ML20054F582
ML20054F582 | |
Person / Time | |
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Site: | Brunswick |
Issue date: | 06/04/1982 |
From: | Burger C, Hardin A NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
References | |
PNO-II-82-061A, PNO-II-82-61A, NUDOCS 8206170125 | |
Download: ML20054F582 (2) | |
Similar Documents at Brunswick | |
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Category:PRELIMINARY NOTIFICATION OF EVENT OR OCCURRENCE (PNO
MONTHYEARPNO-II-99-045, on 991018,Hurricane Irene Was Located Approx 105 Miles East of Cape Hatteras,Nc.Ctr of Hurricane Was Estimated Near Latitude 35.6 North & Longitude 73.8 West. Storm Was Moving Northeast at 35 Mph1999-10-18018 October 1999
[Table view]PNO-II-99-045:on 991018,Hurricane Irene Was Located Approx 105 Miles East of Cape Hatteras,Nc.Ctr of Hurricane Was Estimated Near Latitude 35.6 North & Longitude 73.8 West. Storm Was Moving Northeast at 35 Mph PNO-II-99-037H, on 990915,Hurricane Floyd Was Located Approx 168 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 31.3 North & Longitude 79.0 West.Storm Was Moving North at 17 Mph with Max Winds at 115 Mph1999-09-15015 September 1999 PNO-II-99-037H:on 990915,Hurricane Floyd Was Located Approx 168 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 31.3 North & Longitude 79.0 West.Storm Was Moving North at 17 Mph with Max Winds at 115 Mph PNO-II-99-037G, on 990915,Hurricane Floyd Was Located Approx 216 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 30.6 North & Longitude 79.1 West.Storm Was Moving north-northwest at 14 Mph with Max Winds at 125 Mph1999-09-15015 September 1999 PNO-II-99-037G:on 990915,Hurricane Floyd Was Located Approx 216 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 30.6 North & Longitude 79.1 West.Storm Was Moving north-northwest at 14 Mph with Max Winds at 125 Mph PNO-II-99-037F, on 990915,Hurricane Floyd Was Located Approx 350 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.9 North & Longitude 79.0 West. Storm Was Moving north-northwest at 14 Mph1999-09-15015 September 1999 PNO-II-99-037F:on 990915,Hurricane Floyd Was Located Approx 350 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.9 North & Longitude 79.0 West. Storm Was Moving north-northwest at 14 Mph PNO-II-99-037E, on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.3 North & Longitude 78.8 West. Storm Was Moving north-northwest at 14 Mph1999-09-15015 September 1999 PNO-II-99-037E:on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.3 North & Longitude 78.8 West. Storm Was Moving north-northwest at 14 Mph PNO-II-99-037D, on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 28.8 North & Longitude 78.8 West. Storm Was Moving Northwest at 14 Mph.Max Winds Were 140 Mph1999-09-15015 September 1999 PNO-II-99-037D:on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 28.8 North & Longitude 78.8 West. Storm Was Moving Northwest at 14 Mph.Max Winds Were 140 Mph PNO-II-99-035, on 990830,util Secured from Notification of Unusual Event After Hurricane Warning Lifted for Area.Plant Had Been Placed in Hot Shutdown Due to Predicted Hurricane Track.Unit 2 Commenced Restart on 9908311999-08-31031 August 1999 PNO-II-99-035:on 990830,util Secured from Notification of Unusual Event After Hurricane Warning Lifted for Area.Plant Had Been Placed in Hot Shutdown Due to Predicted Hurricane Track.Unit 2 Commenced Restart on 990831 PNO-II-99-033, on 990830,Hurricane Dennis Was Located Approx 72 Miles Southeast of Bsep.No Significant Damage Has Been Sustained at Site.Ge Facility Suspended Fuel Fabrication Processes & No Significant Damage Was Sustained1999-08-30030 August 1999 PNO-II-99-033:on 990830,Hurricane Dennis Was Located Approx 72 Miles Southeast of Bsep.No Significant Damage Has Been Sustained at Site.Ge Facility Suspended Fuel Fabrication Processes & No Significant Damage Was Sustained PNO-II-98-050, on 981123,licensee Declared Notification of Unusual Event,Due to Release of Chlorine Gas from Svc Water Injection Sys in Chlorination Bldg.Personnel Were Moved to Alternate Locations Away from Gas Leak,As Precautionary1998-11-24024 November 1998 PNO-II-98-050:on 981123,licensee Declared Notification of Unusual Event,Due to Release of Chlorine Gas from Svc Water Injection Sys in Chlorination Bldg.Personnel Were Moved to Alternate Locations Away from Gas Leak,As Precautionary PNO-II-98-039D, on 980827,update on Hurricane Bonnie Made. Walkdowns Confirmed,No Significant Damage to Security Barriers.Licensee Preparations for Plant Restart Continuing, Including Restoration of Warning Sirens1998-08-27027 August 1998 PNO-II-98-039D:on 980827,update on Hurricane Bonnie Made. Walkdowns Confirmed,No Significant Damage to Security Barriers.Licensee Preparations for Plant Restart Continuing, Including Restoration of Warning Sirens PNO-II-98-039C, on 980827,update on Hurricane Bonnie Made. No Significant Damage Has Occurred at Brunswick Plant or GE Fuel Fabrication Facility.Licensee Continues to Staff Technical Support Ctr & Emergency Operations Facility1998-08-27027 August 1998 PNO-II-98-039C:on 980827,update on Hurricane Bonnie Made. No Significant Damage Has Occurred at Brunswick Plant or GE Fuel Fabrication Facility.Licensee Continues to Staff Technical Support Ctr & Emergency Operations Facility PNO-II-98-039B, on 980826,update on Hurricane Bonnie Made. Hurricane Force Winds Have Been Experienced at Site,But No Significant Damage Has Occurred.Licensee Continues to Staff Emergency Facilities.No Other Damage Has Been Reported1998-08-26026 August 1998 PNO-II-98-039B:on 980826,update on Hurricane Bonnie Made. Hurricane Force Winds Have Been Experienced at Site,But No Significant Damage Has Occurred.Licensee Continues to Staff Emergency Facilities.No Other Damage Has Been Reported PNO-II-98-039A, on 980826,update on Hurricane Bonnie Made. Brunswick Resident Inspectors & One Regional Inspector Remain on Site to Monitor Licensee Activities.Region II State Liaison Officer Arrived in Raleigh Area1998-08-26026 August 1998 PNO-II-98-039A:on 980826,update on Hurricane Bonnie Made. Brunswick Resident Inspectors & One Regional Inspector Remain on Site to Monitor Licensee Activities.Region II State Liaison Officer Arrived in Raleigh Area PNO-II-98-039, on 980525,preparations for Hurricane Bonnie Made.Licensee Monitoring Progress of Hurricane in Order to Have Both Units in Cold Shutdown Three H Prior to Arrival of Hurricane Force Winds on Site1998-08-25025 August 1998 PNO-II-98-039:on 980525,preparations for Hurricane Bonnie Made.Licensee Monitoring Progress of Hurricane in Order to Have Both Units in Cold Shutdown Three H Prior to Arrival of Hurricane Force Winds on Site PNO-II-93-067, on 931130,util Announced That Indepth Independent Review Found No Evidence to Support Allegations That Util Discovered Cracks in Plant Core Shrouds in 1984, But Covered Up Existance of Cracks Until 19931993-11-30030 November 1993 PNO-II-93-067:on 931130,util Announced That Indepth Independent Review Found No Evidence to Support Allegations That Util Discovered Cracks in Plant Core Shrouds in 1984, But Covered Up Existance of Cracks Until 1993 PNO-II-93-060, on 931108,licensee Made NOUE When Potentially Contaminated Employee Transported to Dosher Memorial Hosp in Southport,Nc.Employee Partially Surveyed Due to Injuries. Employee Subsequently Determined Not to Be Contaminated1993-11-0808 November 1993 PNO-II-93-060:on 931108,licensee Made NOUE When Potentially Contaminated Employee Transported to Dosher Memorial Hosp in Southport,Nc.Employee Partially Surveyed Due to Injuries. Employee Subsequently Determined Not to Be Contaminated PNO-II-93-050, on 930928,media Issued Statement Re Core Shroud Cracks at Facility.Activity Delayed Current Refueling Outage Schedule.Licensee Developing Permanent Mechanical Repair.State of Nc Informed1993-09-28028 September 1993 PNO-II-93-050:on 930928,media Issued Statement Re Core Shroud Cracks at Facility.Activity Delayed Current Refueling Outage Schedule.Licensee Developing Permanent Mechanical Repair.State of Nc Informed PNO-II-93-042, on 930830,NRC Entered Monitoring Mode, Responding to Hurricane Emily,Located SE of Brunswick Plant. Inspectors Observing Licensee Preparations.Region II Informed States of Nc & VA of Activity1993-08-30030 August 1993 PNO-II-93-042:on 930830,NRC Entered Monitoring Mode, Responding to Hurricane Emily,Located SE of Brunswick Plant. Inspectors Observing Licensee Preparations.Region II Informed States of Nc & VA of Activity PNO-II-92-007, on 920202,plant Experienced Reactor Scram from 79% Power During Main Turbine Cv Testing.Licensee Actions Towards Determining/Correcting Root Cause of Scram Have Been Focused on EHC Sys1992-02-0505 February 1992 PNO-II-92-007:on 920202,plant Experienced Reactor Scram from 79% Power During Main Turbine Cv Testing.Licensee Actions Towards Determining/Correcting Root Cause of Scram Have Been Focused on EHC Sys PNO-II-90-047B, on 900825,AIT Conducted Meeting Which Was Followed by Press Conference to Discuss Excessive Cooldown Rate in Reactor Vessel Lower Portion Experienced During 900816 & 19 Reactor Trips & Other Listed Items1990-08-30030 August 1990 PNO-II-90-047B:on 900825,AIT Conducted Meeting Which Was Followed by Press Conference to Discuss Excessive Cooldown Rate in Reactor Vessel Lower Portion Experienced During 900816 & 19 Reactor Trips & Other Listed Items PNO-II-90-047A, provides as Update to 900821 Notification Re 900819 Reactor Trip,Findings of Investigation.Reactor Trip Due to Closure of MSIVs Resulted from Primary Containment Isolation Sys Testing.Util Correcting Safety Relief Valves1990-08-24024 August 1990 PNO-II-90-047A:provides as Update to 900821 Notification Re 900819 Reactor Trip,Findings of Investigation.Reactor Trip Due to Closure of MSIVs Resulted from Primary Containment Isolation Sys Testing.Util Correcting Safety Relief Valves PNO-II-89-066, licensees Prepared for Adverse Weather Conditions Due to Hurricane.Briefings Held W/Key Managers on Responsibilities to Check All Trailers,Secure Crane Hooks & Increase Emergency Food Supplies1989-09-21021 September 1989 PNO-II-89-066:licensees Prepared for Adverse Weather Conditions Due to Hurricane.Briefings Held W/Key Managers on Responsibilities to Check All Trailers,Secure Crane Hooks & Increase Emergency Food Supplies PNO-II-89-067, on 890921,alert Declared Due to Loss of Audible Annunciators to Control Board.Caused by Short in Annunciator Reset Circuitry in safety-related Control Panel. Short Removed & Annunciator Operability Verified1989-09-21021 September 1989 PNO-II-89-067:on 890921,alert Declared Due to Loss of Audible Annunciators to Control Board.Caused by Short in Annunciator Reset Circuitry in safety-related Control Panel. Short Removed & Annunciator Operability Verified PNO-II-89-066A, updates Status of Hurricane Hugo for Nuclear Facilities in Southeast.Manning of Incident Response Ctr by Region II Continuing1989-09-21021 September 1989 PNO-II-89-066A:updates Status of Hurricane Hugo for Nuclear Facilities in Southeast.Manning of Incident Response Ctr by Region II Continuing PNO-II-89-048, on 890617,reactor Manually Scrammed Following Loss of Offsite Power.Caused by Troubleshooting in Progress to Investigate Ground on Startup Auxiliary Transformer (Sat).Plant to Remain Shutdown Until SAT Repaired1989-06-19019 June 1989 PNO-II-89-048:on 890617,reactor Manually Scrammed Following Loss of Offsite Power.Caused by Troubleshooting in Progress to Investigate Ground on Startup Auxiliary Transformer (Sat).Plant to Remain Shutdown Until SAT Repaired PNO-II-88-043C, Augmented Insp Team Dispatched to Site on 880715 & Departed on 880722,after Informal Debriefing W/ Licensee on Insp Findings.Team Continues to Review Several Mod Packages & Positions Re Dc Motor Deficiencies1988-07-25025 July 1988 PNO-II-88-043C:Augmented Insp Team Dispatched to Site on 880715 & Departed on 880722,after Informal Debriefing W/ Licensee on Insp Findings.Team Continues to Review Several Mod Packages & Positions Re Dc Motor Deficiencies PNO-II-88-043B, on 880722,augmented Insp Team at Brunswick Departs.Team Completed Review of Events & Associated Corrective Actions for Equipment Failures Encountered During Shutdown & DC Motor Problems1988-07-22022 July 1988 PNO-II-88-043B:on 880722,augmented Insp Team at Brunswick Departs.Team Completed Review of Events & Associated Corrective Actions for Equipment Failures Encountered During Shutdown & DC Motor Problems PNO-II-88-043A, on 880715,augmented Insp Team Reviewed Events & Associated Corrective Actions for Equipment Failures.All Repairs Completed on 880716 Except Testing.Request for HPCI Limiting Condition for Operation Extension Granted1988-07-20020 July 1988 PNO-II-88-043A:on 880715,augmented Insp Team Reviewed Events & Associated Corrective Actions for Equipment Failures.All Repairs Completed on 880716 Except Testing.Request for HPCI Limiting Condition for Operation Extension Granted PNO-II-88-043, on 880715,Augmented Insp Team Dispatched to Plant to Review Equipment Failure Events That Were Encountered During Planned Shutdown of Facility,Including Failure of F006 HPCI Valve1988-07-15015 July 1988 PNO-II-88-043:on 880715,Augmented Insp Team Dispatched to Plant to Review Equipment Failure Events That Were Encountered During Planned Shutdown of Facility,Including Failure of F006 HPCI Valve PNO-II-88-042, on 880713,NRC Notified of Util Intent to Initiate Shutdown of Unit to Repair F006 Injection Valve on HPCI Sys.Shutdown Prompted by Evaluation Indicating That Inadequate Torque May Be Available Under Reduced Voltage1988-07-13013 July 1988 PNO-II-88-042:on 880713,NRC Notified of Util Intent to Initiate Shutdown of Unit to Repair F006 Injection Valve on HPCI Sys.Shutdown Prompted by Evaluation Indicating That Inadequate Torque May Be Available Under Reduced Voltage PNO-II-88-014, on 880219,util Discovered Random Failures of 5/16 Inch Silicon/Bronze Carriage Bolts Which Are Used to Tie Electrical Busses Together within Panels.Bolts Replaced. NRC Pursuing Generic Implications W/Ge1988-02-26026 February 1988 PNO-II-88-014:on 880219,util Discovered Random Failures of 5/16 Inch Silicon/Bronze Carriage Bolts Which Are Used to Tie Electrical Busses Together within Panels.Bolts Replaced. NRC Pursuing Generic Implications W/Ge PNO-II-88-003, licensee Identified 4 Inch 85% Throughwall Circumferential Indication on E 12-inch Inlet Recirculation Riser to Nozzle Safe & Weld,While Performing Automated Ultrasonic Testing1988-01-14014 January 1988 PNO-II-88-003:licensee Identified 4 Inch 85% Throughwall Circumferential Indication on E 12-inch Inlet Recirculation Riser to Nozzle Safe & Weld,While Performing Automated Ultrasonic Testing PNO-II-88-001, on 880102,primary Containment Isolation Valves Drywell Equipment & Floor Drains Failed to Close Automatically After Receipt of Valid Group 2 Isolation Signal.Cause Under Investigation.Insp Team Dispatched1988-01-0404 January 1988 PNO-II-88-001:on 880102,primary Containment Isolation Valves Drywell Equipment & Floor Drains Failed to Close Automatically After Receipt of Valid Group 2 Isolation Signal.Cause Under Investigation.Insp Team Dispatched PNO-II-87-023, on 870406,unit Shut Down for More than 48 H Due to Increase in Unidentified Leakage in Drywell.Caused by Leaks in Recirculation Pump a Discharge Valve Packing & Outboard Feedwater Sys Check Valves1987-04-0707 April 1987 PNO-II-87-023:on 870406,unit Shut Down for More than 48 H Due to Increase in Unidentified Leakage in Drywell.Caused by Leaks in Recirculation Pump a Discharge Valve Packing & Outboard Feedwater Sys Check Valves PNO-II-86-065, on 860917,reactor Manually Tripped from 3% Power Due to Decreasing Condenser Vacuum.Caused by Leak in Condenser Tube Cleaning Sys & Flooding of Condenser Inlet Pit.Leak Isolated & Plant Taken to Hot Shutdown1986-09-19019 September 1986 PNO-II-86-065:on 860917,reactor Manually Tripped from 3% Power Due to Decreasing Condenser Vacuum.Caused by Leak in Condenser Tube Cleaning Sys & Flooding of Condenser Inlet Pit.Leak Isolated & Plant Taken to Hot Shutdown PNO-II-86-024, on 860326,reactor Scrammed Due to Turbine Trip.Caused by Spurious High Reactor Water Level Signal. Plant Brought to Cold Shutdown to Repair Degraded Reactor Recirculation Pump Seal.Outage Expected to Last 6 Days1986-03-27027 March 1986 PNO-II-86-024:on 860326,reactor Scrammed Due to Turbine Trip.Caused by Spurious High Reactor Water Level Signal. Plant Brought to Cold Shutdown to Repair Degraded Reactor Recirculation Pump Seal.Outage Expected to Last 6 Days PNO-II-86-017A, on 860223,some Contamination Found on Protective Clothing & Stretcher Used to Transfer Const Worker Who Fell in Drywell.Surveys Show Contamination Confined to Single Spot1986-02-25025 February 1986 PNO-II-86-017A:on 860223,some Contamination Found on Protective Clothing & Stretcher Used to Transfer Const Worker Who Fell in Drywell.Surveys Show Contamination Confined to Single Spot PNO-II-86-017, on 860223,contract Const Worker Lost Footing & Fell 3 Ft in Drywell.Cause Not Stated.Worker Sent to Hosp.No Contamination Found on Worker,Protective Clothing,In Ambulance or at Hosp1986-02-24024 February 1986 PNO-II-86-017:on 860223,contract Const Worker Lost Footing & Fell 3 Ft in Drywell.Cause Not Stated.Worker Sent to Hosp.No Contamination Found on Worker,Protective Clothing,In Ambulance or at Hosp PNO-II-85-091, Region II Dispatched Emergency Response Specialist to Plant to Set Up High Frequency Radio Communications as Result of Hurricane Gloria.Unit 1 in Shutdown for Refueling1985-10-0303 October 1985 PNO-II-85-091:Region II Dispatched Emergency Response Specialist to Plant to Set Up High Frequency Radio Communications as Result of Hurricane Gloria.Unit 1 in Shutdown for Refueling PNO-II-85-093, on 850926,Unit 2 Shut Down & on 850927,Unit 1 Shut Down Due to Hurricane Gloria w/35-40 Miles Per Hour Winds.Unit 1 Expected to Restart on 850927.Unit 2 Will Remain Shut Down for 2 Wks for Repair of LPSI Valves1985-09-27027 September 1985 PNO-II-85-093:on 850926,Unit 2 Shut Down & on 850927,Unit 1 Shut Down Due to Hurricane Gloria w/35-40 Miles Per Hour Winds.Unit 1 Expected to Restart on 850927.Unit 2 Will Remain Shut Down for 2 Wks for Repair of LPSI Valves PNO-II-85-092, on 850926,Hurricane Gloria Located About 240 Miles South of Cape Hatteras,Nc,Moving North Northwest at 15 to 20 Miles Per Hour.Brunswick Unit 1 in Refueling Shutdown,Unit 2 Shut Down & Surry 1 & 2 at Full Power1985-09-26026 September 1985 PNO-II-85-092:on 850926,Hurricane Gloria Located About 240 Miles South of Cape Hatteras,Nc,Moving North Northwest at 15 to 20 Miles Per Hour.Brunswick Unit 1 in Refueling Shutdown,Unit 2 Shut Down & Surry 1 & 2 at Full Power PNO-II-85-070B, monitoring of Tropical Storm Bob Terminated.Natl Weather Svc No Longer Issuing Special Repts on Storm1985-07-26026 July 1985 PNO-II-85-070B:monitoring of Tropical Storm Bob Terminated.Natl Weather Svc No Longer Issuing Special Repts on Storm PNO-II-85-070A, on 850724,tropical Storm Bob Near Latitude 29.5 North & Longitude 80.3 West,About 40 Miles east-southeast of Daytona Beach,Fl.Storm Will Continue in Direction for Next 24 H.Precautions Will Be Taken If Needed1985-07-24024 July 1985 PNO-II-85-070A:on 850724,tropical Storm Bob Near Latitude 29.5 North & Longitude 80.3 West,About 40 Miles east-southeast of Daytona Beach,Fl.Storm Will Continue in Direction for Next 24 H.Precautions Will Be Taken If Needed PNO-II-84-069A, update to PNO-II-84-069,issued on 841010. Region II Continues to Monitor Hurricane Josephine,Centered Near Latitude 29.4 North & Longitude 72.5 West1984-10-11011 October 1984 PNO-II-84-069A:update to PNO-II-84-069,issued on 841010. Region II Continues to Monitor Hurricane Josephine,Centered Near Latitude 29.4 North & Longitude 72.5 West PNO-II-83-073, on 830912,CP&L Declared Alert in Accordance W/Plant Emergency plan,15 Minutes After All Annunciators Alarmed But Could Not Be Reset.Licensee Continued Plant Operation & Assigned Addl People to Increase Surveillance1983-09-12012 September 1983 PNO-II-83-073:on 830912,CP&L Declared Alert in Accordance W/Plant Emergency plan,15 Minutes After All Annunciators Alarmed But Could Not Be Reset.Licensee Continued Plant Operation & Assigned Addl People to Increase Surveillance PNO-II-82-088, on 820728,licensee Reported Updated Info Re Failure of shaft-driven Cooling Pump on Emergency Diesel Generator 2.Caused by Sheared Cap Screws & Broken Dowel Pins in Pump Coupling.Cap Screws & Dowel Pins Replaced1982-07-28028 July 1982 PNO-II-82-088:on 820728,licensee Reported Updated Info Re Failure of shaft-driven Cooling Pump on Emergency Diesel Generator 2.Caused by Sheared Cap Screws & Broken Dowel Pins in Pump Coupling.Cap Screws & Dowel Pins Replaced PNO-II-82-085, on 820628,unit Shut Down After Determining That Required Surveillance Test Not Be Performed Prior to Exceeding Limiting Condition for Operation.Shutdown of 10 Days Anticipated1982-07-20020 July 1982 PNO-II-82-085:on 820628,unit Shut Down After Determining That Required Surveillance Test Not Be Performed Prior to Exceeding Limiting Condition for Operation.Shutdown of 10 Days Anticipated ML20054F5821982-06-0404 June 1982 PNO-II-82-61A,updating 820603 Submittal Re Bent Incore Neutron Range Monitoring Tubes Found Beneath Reactor Vessel.Sabotage Suspected.Security Measures Including Daily Walkthrough Insp & Addl Patrols Initiated PNO-II-82-060, on 820527,during Inservice Insp,Pinhole Leak Discovered in 6-inch RWCU Sys Suction Piping.Reactor Defueled.Southwest Research Inst Evaluating Defective Pipe Section1982-05-28028 May 1982 PNO-II-82-060:on 820527,during Inservice Insp,Pinhole Leak Discovered in 6-inch RWCU Sys Suction Piping.Reactor Defueled.Southwest Research Inst Evaluating Defective Pipe Section PNO-II-82-030, on 820319,telcon Bomb Threat Received.Initial Search Yielded Negative Results.Addl Search Being Performed. Authorities Not Notified1982-03-19019 March 1982 PNO-II-82-030:on 820319,telcon Bomb Threat Received.Initial Search Yielded Negative Results.Addl Search Being Performed. Authorities Not Notified 1999-09-15 Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS MONTHYEARPNO-II-99-045, on 991018,Hurricane Irene Was Located Approx 105 Miles East of Cape Hatteras,Nc.Ctr of Hurricane Was Estimated Near Latitude 35.6 North & Longitude 73.8 West. Storm Was Moving Northeast at 35 Mph1999-10-18018 October 1999
[Table view]PNO-II-99-045:on 991018,Hurricane Irene Was Located Approx 105 Miles East of Cape Hatteras,Nc.Ctr of Hurricane Was Estimated Near Latitude 35.6 North & Longitude 73.8 West. Storm Was Moving Northeast at 35 Mph IR 05000324/19990061999-10-0606 October 1999 Insp Repts 50-324/99-06 & 50-325/99-06 on 990801-0911.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support PNO-II-99-037D, on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 28.8 North & Longitude 78.8 West. Storm Was Moving Northwest at 14 Mph.Max Winds Were 140 Mph1999-09-15015 September 1999 PNO-II-99-037D:on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 28.8 North & Longitude 78.8 West. Storm Was Moving Northwest at 14 Mph.Max Winds Were 140 Mph PNO-II-99-037E, on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.3 North & Longitude 78.8 West. Storm Was Moving north-northwest at 14 Mph1999-09-15015 September 1999 PNO-II-99-037E:on 990915,Hurricane Floyd Was Located Approx 380 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.3 North & Longitude 78.8 West. Storm Was Moving north-northwest at 14 Mph PNO-II-99-037F, on 990915,Hurricane Floyd Was Located Approx 350 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.9 North & Longitude 79.0 West. Storm Was Moving north-northwest at 14 Mph1999-09-15015 September 1999 PNO-II-99-037F:on 990915,Hurricane Floyd Was Located Approx 350 Miles Southeast of Wilmington,Nc.Ctr of Hurricane Was Estimated Near Latitude 29.9 North & Longitude 79.0 West. Storm Was Moving north-northwest at 14 Mph PNO-II-99-037H, on 990915,Hurricane Floyd Was Located Approx 168 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 31.3 North & Longitude 79.0 West.Storm Was Moving North at 17 Mph with Max Winds at 115 Mph1999-09-15015 September 1999 PNO-II-99-037H:on 990915,Hurricane Floyd Was Located Approx 168 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 31.3 North & Longitude 79.0 West.Storm Was Moving North at 17 Mph with Max Winds at 115 Mph PNO-II-99-037G, on 990915,Hurricane Floyd Was Located Approx 216 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 30.6 North & Longitude 79.1 West.Storm Was Moving north-northwest at 14 Mph with Max Winds at 125 Mph1999-09-15015 September 1999 PNO-II-99-037G:on 990915,Hurricane Floyd Was Located Approx 216 Miles Southeast of Bsep.Ctr of Hurricane Was Estimated Near Latitude 30.6 North & Longitude 79.1 West.Storm Was Moving north-northwest at 14 Mph with Max Winds at 125 Mph PNO-II-99-035, on 990830,util Secured from Notification of Unusual Event After Hurricane Warning Lifted for Area.Plant Had Been Placed in Hot Shutdown Due to Predicted Hurricane Track.Unit 2 Commenced Restart on 9908311999-08-31031 August 1999 PNO-II-99-035:on 990830,util Secured from Notification of Unusual Event After Hurricane Warning Lifted for Area.Plant Had Been Placed in Hot Shutdown Due to Predicted Hurricane Track.Unit 2 Commenced Restart on 990831 PNO-II-99-033, on 990830,Hurricane Dennis Was Located Approx 72 Miles Southeast of Bsep.No Significant Damage Has Been Sustained at Site.Ge Facility Suspended Fuel Fabrication Processes & No Significant Damage Was Sustained1999-08-30030 August 1999 PNO-II-99-033:on 990830,Hurricane Dennis Was Located Approx 72 Miles Southeast of Bsep.No Significant Damage Has Been Sustained at Site.Ge Facility Suspended Fuel Fabrication Processes & No Significant Damage Was Sustained IR 05000324/19990051999-08-27027 August 1999 Insp Repts 50-324/99-05 & 50-325/99-05 on 990620-0731.Two Violations Noted Being Treated as Ncv.Major Areas Inspected: Operations,Maint & Plant Support IR 05000324/19990041999-07-19019 July 1999 Insp Repts 50-324/99-04 & 50-325/99-04 on 990509-0619. Non-cited Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support.Includes Results of Y2K Readiness Program Review IR 05000324/19990031999-06-0707 June 1999 Insp Repts 50-324/99-03 & 50-325/99-03 on 990328-0508.Two Violations Noted & Being Treated as non-cited Violations. Major Areas Inspected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000324/19990021999-04-26026 April 1999 Forwards Insp Repts 50-324/99-02 & 50-325/99-02 on 990214-0327.No Violations Noted.Major Areas Inspected: Licensee Operation,Engineering,Maint & Plant Support IR 05000324/19980141999-03-18018 March 1999 Insp Repts 50-324/98-14 & 50-325/98-14 on 990111-15,25 & 29. No Violations Noted.Major Areas Inspected:Licensee Calculations,Analysis,Performance Test Procedures & Other Engineering Activities IR 05000324/19990011999-03-15015 March 1999 Insp Repts 50-324/99-01 & 50-325/99-01 on 990103-0213.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000324/19980111999-01-28028 January 1999 Insp Repts 50-324/98-11 & 50-325/98-11 on 981122-990102.No Violations Noted.Major Areas Inspected:Licensee Operations, Maint & Plant Support ML20198P0261998-12-21021 December 1998 Notice of Violation from Insp on 981011-1121.Violation Noted:On 981030,licensee Failed to Correctly Shutdown & Verify That Unit 1 Standby Gas Treatment Sys in Standby Alignment Per Section 7.1 of Procedure 1OP-10 IR 05000324/19980101998-12-21021 December 1998 Insp Repts 50-324/98-10 & 50-325/98-10 on 981011-1121. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support.Also Includes Results of Engineering & Health Physics Insp PNO-II-98-050, on 981123,licensee Declared Notification of Unusual Event,Due to Release of Chlorine Gas from Svc Water Injection Sys in Chlorination Bldg.Personnel Were Moved to Alternate Locations Away from Gas Leak,As Precautionary1998-11-24024 November 1998 PNO-II-98-050:on 981123,licensee Declared Notification of Unusual Event,Due to Release of Chlorine Gas from Svc Water Injection Sys in Chlorination Bldg.Personnel Were Moved to Alternate Locations Away from Gas Leak,As Precautionary IR 05000324/19980131998-11-24024 November 1998 Partially Withheld Insp Repts 50-324/98-13 & 50-325/98-13 on 981026-30 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected:Aspects of Licensee Plant Support IR 05000324/19980091998-11-0909 November 1998 Insp Repts 50-324/98-09 & 50-325/98-09 on 980830-1010. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support ML20195G4191998-11-0909 November 1998 Notice of Violation from Insp on 980830-1010.Violation Noted:On 980916,licensee Failed to Perform Section 7.1.5 of Procedure OMST-RHR-28Q as Required When Returning Flow Transmitter E11-FT-3338 to Service IR 05000324/19980081998-09-28028 September 1998 Insp Repts 50-324/98-08 & 50-325/98-08 on 980719-0829.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support PNO-II-98-039D, on 980827,update on Hurricane Bonnie Made. Walkdowns Confirmed,No Significant Damage to Security Barriers.Licensee Preparations for Plant Restart Continuing, Including Restoration of Warning Sirens1998-08-27027 August 1998 PNO-II-98-039D:on 980827,update on Hurricane Bonnie Made. Walkdowns Confirmed,No Significant Damage to Security Barriers.Licensee Preparations for Plant Restart Continuing, Including Restoration of Warning Sirens PNO-II-98-039C, on 980827,update on Hurricane Bonnie Made. No Significant Damage Has Occurred at Brunswick Plant or GE Fuel Fabrication Facility.Licensee Continues to Staff Technical Support Ctr & Emergency Operations Facility1998-08-27027 August 1998 PNO-II-98-039C:on 980827,update on Hurricane Bonnie Made. No Significant Damage Has Occurred at Brunswick Plant or GE Fuel Fabrication Facility.Licensee Continues to Staff Technical Support Ctr & Emergency Operations Facility PNO-II-98-039B, on 980826,update on Hurricane Bonnie Made. Hurricane Force Winds Have Been Experienced at Site,But No Significant Damage Has Occurred.Licensee Continues to Staff Emergency Facilities.No Other Damage Has Been Reported1998-08-26026 August 1998 PNO-II-98-039B:on 980826,update on Hurricane Bonnie Made. Hurricane Force Winds Have Been Experienced at Site,But No Significant Damage Has Occurred.Licensee Continues to Staff Emergency Facilities.No Other Damage Has Been Reported PNO-II-98-039A, on 980826,update on Hurricane Bonnie Made. Brunswick Resident Inspectors & One Regional Inspector Remain on Site to Monitor Licensee Activities.Region II State Liaison Officer Arrived in Raleigh Area1998-08-26026 August 1998 PNO-II-98-039A:on 980826,update on Hurricane Bonnie Made. Brunswick Resident Inspectors & One Regional Inspector Remain on Site to Monitor Licensee Activities.Region II State Liaison Officer Arrived in Raleigh Area PNO-II-98-039, on 980525,preparations for Hurricane Bonnie Made.Licensee Monitoring Progress of Hurricane in Order to Have Both Units in Cold Shutdown Three H Prior to Arrival of Hurricane Force Winds on Site1998-08-25025 August 1998 PNO-II-98-039:on 980525,preparations for Hurricane Bonnie Made.Licensee Monitoring Progress of Hurricane in Order to Have Both Units in Cold Shutdown Three H Prior to Arrival of Hurricane Force Winds on Site IR 05000324/19980071998-08-11011 August 1998 Insp Repts 50-324/98-07 & 50-325/98-07 on 980607-0718. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20237B9211998-08-11011 August 1998 Notice of Violation from Insp on 980607-0718.Violation Noted:Licensee Failed to Accomplish Activities Affecting Quality in Accordance W/Documented Instructions in Procedures for Listed Examples IR 05000324/19980061998-07-0606 July 1998 Insp Repts 50-324/98-06 & 50-325/98-06 on 980426-0606. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20236N9451998-07-0606 July 1998 Notice of Violations from Insp on 980426-0606.Violations Noted:On 980521,licensee Made Temporary Procedure Change That Altered Intent of Maint Surveillance Test 1MST-DG11R, DG-1 Loading Test,By Substituting 25 for 50 Horsepower Load IR 05000324/19983001998-06-15015 June 1998 NRC Operator Licensing Exam Repts 50-324/98-300 & 50-325/98-300 on 980508-15.Six SRO & Four RO Candidates Tested.All Passed Exam.One Candidate Identified as Having Some Performance Weaknesses ML20249A2191998-06-0101 June 1998 Notice of Violation from Insp on 980315-0425.Violation Noted:On 980331 Licensee Failed to Accomplish Scaffolding Erection Activities in Accordance W/Documented Procedure OMMM-022 IR 05000324/19980051998-06-0101 June 1998 Insp Repts 50-324/98-05 & 50-325/98-05 on 980315-0425. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20216H4431998-04-16016 April 1998 Insp Repts 50-324/98-04 & 50-325/98-04 on 980209-13,0309-12 & 16-20.Violations Noted.Major Areas inspected:follow-up on Licensee Corrective Actions for Electrical Equipment Environ Qualification & Review of Instrument Response Time Testing ML20216H4341998-04-16016 April 1998 Notice of Violation from Insp on 980209-13,0309-12 & 16-20. Violation Noted:On 970603,licensee Failed to Accomplish Activities Affecting Quality in Accordance W/Procedure EGR-NGGC-0005 IR 05000324/19980031998-04-13013 April 1998 Insp Repts 50-324/98-03 & 50-325/98-03 on 980201-0314.No Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support.Also Includes Results of Health Physics Insp by Regional Inspectors ML20217C8011998-03-16016 March 1998 Notice of Violation from Insp on 980126-30.Violation Noted: Rev 46 to Licensee Emergency Plan Decreased Effectiveness of Plan That Adopted Regulatory Provision for Biennial Exercise ML20217C8061998-03-16016 March 1998 Insp Repts 50-324/98-01 & 50-325/98-01 on 980126-30. Violations Noted.Major Areas Inspected:Emergency Preparedness Exercise ML20216B1741998-03-0202 March 1998 Insp Repts 50-324/97-15 & 50-325/97-15 on 971228-980131. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support ML20216B1621998-03-0202 March 1998 Notice of Violation from Insp on 971228-980131.Violation Noted:On 971203 & 971230,for Unit 1 & 971203,971210 & 971220 & 980104 for Unit 2,Condition Repts Were Not Initiated to Address Repetitive Failures of Plant Computer ML20202D3161998-02-0505 February 1998 Omitted Page 42 to Insp Repts 50-324/97-13 & 50-325/97-13 Transmitted on 980123 IR 07100109/20120271998-01-23023 January 1998 Notice of Violation from Insp on 971109-1227.Violation Noted:On 971209,inspector Determined That Licensee Had Not Maintained Data Sheets or Logs for Equipment Alignment ML20199G7501998-01-23023 January 1998 Insp Repts 50-324/97-13 & 50-325/97-13 on 971109-1227. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support.Includes Results of Maint, Engineering & FP Insps ML20198N6461997-12-30030 December 1997 Notice of Violation from Insp on 971209-12.Violation Noted: on 971118,locked High Radiation Area Was Left Unattended & Entrance Was Not Secured W/Designated Special cal-core Locks Prior to Leaving Area Unguarded ML20198N6561997-12-30030 December 1997 Insp Repts 50-324/97-14 & 50-325/97-14 on 971209-12. Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Controls,Miscellaneous Radiation Protection & Chemistry Issues & Mgt Meetings IR 05000324/19970141997-12-30030 December 1997 Insp Repts 50-324/97-14 & 50-325/97-14 on 971209-12. Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Controls,Miscellaneous Radiation Protection & Chemistry Issues & Mgt Meetings ML20198P0561997-12-23023 December 1997 NOV from Insp Completed on 971113.Violation Noted:Licensee Failed to Promptly Correct Condition Adverse to Quality Re Unit 1 High Drywell Temp Condition ML20197H1691997-12-0808 December 1997 Notice of Violation from Insp on 970928-1108.Violation Noted:On 970923,torus Master clearance,2-97-555 Was Not Adequate to Prevent Draining of Water Into Unit 2 Torus 1999-09-15 |
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j June 4, 1982 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PN0-II-82-61A 1
This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verifi-cation or evaluation, and is basically all that is known by IE staff on this date.
FACILITY: Carolina Power & Light Company Licensee Emergency Classification:
Brunswick Units 1 & 2 Notification of Unusual Event Docket Nos. 50-324 and 50-325 Alert Southport, North Carolina Site Area Emergency i General Emergency X Not Applicable
SUBJECT:
UPDATE ON LICENSEE REPORT OF P0TENTIAL SABOTAGE This infonnation updates PN0-II-82-61, issued June 3.
l In discussions with Region II, the licensee has identified actions being taken to assure the adequacy of plant prctection, pending final resolution of concerns associated with the identification of bent incore neutron range monitoring tubes beneath the Unit 2 reactor vessel.
The actions, which are the subject of a Confirmation of Action letter, are:
Prior to Unit 1 startup, the licensee will:
Verify proper alignment in accessible areas, of the components of seven emergency core cooling systems (ECCS).
-- Conduct a detailed inspection of safety-related electrical panels and cabinets.
l, l -- Review procedures for access control of contractor personnel to vital areas.
4
-- Conduct walkthrough inspections of all accessible areas and valves for evidence of l abnormal conditions.
i l
In addition, the following interim operational and security surveillance measures will be initiated:
-- The licensee will conduct daily walkthrough inspections and verifications of critical valve and electrical alignments for emergency core cooling systems. ,
-- Two edditional security patrols will be implemented on each shift.
The licensee estimates completion of these actions by noon today. Unit I restart is expected to begin in early afternoon.
These conditions also apply to Unit 2, presently scheduled for startup in July.
The resident inspectors and the Region II security inspectors and investigators at the site will continue to monitor all licensee activities associated with the unexplained tube damage on Unit 2. .
The State of North Carolina, the IAT and the FBI have been kept informed.
8206170125 820604 PDR I&E PNO-II-82-061A PDR M"Q,k
Ifedii interest has not occurred. fleither the lic:nsee nor the flRC plans to issu: c ;
n:ws release at this time.
This information is current as of 10:30 a.m. (EDT) on June 4.
Contact:
A. K. liardin, RII 242-5589 C. W. Burger, RII 242-5538 DISTRIBUTI0rl: M' H. Street titlBB Phillips E/W Willste f1 AIL:
Chairman Palladino EDO tlRR IE fillSS - Adit:DitB Conm. Gilinsky PA OIA RES DOT: Trans Only Comm. Ahearne fiPA AELD Applicable State Comm. Roberts ELD Comm. Asselstine Air Rights I!1P0 SECY SP NSAC ACRS CA PDR Regions:
Licensee: / 3 , < 35 (Reactor Licensees)
Applicable Resident Site