Letter Sequence Other |
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Results
Other: A02357, Ro:On 820629,primary to Secondary Leakage Rate Increased. Caused by Erosion & Thermal Cycling.Prompt Corrective Action Initiated for Leakage in Excess of 0.5 Gpm Per Steam Generator, B10581, Describes Activities Currently Planned for 1983 Refueling Outage to Assure Continued Operability of Steam Generators. Any Licensing Action Will Be Initiated in Time to Support Scheduled 830416 Outage, B10672, Ro:On 830131,increased Primary to Secondary Leakage Rate Noted in Steam Generator 1.Caused by Expected Erosion in Leakage Area & Thermal Cycling Due to Power Transients & Plant Trips.Leakage Rate Measurements on 830202 Listed, ML20054C168, ML20054F221, ML20072H501
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MONTHYEARML20054C1681982-04-0707 April 1982 Ro:On 820323,during Reactor Trip from Full Power Operating Conditions,Baseline primary-to-secondary Leakage Rates Increased.Caused by Increased Steam Generator Activity Due to Trip.Equilibrium Operation in Mode 1 Achieved on 820326 Project stage: Other ML20054F2211982-06-0202 June 1982 Forwards Cycle 5 Refueling Outage Steam Generator Profilometry Insp Results,Per Util .Results Confirm Integrity of Steam Generator Tubes & Supports & Assure Continued Applicability of Design Basis Analyses Project stage: Other A02357, Ro:On 820629,primary to Secondary Leakage Rate Increased. Caused by Erosion & Thermal Cycling.Prompt Corrective Action Initiated for Leakage in Excess of 0.5 Gpm Per Steam Generator1982-07-0909 July 1982 Ro:On 820629,primary to Secondary Leakage Rate Increased. Caused by Erosion & Thermal Cycling.Prompt Corrective Action Initiated for Leakage in Excess of 0.5 Gpm Per Steam Generator Project stage: Other B10581, Describes Activities Currently Planned for 1983 Refueling Outage to Assure Continued Operability of Steam Generators. Any Licensing Action Will Be Initiated in Time to Support Scheduled 830416 Outage1982-11-19019 November 1982 Describes Activities Currently Planned for 1983 Refueling Outage to Assure Continued Operability of Steam Generators. Any Licensing Action Will Be Initiated in Time to Support Scheduled 830416 Outage Project stage: Other B10672, Ro:On 830131,increased Primary to Secondary Leakage Rate Noted in Steam Generator 1.Caused by Expected Erosion in Leakage Area & Thermal Cycling Due to Power Transients & Plant Trips.Leakage Rate Measurements on 830202 Listed1983-02-10010 February 1983 Ro:On 830131,increased Primary to Secondary Leakage Rate Noted in Steam Generator 1.Caused by Expected Erosion in Leakage Area & Thermal Cycling Due to Power Transients & Plant Trips.Leakage Rate Measurements on 830202 Listed Project stage: Other ML20072H5011983-03-0101 March 1983 Proposed Tech Spec Revs Re Frequency of Steam Generator Inservice Insp Project stage: Other ML20071D7771983-03-0101 March 1983 Proposed Changes to Tech Spec 3.4.6.2.b,extending Time Period Which Plant Must Be in Cold Shutdown Following Determination That Unidentified RCS Leakage Exceeded 1.0 Gpm Limit Project stage: Request B10712, Application for Amend to License DPR-65,changing Tech Spec 3.4.6.2.b to Extend Time Period Which Plant Must Be in Cold Shutdown Following Determination That Unidentified RCS Leakage Exceeded 1.0 Gpm Limit1983-03-0101 March 1983 Application for Amend to License DPR-65,changing Tech Spec 3.4.6.2.b to Extend Time Period Which Plant Must Be in Cold Shutdown Following Determination That Unidentified RCS Leakage Exceeded 1.0 Gpm Limit Project stage: Request B10724, Application for Amend to License DPR-65,revising Tech Specs Re Steam Generator Inservice Insp1983-03-14014 March 1983 Application for Amend to License DPR-65,revising Tech Specs Re Steam Generator Inservice Insp Project stage: Request 1982-07-09
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Text
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April 7, 1982 g
D Docket No. 50-336 p
A02357 RECEIVED 9
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Director of Nuclear Reactor Regulation
(
saem Attn:
Mr. Robert A. Clark, Chief las
//
Operating Reactors Branch #3 g
U. S. Nuclear Regulatory Commission 4
Washington, D.C.
20555
Reference:
(1)
R. A. Clark letter to W. G. Counsil, dated March 5, 1982, transmitting Amendment No. 73 to Facility Operating License No. DPR-65.
Centlemen:
Millstone Nuclear Power Station, Unit No. 2 Baseline Primary-to-Secondary Leakage Rates In accordance with the reporting requirements of Technical Specification 3/4.7.1.4, Table 4.7-2, as issued in Reference (1) for Cycle 5 operation of Millstone Unit No. 2, Northeast Nuclear Energy Company (NNECO) hereby provides the following information.
The primary-to-secondary leakage rate in each steam generator has been determined to be:
0.012 gpm Steam Generator No. 1
<0.005 gpm Steam Generator No. 2 These leakage rate measurements were complete 3 in Mode 1 during steady state operating conditions at a power level of approximately 2700 MW(th).
The plant achieved equilibrium operation in Mode 1 on March 26, 1982.
Millstone Unit No. 2 tripped from full power operating conditions on March 23, 1982. As a result of this trip, the activity measured in the steam generators increased resulting in a change in the in-dicated leakage rate.
NNECO performed additional measurements of the primary-to-secondary leakage rates following this Plant trip in an effort to trend these variations.
O hl0 8204200169 820407 PDR ADOCK 05000336 S
PDR
o
, The results._f the additional leak rate measurements confirm that an increase in the indicated leak rate will occur after a Plant trip wi
subsequent decrease to a lower value upon return to steady sto.e operation. These additional leak rate determinations clearly demonstrate the effects of a Plant trip on the indicated primary-to-secondary leakage rate as well as the need to conduct leak rate measure-ments during periods of steady state, equilibrium operating conditions.
We trust you find this information satisfactory.
Very truly yours, NORTilEAST NUCLEAR ENERGY COMPANY A4Ld4 W. t. Counsil Senior Vice President
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