliability and

availability of the 80P.

Emeroent Issues

Subsequent to the licensee establishing the backlog of existing

work as of May 1,1993, numerous material deficiencies were

identified through the licensee's material condition walkdowns and

during other on-going work activities. The items were documented

in the licensee's corrective action program. The licensee was

evaluating all of the emergent issues to determine which items

needed to be corrected before restart. There were several

significant issues identified. These included the ERCW

containment isolation MOVs, PVC jacketed cable, turbine trip

circuitry, and fuses, etc. The ERCW H0Vs are discussed in this

report below. The PVC jacketed cables, turbine trip circuitry,

and fuses are discussed in IR 50-327,328/93-35. Corrective

actions were being performed to address the emergent issues

identified as restart items.

During this inspection, 24 (12 per unit) ERCW containment

isolation MOVs were identified that were wired to close on torque

switch trip rather than limit switch.

Problem evaluation report

SQPER 930302 addressed this issue and, after review, the licensee

determined the condition to not be a restart item.

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The inspectors reviewed the restart evaluation of SQPER 930302

which the licensee had prepared regarding the condition. The

actuators for these MOVs torque against the mechanical stop in the

90 degree gear box located between the Limitorque actuator and the

valve at valve closure. The vendor recommended limit switch

closure and advised the licensee that the gear box was not

intended to be torque closed. However, the gear boxes had been

subjected to testing in which the gear box was tested to 30 ft-lbs

of torque for 14,000 cycles and then to 67 ft-lbs. The evaluation

contained diagnostic test data that determined the torque values

to range from 22 to 49 ft-lbs for the Sequoyah MOVs.

The inspectors requested that the licensee perform a visual

inspection of a gear box. This request was an effort to determine

if any damage had occurred as a result of using the mechanical

stops to trip the torque switch and stop the valve motion rather

than the vendor recommended limit switch method.

The licensee submitted the results of an inspection and evaluation

of the gear box for 2-FCV-067-131-B, which had been subjected to a

torque condition of approximately 140 ft-lbs. This condition had

occurred due to the failure of a motor contactor to open properly

which caused the actuator motor to develop stall torque against

the gear box mechanical stop. The licensee determined this

approximate torque value using the Limitorque equation for stall

torque. The evaluation report indicated that there was no

degradation of the gears, grease, or gaskets for the gear box.

TVA had planned to replace all the gear boxes during the next unit

refueling outages and modify the electrical circuits to provide

for limit switch closure control of these valves as recommended by

the vendor.

Based on the findings of their inspection, the

recommendation was that TVA not replace the gear boxes but modify

the electrical circuits as planned.

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It should be noted that the safety function of these valves is to

close for containment isolation and they are only stroked an

estimated 10 times per year during leak rate testing. Therefore,

based on the results of the evaluation reviewed by the regional

inspectors, the NRC agrees that the replacement of the gear boxes

is not required. Modification of the closing circuits for these

valves should be performed during the next refueling outages for

each unit. The modification of the closing circuits for these

MOVs will be reviewed during the Phase II MOV inspection and is

identified as Inspector Followup Item 50-327,328/93-36-01, Review

the Electrical Modifications for ERCW MOVs.

The emergent issues for the 13 selected B0P systems and the

corrective actions being developed to address the more significant

items before restart were reviewed by NRC inspectors during the

inspections referenced above. The items that were determined to

be non-restart were reviewed also.

It was determined that the

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emergent issues were being evaluated for restart.

In general, the

items identified for correction before restart were considered to

be appropriate.

Based on the results of the inspections conducted in the B0P area during

the period June-August 1993, it was concluded that the corrective

actions already taken or planned to improve the material condition of

the B0P adequately addressed the more significant problems that have

contributed to the adverse trends in the reliability and availability of

B0P components and systems, as identified in the various studies.

However, there is still quite a bit of work remaining to be completed

before restart.

This includes backlogged work and emergent work

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activity.

Violations or deviations were not identified in the areas inspected.

5.

Quality Assurance (QA) Assessment and Oversight

The inspector held discussions with Site Quality personnel and reviewed

QA audits, assessments, and performance evaluations of B0P and safety

related activities conducted by the Site Quality organization. The

assessments and performance evaluations were part of the overall Nuclear

Assurance plan for oversight of restart activities at Sequoyah. The

objective of the Nuclear Assurance plan was to independently verify

completion and effective implementation of the Sequoyah Restart Plan by

assessing, overseeing, and trending station performance in relation to

the six " focus areas" identified in the Restart Plan. The inspector

reviewed results of the following Site Quality activities that were

either completed or in progress:

NA-SQ-93-033, Assessment of Design Change Process

NA-SQ-93-035, Maintenance Performance Evaluation Follow-up

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NA-SQ-93-047, Assessment of Surveillance Program Performance

SQA93308, Maintenance Audit

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In addition to reviewing results of the above activities, the inspector

reviewed several Weekly Nuclear Assurance Assessment of Restart Plan

reports and assessment results which provided inputs for the Weekly

Nuclear Assurance Assessment of Restart Plan.

The inspector found that the Site Quality organization has been heavily

involved in assessing restart activities.

This included observation of

numerous work activities in the field. Site Quality has been aggressive

in identifying work performance problems and other areas of weakness.

These efforts have identified areas to site senior management where

improvement is needed prior to restart. The inspector considered the QA

assessment and oversight activities to be a strength in the licensee's

restart efforts.

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Violations or deviations were not identified in the areas inspected.

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6.

Exit Interview

The inspection scope and results were summarized on August 20, 1993,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the 2nspection findings

listed below.

Proprietary information is not contained in this report.

Dissenting comments were not received fiom the licensee. The following

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finding was discussed:

IFI 50-327, 328/93-36-01, Review Electrical Modifications to ERCW

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H0Vs (paragraph 4).

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Acronyms and Initialisms

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B0P

Balance of Plant

BRC

Backlog Review Committee

DCN

Design Change Notice

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ERCW

Essential Raw Cooling Water

FCV

Flow Control Valve

IFI

Inspector Followup Item

IR

Inspection Report

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MOV

Motor Operated Valve

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PVC

Polyvinyl Chloride

QA

Quality Assurance

QC

Quality Control

SQPER

Sequoyah Problem Evaluation Report

SWEC

Stone and Webster Engineering Corporation

TVA

Tennessee Valley Authority

WR

Work Request

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