ML20050E236
| ML20050E236 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 04/30/1982 |
| From: | Zufelt E POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML20050E235 | List: |
| References | |
| NUDOCS 8204130128 | |
| Download: ML20050E236 (9) | |
Text
'
OPERATING DATA REPORT DOCKET NO. 50-333 DATE ADP11, 1982 COMPLETED BY E. Zurelt TELEPilONE (919942-9840 OPERATING STATUS
- 1. Unit Name:
Wit @nt"i'+
- 2. Reporting Period:
820101-820171
- 3. Licensed Thermal Power (MWt):
2436
- 4. Nameplate Rating (Gross MWe):
883 621
- 5. Design Electrical Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe): 030 810
- 7. Maximum Dependable Ca;9 city (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
NOME
- 9. Power Level To Which Restricted,if Any (Net MWe):
NONE
- 10. Reasons For Restrictions,If Any:
C This Month Yr..to Date Cumulatise I1. Ilours In Reporting Period 744 2160 58537
- 12. Number Of Ilours Reactor Was Critical 587.3 587.3 40138.5
- 13. Reactor Reserve Shutdown flours 0
0 o
- 14. Ilours Generator On-Line 501.5 501.5 36945 1
- 15. Unit Reserve Shutdown flours 0
0 0
- 16. Gross Thermal Energy Generated (MWil) 881502 881592 79282006
- 17. Gross Electrical Energy Generated (MWil) 296780 296780 27057390
- 18. Net Electrical Energy Generated (MWil) 287110 287110 26191840
- 19. Unit Service Factor 67.4%
23.2%
66.5%
- 20. Unit Availability Factor 67.47.
23 2%
66.5%
- 21. Unit Capecity Factor (Using MDC Net) 47.6%
16.4%
59.5%
- 22. Unit Capacity Factor (Using DER Net) 47.0%
16.2%
54.5%
- 23. Unit Forced Outage Rate 05.0%
05.0%
16.8%
- 24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each):
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved i
INITIA1. CRITICALITY INITIA L ELECTRICITY COMMERCIAL OPER ATION 8204130128 820407 PDR ADOCK 05000333 i
R ppg 3
o AVER AGE DAILY UNIT POWER LEVEL 50-333
~
DocKETNO.
UNIT. JAFNPP April, 1982 DATE E. Zufelt f
COMPLETED BY TELEPflONE (315)342-3840 MONTH March 1982 DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe Net)
(ywe.ge 3 1
0 37 q73 0
599 2
is 0
666 3
j, 0
20 592 4
0 5
21 720 756 0
22 6
0 794 7
23 774 0
7, s
752 50 25 46 736 to 26 104 504 1:
27 530 215 28 12 583 231 2,
13 747 265 3,
14 797 427 3,
15 556 16 SLM4ARY:
Unit was returned to service at 2355 March 9, 1982 following the fourth refueling outage. The unit tripped at 0616 March 10, 1982 due to a clogged filter to number 2 main stop valve. Unit was returned to service at 0830 bhrch 11,1982.
l
UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKETNO. WW UNIT N AME MWP DATE At:ril, 1902 March 1982 COMPLETED BY (E ZutNt REPORT MONTH TELEPilONE S15I$42-3040 e.
E E
5?
j YE Licensee
,E v, j"3 E
Cause & Corrective N..
Date g
3g 4
jjE Event gi gO Action to 6-f5 5
j@g Report a mV g
Prevent Recurrence 6
12 811031 S
215 9 C
1 N/A N/A N/A Refueling outage (cumulative hours 3118.6).
1 820310 F
26.6 A
3 N/A HA Filter Dirty filter to number 2 main stop valve.
2 820326 S
0 H
4 N/A N/A N/A Reduced power for relief valve testing.
I 2
3 4
F: Forced Reason:
Method:
Exhibit G -Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2 Manual Scram.
Entry Sheets for Licensee C Refueling 3 Automatic Scram.
Event Report (LER) File (NUREG-D Regulatory Rest iction 4 Other (Explain) 0161)
E-Operator Training & License Examination F Administrative 5
G-Operational Error (Explain)
Exhibit I Same Source 1101her (Explain)
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT l
NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE MARCH, 1982 The refueling outage was completed on March 9, 1982 and the unit was returned to service at approximately 2355 hours0.0273 days <br />0.654 hours <br />0.00389 weeks <br />8.960775e-4 months <br />. At 0615 hours0.00712 days <br />0.171 hours <br />0.00102 weeks <br />2.340075e-4 months <br /> the unit tripped because of a dirty filter on the EHC hydraulic line to the number 2 main stop valve.
The filter was replaced and the unit was placed on line at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on March 11, 1982. Power was increased at the preconditioning rate.
On March 26, 1982 power was reduced for relief valve testing.
i
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL & MECHANICAL MAINTENANCE
SUMMARY
MARCH 1982 REO DATE SYSTEM HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE T ME HOURS 2/26 29 14718 IEDRO Body to bonnet & packing Repaired as required 140.5 M7/-74 leaks 2/18 02-2 16124 loose nuts Torqued nuts 96.5 Reirc. Supports ISI 2/20 29 15144 ISI Incse bolt Tightened bolt 63.75 1C-1.li-24 2/20 02 16780 HYDRO Packing leak Torqued packirg 22 MOV-53B 2/21 29 16611 HYDRO Pecking leak Repacked 26 f."GT-402 2/20 10 16790 HYDRO Packing leak Torqued packing 87.5 RHR-81B 2/20 13 14715 If/DRO Packing leak Torqued packing 84 MOV-15 2/20 10 14717 IWDRO Packing leak Torqued packing 14 M7/-18 2/20 02 16779 OPS Pilot seat leakage Sent to Wyle, repaired & reset full 96.4 SRV-71G flow test 2/20 02 16778 OPS /IEDRO Pilot seat leakage Sent to Wyle - reset & full flow test 147.5 SFV-71C 2/20 23 15)64 HYDRO Body to bonnet & packing Installed new pressure seal - repacked 782 MG'-15 leak
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED ELECTRICAL a MECHANICAL MAINTENANCE
SUMMARY
MARCH 1982 DATE SYSTEM HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE T
2/13 16 15200 WA None Removed hatches for Torus modification 314.5 X200A, B, C 2/22 10 16889 RHR-42D OPS Loose dise nut Replaced nut & pin 99 2/23 23 12419 TU-2 OPS Damagad insulation Repaired insulation 289 5
-r-
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
I&C MARG 1982 (Tl WORK REQUEST #
CAUSE OF RESULTS OF DATE SYSTEM HOW DETECTED E
TIME COMPONENT #
MALFUNCTION MALFUNCTION RECURRENCE HOURS 11265 Valves had been Adjusted stroke 3/1/82 02 Aav-17,1S OPS re-worked Eeat leakage on valves 16 13256 Repaired 3/2/82 02 w a-71J OPS Loose connector Spurious alarms connector 2
13280 3/1/82 02 W3-71A JIC Broken detector No response Replaced 2
detector Bad cable and Replaced 3/2/82 02 13281 JIC pre-anp No response defective 1
WR 71M C ""*" D Unable to connect 13342
@ css threaded test equipment Replace drain 2
3/5/82 02 PS-134A JIC 7alve valve 13958 Jefective 60 cycle hum Replaced sensors 10 3/2/82 02 WE-71G OPS sensor 14209 Bias set high on Set bias per OPS Wa-D, J, G, H ST limits 1
3/3/82 02 wa-71D OPS 1/A Possible leaky Irw output from Tightened 14229 bypass on 110E flow unit A packing on bypass 6
3/5/82 02 Flow Unit A JIC Timing / test card Will not pass 14287 defective OPS ST Replaced card 6
3/5/82 02 RSCS OPS 14351 Corrected bias to D
E, OPS N/A Out of range 60%
1
- -7 k h'g 3/9/82 02 Blown output Output reads Replaced 3/26/82 02-3 18538 OPS transistor zero square rooter 20 l
1 SOX-74.T 1
l
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
I&C MARCH 1982 WORK REQUEST #
CAUSE OF RESULTS OF ACTION TAKEN REPAIR DATE SYSTEM HOW DETECTED COMPONENT #
MALFUNCTION MALFUNCTION R CU RE RS 14267 Defective IC Dual full in/ full Replaced G-33, 3/18/82 03 ROD 10-23 OPS G-33 out indication Q-16, R-39 5
16664 10" dif. between None, calibrated 3/4/82 05 SCRAM OPS LI-94 & LIS-101 for different None 12 clant conditiorm 13254 Possible dirt in Applied high m-A TS nne r
pera n
mltg 16 3/3/82 07 13285 Cable pulled out Dicontinuity in Replaced cable &
3/4/82 07 IRM-E JIC of connector cable or detector detection 32 cnnnections 13376 Dirty jewel in Over current 3/3/82 10 RHR-P-3D OPS relay annunciator on Cleaned relay 16 14226 Static buildup 3/5/82 10 FI-132A, B OPS on meter case Meters erratic Washed cases 3
14295 Holding screws on 13-A0V-32 open Tightened 3/6/82 13 LS-74 OPS switch loose with no hi-lo holding screws 8
annunciator 13351 Detector slipped Broken tip on Replaced 3/5/82 17 RE-458A OPS while deconning gaseous detector A detector assembly 5
18515 Monitor reading 3/22/82 17 PN-251A OPS Age of detectors high Changed setpoints 1
18604 Monitor not Out of Calibrated using 3/30/82 17 RIS - 431 JIC ggaty g calibration latest rev 8
13299 Change of Time ccr5 tant too Moved snubbers 3/12/82 23 DPIS 76 & 77 JIC set point low from lo-hi side 1
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
I&C MARCH 1982 (T
WORK REQUEST #
CAUSE OF RESULTS OF DATE SYSTEM HOW DETECTED E U TIME COMPONENT #
MALFUNCTION MALFUNCTION RECURRENCE HOURS 16793 Original set Set points out of Recalibrated to 3/2/82 23 DPIS-76 & 77 OPS points incorrect tolerance new set points 5
16843 Set points Out of Calibrated to new 3/16/82 23 DPIS-76 JIC updated calibration set points 4
18400 Test data 3/12/82 23 HPCI Sys OPS N/A N/A collected 10 18415 Faulty snubber HPCI isolates on' Replaced 3/17/82 23 HPCI Sys OPS pins hi steam flow snubber pins 2
18433 Out of Calibrated DPIS-3/17/82 23 DPIS-77 JIC Set points updated calibration gnewset 18406 Loose hose Unable to sa:rple Tightened hose 3/15/82 27 DWA PA OPS connections 02 &H2 connection /
4 calibrated 14181 Switch arm out of 90% switch for Reset switch ann 3/2/82 29 90% switch OPS position AOV-80A inop.
per ISP-65-1 4
.