ML20052G166
| ML20052G166 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 05/06/1982 |
| From: | Roman T NIAGARA MOHAWK POWER CORP. |
| To: | |
| Shared Package | |
| ML20052G163 | List: |
| References | |
| NUDOCS 8205140368 | |
| Download: ML20052G166 (4) | |
Text
s' NIAGARA M0llAWK POWER CORPORATION NINE MILE POINT NUCLEAR STATION UNIT #1 NARRATIVE OF OPERATING EXPERIENCE-April 1982 The Station operated during the month of April 1982 with a monthly availability factor of 0.0% and a net design electrical capacity factor of 0.0%.
The Station was shut down March 19, 1982, for a scheduled maintenance outage.
The Station remains shut down due to Reactor Recirculation system piping cracks' found during Vessel flydro on March 23, 1982.
CLASS I WORK - MAINTENANCE - APRIL 1982 hR #16170 - Replaced rubber goods on Drywell vent and fill valve #201-32 4/13/82 WR #17274 - Disassembled #15 Recire. Pump - 4/14/82 WR #17264 - Replaced blowdown valve IBA-729 on #12 Inst. Air Compressor -
4/15/82-WR #14194 - Installed new scrapper rings on piston rod to #12 Inst. Air Comp. - 4/20/82 Preventative Maint. Procedure #N1-MPM-SA2 Ip t. Air Compressor Semi-Annual Inspection on #11 Compressor.- 4/20/82 Preventative Maint. Procedure #N1-MPM-SA2 Inst. Air Compressor Semi-Annual Inspection on #12 Compressor - 4/20/82 hR #16092 - Removed thermal sleeve from location 26 4/20/82 hR #16639 - Removed CRD from location 26 4/20/82.
hR #16091 - Disassembled #13 Recirc Pump - 4/22/82 hR #16134 - Overhauled snubber #40-IIS 4/23/82 i
WR #16024 - Installed new gasket on manhole to #111 moisture separator.
drain tank - 4/26/82 CLASS I WORK - INSTRUMENTATION AND CONTROL - APRIL 1982 WR #16136 - Drywell high press, gross failure ind. lamp on C Panel not resetting.
(Replaced Analog Card #10546 with new Card
- 10545.)
I
- 16201 - Inspect and test all I.R.M. cables under vessel - Replace where necessary.
(Tested all - no failures found.)
CLASS I WORK - ELECTRICAL - APRIL 1982 WR #9879 - #102 Diesel Generator Ground Alarm MO #2151 - Mark I Containment - 4cw Torus Temp.
N1-ST-W111 - 125 VDC Battery Pilot Cell Voltage and Specific Gravity Test 8205140368 820506 DR ADOCK 05000220 g
I 1-UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
S0.220 UNIT NAME 9 Mile Pt. 81 DATE 5/6/82 April 1982 COMPLETED BY T.W.
Rom m 4 thb REPORT MONTil TELEPilONE (3151343-2110 X1383 t
3
.3 na 5"
e ei
.2 E
g.E 'A Ligasee E r, c.,
Cause & Curreceive e
W.
Daic
{
3g g
,3g; Event aT Action to j 'g
$3 5
ji2y Report
- NG Prevent Recurrence 5
l 8206 820323 F
874.0 A
Major repairs continue on Recire.
piping, core offloaded to SFP.
l l
l i
1 I
2 3
4 F: Forced Reason:
MethoJ:
Exhibit G-Instructions S: Scheduled A Equipnient Failure (Explain) 1 Manual for Preparation of Dasa B Maintenance of Test 2 Manual Scrain.
Entry Sheets for Licensee C. Refueling 3-Automatic Scram.
Esent Report (LER) File (NUREG.
D Regulatory Restriction 4-Oiher (Explain) 0161)
E. Operator Training & Ucense Examination F. Administrative 5
G-Operational Error (Explain)
Exhibit 1 - Sanw Source til/77)
Il Other (Explain)
AVER AGE I) ALLY UNIT POh ER LEVEL 4
DOCK'ET NO.
0-220 UNIT 9 hfild Pt. #1 DATE 5/6/82 COMPLETED BY T.W. Roma TELEPilONE [315)I43-2110 X1383 MONTH April 1982.
DAY AVERACE DAILY POWER LEVEL DA ',
(MWe NetI
,VERAGE DAILY POWER LEVEL (MWeNet1 I
n' 37 0
2 0
IS 0
3 0
19 0
4 0
29 o
5 0
21 0
6 0
2 0
7 0
23 0-8 0
0 y
9 0
25 0
10 0
26 0
II O
27 0
12 O
3 0
13 0
0 29 14 o
30 0
IS 0
31 16 0
l INSTRUCTIONS On this format.hst the aserage daily unit power leselin MWe Net for each day m th reporim;: m.mi the nearest whole megsws:t, o
j
- P1177 l
t i
me h
OPERATING DATA REPORT DOCKET NO.
50-220
'CO. lPLETED BY !, DATE
-_R /MR, M 07
\\
r te TELEPllONE (315) 343 21 0 X1383 OPERATING STATL'S
- 1. Unit Name:
Nine Mile Point Unit #1 Not'5
- 2. Reporting Period:
04/01/82 to 04/30/82 t
1850 i
2 Licensed Thermal Pow er (alWt):
- 4. Nameplat.- Rating (Gross SlWe):
- 5. Desi;n Electries! Rating (Net AIWe):
bZU
- 6..\\laximum Dependable Capacity (Gross hlWe):
630
- 7. Stasimum Dependable Capacity (Net A!We):
--610
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7)Since Last Report. Gise Reasons:
- 9. Power Lesel To Which Restricted.If Any(Net $1We):
- 10. Reasons For Restrictions.lf Any:
9 This 5fonth Yr. to Date Cumuistise
- 11. Ilours in Reportin; Period 770.0 2880.0 109,536.0
- 12. Number Of Hours Reactor Was Critical 0.0 1874.0 81,305. E
- 13. Reactor Resene Shutdowr. Ilours 0.0 0.0 1,204.2
- 14. iiours Generatur On Line 0.0 1872.5 73,562.3
- 15. Unit Resene Shutdown lio::rs 0.0 0.0 20.4
- 16. Gross Thermal Energy Ger.uahd DIWII) 0.0 3,421,093.0 129,374,390.0
- 17. Gmu Electrical Ener;y Generated Othil)
Q A_ _ _. 1.169.791.0 42,743,090.0 IS. Net Electrical Energy Generated pihti) 0.0
_1,134,758.0 41,392,651.0
- 19. Qut Senice factor 0.0 65.0 71.7 20 'J dt Au:!:ba, F:::a:
0.0 65.0 71.7 2. L'.d! Capacity Tatter (L'd;.; 5 DC ;;ct) 0.0 64.6 61.9 22, Unit Capacity Facter (Using DER Net) 0.0 63.6 61.0
- 23. Unit Furced Outage Rate 100.0 31.8 9.1
- 24. Shutdowns Scheduled Oser Nest 6 5tunths (Type. Date.as.d Durathm uf Leh1:
- 25. If Shut Down At EnJ Of I:eport Per,ud.Estunated Date of Startup:
Mntch - 10RR
- 26. Unas In Test Status (Prior to Commercial Operation):
Forecast Achiesed INITIT L CRITICA LITY INITIA L ELECTRICITY CO\\t.\\1ERCI A L Ol'ER ATION (9/77 )
.